GTG incident on 2021-11-19 — TX

Operator
Columbia Gas Transmission, Llc
Cause
Equipment Failure
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$125
Incident datetime
2021-11-19 01:20
Report number
Location
TX
Narrative
Coco compressor station's emergency shutdown system (esd) blowdown valve (6"- bdv#:197) unintentionally opened at 1:02am on november 19, 2021 and released 4370 mcf of natural gas through the esd blow-down stack for approximately18 minutes before the valve was manually closed. The operating pressure at the time of the release was 916 psig. The station operator was on-site during the event and was able to isolate the station piping and stop the release. As part of the preliminary investigation, ice/moisture was found in the pilot control valve of the blow-down actuator valve, potentially caused the event. The isolated esd facilities were returned back to service at 4:01 am est after the pilot control valve associated sensing lines were cleared of moisture/ice and inspected.
Detailed record list
Report Received Date
2021-12-14 00:00:00
Iyear
2021
Report Number
20210115
Supplemental Number
36140
Report Type
Supplemental Final
Operator Id
Name
Columbia Gas Transmission, Llc
Operator Street Address
700 Louisiana St. Suite 700
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2021-11-19 01:20:00
Time Zone
Eastern
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2021-11-19 03:21:00
Additional Nrc Report Numbers
1322509
Commodity Released Type
Natural Gas
Unintentional Release
4370
Intentional Release
0
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Status When Identified
Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2021-11-19 01:38:00
Restart Datetime
2021-11-19 04:01:00
Communication State Fed Ind
No
Ignite Ind
No
Num Pub Evacuated
0
Incident Identified Datetime
2021-11-19 01:20:00
On Site Datetime
2021-11-19 01:50:00
On Off Shore
Onshore
Onshore State Abbreviation
Wv
Onshore Postal Code
25156
Onshore City Name
Pinch
Onshore County Name
Kanawha
Designated Location
Not Applicable
Pipe Fac Name
Coco Compressor Station
Federal
No
Location Type
Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
System Part Involved
Onshore Compressor Station Equipment And Piping
Item Involved
Esd System, But Excluding Product Drain Lines And Tubing
Installation Year
Unknown
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Release Involved An Emergency Shutdown System (Esd) Blow-Down Valve And Blow-Off Stack, Design To Safely Evacuate Gas From The Station.
Class Location Type
Class 2 Location
Could Be Hca
No
Pir Radius
276
Heat Damage Ind
No
Non Heat Damage Ind
No
Did Occur In Mca Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
24297
Est Cost Intentional Release
0
Est Cost Prop Damage
125
Est Cost Emergency
350
Est Cost Other
0
Gas Cost In Mcf
5.56
Prpty
24772
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Wildlife Impact Ind
No
Accident Psig
916
Gas Flow In Pipe In Mcf
0
Mop Psig
1000
Mop Cfr Section
192.619(A)(1)
Maop Established Date
2007-11-30 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Gas Required Odorized Ind
No
Pipeline Function
Transmission In Storage Field
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
No
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Investigation was not deemed necessary based on having an operator/responder (employee) on-site during the event and actions of the control room played a minor role during the response efforts.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Esd System Failure Ind
Yes
Eq Additional Other Ind
Yes
Eq Additional Other Details
Possibly Moisture In The Valve Actuator Sensing Line.
Preparer Name
C********** L L***
Preparer Title
Us Regulatory Compliance Specialist
Preparer Email
C*********@t*******.com
Preparer Telephone
304-545-4350
Local Contact Name
C********** L L***
Local Contact Email
C*********@t*******.com
Local Contact Telephone
304-545-4350
Authorizer Name
L** R*****
Authorizer Title
Director Us Regulatory Compliance
Authorizer Telephone
832-320-5315
Authorizer Email
L*********@t*******.com
Narrative
Coco compressor station's emergency shutdown system (esd) blowdown valve (6"- bdv#:197) unintentionally opened at 1:02am on november 19, 2021 and released 4370 mcf of natural gas through the esd blow-down stack for approximately18 minutes before the valve was manually closed. The operating pressure at the time of the release was 916 psig. The station operator was on-site during the event and was able to isolate the station piping and stop the release. As part of the preliminary investigation, ice/moisture was found in the pilot control valve of the blow-down actuator valve, potentially caused the event. The isolated esd facilities were returned back to service at 4:01 am est after the pilot control valve associated sensing lines were cleared of moisture/ice and inspected.
