GTG incident on 2021-11-12 — NE

Operator
Northern Natural Gas Co
Cause
Incorrect Operation
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,700,181
Incident datetime
2021-11-12 10:30
Report number
Location
NE
Narrative
On november 12, 2021, new valves were being manipulated for commisioning and lubrication. At 10:30, a 30 inch bypass valve was manipulated when then ground was reported to raise and settle with a muffled sound. The on-site personnel evacuated the location to report the event. Initial reporting did not see any pressure changes on scada, and due to extremley high winds, no visual or audible indications could be made of venting gas. A plan was created to reduce pressure to 600 pounds for the b, c and d lines as they were all in common at the location. At 21:00, it was reported that as technicians approached the valve setting, the lel monitoring equipment detected gas approximately 100 yards upwind of the valve assembly. The pipeline was isolated at 1555 on november 14, 2021. Excavation of the valve found that a 1.5 inch diameter body bleed plug was missing, concluding it was not installed or improperly installed.
Detailed record list
Report Received Date
2021-12-01 00:00:00
Iyear
2021
Report Number
20210110
Supplemental Number
36591
Report Type
Supplemental Final
Operator Id
Name
Northern Natural Gas Co
Operator Street Address
1111 South 103rd Street
Operator City Name
Omaha
Operator State Abbreviation
NE
Operator Postal Code
68124
Local Datetime
2021-11-12 21:00:00
Time Zone
Central
Daylight Savings Ind
No
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2021-11-12 22:05:00
Additional Nrc Report Numbers
1321930
Commodity Released Type
Natural Gas
Unintentional Release
8375
Intentional Release
2975
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Status When Identified
Post-Construction Commissioning
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Initial Responder Com Datetime
2021-11-12 22:05:00
Ignite Ind
No
Upstream Action Taken
Operational Control
Upstream Oprtnl Cntrl Detail
Pressure Was Reduced Upstream To Safely Approach The Location.
Downstream Action Taken
Operational Control
Downstream Oprtnl Cntrl Detail
Pressure Was Reduced Upstream To Safely Approach The Location.
Num Pub Evacuated
3
Incident Identified Datetime
2021-11-12 10:30:00
On Site Datetime
2021-11-12 10:30:00
On Off Shore
Onshore
Onshore State Abbreviation
Ia
Onshore Postal Code
50122
Onshore City Name
Not Within A Municipality
Onshore County Name
Hardin
Designated Location
Milepost
Designated Name
21.78
Pipe Fac Name
30" Loop Line From Ogden Compressor Station
Segment Name
M521d
Federal
No
Location Type
Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Other Underground Facilities
No
Crossing
No
Pipe Facility Type
Interstate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
2021
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Body Bleed Plug Was Missing, Causing The Location Of The Release.
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
692
Heat Damage Ind
No
Non Heat Damage Ind
No
Did Occur In Mca Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
39446
Est Cost Intentional Release
14012
Est Cost Prop Damage
1700181
Est Cost Emergency
840
Est Cost Other
0
Gas Cost In Mcf
4.71
Prpty
1754479
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
2
Num Business Building Affctd
0
Wildlife Impact Ind
No
Accident Psig
800
Gas Flow In Pipe In Mcf
211
Mop Psig
1000
Mop Cfr Section
192.619(A)(2)
Maop Established Date
1997-11-01 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Gas Required Odorized Ind
No
Length Segment Isolated
44246
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Control room had no impact to the incident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Equipment Not Installed Properly
Operation Type
Equipment Not Installed Properly
Related Failure Follow Ind
Yes
Category Type
Construction
Operator Qualification Ind
No
Io Not Installed Properly Ind
Yes
Io Follow Procedure Ind
Yes
Preparer Name
D**** C*******
Preparer Email
D*************@n****.com
Preparer Telephone
402-398-7439
Authorizer Name
T** C******
Authorizer Telephone
402-398-7715
Authorizer Email
T*************@n****.com
Narrative
On november 12, 2021, new valves were being manipulated for commisioning and lubrication. At 10:30, a 30 inch bypass valve was manipulated when then ground was reported to raise and settle with a muffled sound. The on-site personnel evacuated the location to report the event. Initial reporting did not see any pressure changes on scada, and due to extremley high winds, no visual or audible indications could be made of venting gas. A plan was created to reduce pressure to 600 pounds for the b, c and d lines as they were all in common at the location. At 21:00, it was reported that as technicians approached the valve setting, the lel monitoring equipment detected gas approximately 100 yards upwind of the valve assembly. The pipeline was isolated at 1555 on november 14, 2021. Excavation of the valve found that a 1.5 inch diameter body bleed plug was missing, concluding it was not installed or improperly installed.