Report Received Date 2021-12-14 00:00:00
Iyear 2021
Report Number 20210115
Supplemental Number 36140
Report Type Supplemental Final
Operator Id 2616 PHMSA Enforcement
Name Columbia Gas Transmission, Llc
Operator Street Address 700 Louisiana St. Suite 700
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2021-11-19 01:20:00
Time Zone Eastern
Daylight Savings Ind Yes
Location Latitude 38.401907 Google Maps OpenStreetMap
Location Longitude -81.41727 Google Maps OpenStreetMap
Nrc Rpt Num 1322483 NRC Report How to search
Nrc Rpt Datetime 2021-11-19 03:21:00
Additional Nrc Report Numbers 1322509
Commodity Released Type Natural Gas
Unintentional Release 4370
Intentional Release 0
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Status When Identified Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind Yes
Shutdown Datetime 2021-11-19 01:38:00
Restart Datetime 2021-11-19 04:01:00
Communication State Fed Ind No
Ignite Ind No
Num Pub Evacuated 0
Incident Identified Datetime 2021-11-19 01:20:00
On Site Datetime 2021-11-19 01:50:00
On Off Shore Onshore
Onshore State Abbreviation Wv
Onshore Postal Code 25156
Onshore City Name Pinch
Onshore County Name Kanawha
Designated Location Not Applicable
Pipe Fac Name Coco Compressor Station
Federal No
Location Type Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
System Part Involved Onshore Compressor Station Equipment And Piping
Item Involved Esd System, But Excluding Product Drain Lines And Tubing
Installation Year Unknown
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Other
Release Type Details Release Involved An Emergency Shutdown System (Esd) Blow-Down Valve And Blow-Off Stack, Design To Safely Evacuate Gas From The Station.
Class Location Type Class 2 Location
Could Be Hca No
Pir Radius 276
Heat Damage Ind No
Non Heat Damage Ind No
Did Occur In Mca Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 24297
Est Cost Intentional Release 0
Est Cost Prop Damage 125
Est Cost Emergency 350
Est Cost Other 0
Gas Cost In Mcf 5.56
Prpty 24772
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Wildlife Impact Ind No
Accident Psig 916
Gas Flow In Pipe In Mcf 0
Mop Psig 1000
Mop Cfr Section 192.619(A)(1) View CFR 49 §192
Maop Established Date 2007-11-30 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Gas Required Odorized Ind No
Pipeline Function Transmission In Storage Field
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind No
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Investigation was not deemed necessary based on having an operator/responder (employee) on-site during the event and actions of the control room played a minor role during the response efforts.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Esd System Failure Ind Yes
Eq Additional Other Ind Yes
Eq Additional Other Details Possibly Moisture In The Valve Actuator Sensing Line.
Preparer Name C********** L L***
Preparer Title Us Regulatory Compliance Specialist
Preparer Email C*********@t*******.com
Preparer Telephone 304-545-4350
Local Contact Name C********** L L***
Local Contact Email C*********@t*******.com
Local Contact Telephone 304-545-4350
Authorizer Name L** R*****
Authorizer Title Director Us Regulatory Compliance
Authorizer Telephone 832-320-5315
Authorizer Email L*********@t*******.com
Narrative Coco compressor station's emergency shutdown system (esd) blowdown valve (6"- bdv#:197) unintentionally opened at 1:02am on november 19, 2021 and released 4370 mcf of natural gas through the esd blow-down stack for approximately18 minutes before the valve was manually closed. The operating pressure at the time of the release was 916 psig. The station operator was on-site during the event and was able to isolate the station piping and stop the release. As part of the preliminary investigation, ice/moisture was found in the pilot control valve of the blow-down actuator valve, potentially caused the event. The isolated esd facilities were returned back to service at 4:01 am est after the pilot control valve associated sensing lines were cleared of moisture/ice and inspected.

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