Report Received Date 2021-12-01 00:00:00
Iyear 2021
Report Number 20210110
Supplemental Number 36591
Report Type Supplemental Final
Operator Id 13750 PHMSA Enforcement
Name Northern Natural Gas Co
Operator Street Address 1111 South 103rd Street
Operator City Name Omaha
Operator State Abbreviation NE
Operator Postal Code 68124
Local Datetime 2021-11-12 21:00:00
Time Zone Central
Daylight Savings Ind No
Location Latitude 42.282001 Google Maps OpenStreetMap
Location Longitude -93.28154 Google Maps OpenStreetMap
Nrc Rpt Num 1321904 NRC Report How to search
Nrc Rpt Datetime 2021-11-12 22:05:00
Additional Nrc Report Numbers 1321930
Commodity Released Type Natural Gas
Unintentional Release 8375
Intentional Release 2975
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Status When Identified Post-Construction Commissioning
Communication State Fed Ind Yes
Party Initiated Communication Operator
Initial Responder Com Datetime 2021-11-12 22:05:00
Ignite Ind No
Upstream Action Taken Operational Control
Upstream Oprtnl Cntrl Detail Pressure Was Reduced Upstream To Safely Approach The Location.
Downstream Action Taken Operational Control
Downstream Oprtnl Cntrl Detail Pressure Was Reduced Upstream To Safely Approach The Location.
Num Pub Evacuated 3
Incident Identified Datetime 2021-11-12 10:30:00
On Site Datetime 2021-11-12 10:30:00
On Off Shore Onshore
Onshore State Abbreviation Ia
Onshore Postal Code 50122
Onshore City Name Not Within A Municipality
Onshore County Name Hardin
Designated Location Milepost
Designated Name 21.78
Pipe Fac Name 30" Loop Line From Ogden Compressor Station
Segment Name M521d
Federal No
Location Type Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Other Underground Facilities No
Crossing No
Pipe Facility Type Interstate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 2021
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Other
Release Type Details Body Bleed Plug Was Missing, Causing The Location Of The Release.
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 692
Heat Damage Ind No
Non Heat Damage Ind No
Did Occur In Mca Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 39446
Est Cost Intentional Release 14012
Est Cost Prop Damage 1700181
Est Cost Emergency 840
Est Cost Other 0
Gas Cost In Mcf 4.71
Prpty 1754479
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 2
Num Business Building Affctd 0
Wildlife Impact Ind No
Accident Psig 800
Gas Flow In Pipe In Mcf 211
Mop Psig 1000
Mop Cfr Section 192.619(A)(2) View CFR 49 §192
Maop Established Date 1997-11-01 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Gas Required Odorized Ind No
Length Segment Isolated 44246
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Control room had no impact to the incident.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Equipment Not Installed Properly
Operation Type Equipment Not Installed Properly
Related Failure Follow Ind Yes
Category Type Construction
Operator Qualification Ind No
Io Not Installed Properly Ind Yes
Io Follow Procedure Ind Yes
Preparer Name D**** C*******
Preparer Email D*************@n****.com
Preparer Telephone 402-398-7439
Authorizer Name T** C******
Authorizer Telephone 402-398-7715
Authorizer Email T*************@n****.com
Narrative On november 12, 2021, new valves were being manipulated for commisioning and lubrication. At 10:30, a 30 inch bypass valve was manipulated when then ground was reported to raise and settle with a muffled sound. The on-site personnel evacuated the location to report the event. Initial reporting did not see any pressure changes on scada, and due to extremley high winds, no visual or audible indications could be made of venting gas. A plan was created to reduce pressure to 600 pounds for the b, c and d lines as they were all in common at the location. At 21:00, it was reported that as technicians approached the valve setting, the lel monitoring equipment detected gas approximately 100 yards upwind of the valve assembly. The pipeline was isolated at 1555 on november 14, 2021. Excavation of the valve found that a 1.5 inch diameter body bleed plug was missing, concluding it was not installed or improperly installed.

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