GTG incident on 2021-08-09 — TX

Operator
Boardwalk Texas Intrastate, Llc
Cause
Equipment Failure
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$463,318
Incident datetime
2021-08-09 13:30
Report number
Location
TX
Narrative
On 8/9/2021, a gulf south technician who was taking routine rectifier readings in an area that had recently received rain, noticed minor bubbling on the pipeline right-of-way. The technician checked for and identified two minor leaks approximately 30 feet apart. On 9/14/2021, the site was excavated and the leaks were identified as grade 2 leaks. Gulf south anticipated installing weld over sleeves but, after excavating, determined to replace approximately 40 feet of pipe instead. Arrangements are currently being made to perform the pipe replacement; the leaks are being monitored. The line is not isolated because these are minor leaks and the line serves two city gates. Arrangements are being made to supply temporary gas during the pipe replacement. Part a, question 10 shows 1 mcf of gas loss but it was actually so minimal it could not be measured. 2/10/2022 update repair cost and submit final report. During the repair timeframe, a third pinhole leak was discovered and was repaired as part of the pipe replacement that was already being done. Repairs were completed by pipe replacement on 11/4/2021.
Detailed record list
Report Received Date
2021-10-05 00:00:00
Iyear
2021
Report Number
20210085
Supplemental Number
36330
Report Type
Supplemental Final
Operator Id
Name
Boardwalk Texas Intrastate, Llc
Operator Street Address
9 Greenway Plaza Suite 2800
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77046
Local Datetime
2021-09-14 18:10:00
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2021-09-14 18:10:00
Additional Nrc Report Numbers
1317005
Commodity Released Type
Natural Gas
Unintentional Release
1
Intentional Release
0
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Status When Identified
Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind
No
Shutdown Explain
Minor Leak; Securing Temporary Gas To Keep 2 City Gates In Service
Communication State Fed Ind
No
Ignite Ind
No
Upstream Action Taken
Operational Control
Upstream Oprtnl Cntrl Detail
No Action Was Taken. This Is Minor Leak Only Reportable Because The Repair Cost Will Meet Threshold.
Downstream Action Taken
Operational Control
Downstream Oprtnl Cntrl Detail
No Action Was Taken. This Is Minor Leak Only Reportable Because The Repair Cost Will Meet Threshold.
Num Pub Evacuated
0
Incident Identified Datetime
2021-08-09 13:30:00
On Site Datetime
2021-08-09 13:30:00
On Off Shore
Onshore
Onshore State Abbreviation
Tx
Onshore Postal Code
78377
Onshore City Name
Not Within A Municipality
Onshore County Name
Refugio
Designated Location
Survey Station No.
Designated Name
1592+13
Pipe Fac Name
White Point Field To Refugio
Segment Name
Index 46
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
40
Other Underground Facilities
No
Crossing
No
Pipe Facility Type
Intrastate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Other
Item Involved Details
Dresser Coupling
Installation Year
1927
Manufactured Year
1927
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
201
Heat Damage Ind
No
Non Heat Damage Ind
No
Did Occur In Mca Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
4
Est Cost Intentional Release
0
Est Cost Prop Damage
463318
Est Cost Emergency
0
Est Cost Other
0
Gas Cost In Mcf
3.68
Prpty
463322
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Wildlife Impact Ind
No
Accident Psig
250
Gas Flow In Pipe In Mcf
100
Mop Psig
310
Mop Cfr Section
Maop Established Date
1971-03-12 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Gas Required Odorized Ind
No
Length Segment Isolated
26400
Internal Inspection Ind
No
Other Inspection Ind
Yes
Internal Inspection Details
Dresser Coupling
Operation Complications Ind
Yes
Other Complications Ind
Yes
Inspect Comp Details
Could Only Displace Gas To Atmosphere
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Threaded Connection/coupling Failure
Eq Failure Type
Threaded Connection/coupling Failure
Other Stripped Ind
Mechanical Coupling
Eq Additional Other Ind
Yes
Eq Additional Other Details
Dresser Seals Leaking
Preparer Name
S****** M********
Preparer Title
Pa Oq And Event Program Leader
Preparer Email
S****************@b**********.com
Preparer Telephone
270-903-5764
Authorizer Name
T*** B****
Authorizer Title
Manager Compliance Services
Authorizer Telephone
270-314-6547
Authorizer Email
T*********@b**********.com
Narrative
On 8/9/2021, a gulf south technician who was taking routine rectifier readings in an area that had recently received rain, noticed minor bubbling on the pipeline right-of-way. The technician checked for and identified two minor leaks approximately 30 feet apart. On 9/14/2021, the site was excavated and the leaks were identified as grade 2 leaks. Gulf south anticipated installing weld over sleeves but, after excavating, determined to replace approximately 40 feet of pipe instead. Arrangements are currently being made to perform the pipe replacement; the leaks are being monitored. The line is not isolated because these are minor leaks and the line serves two city gates. Arrangements are being made to supply temporary gas during the pipe replacement. Part a, question 10 shows 1 mcf of gas loss but it was actually so minimal it could not be measured. 2/10/2022 update repair cost and submit final report. During the repair timeframe, a third pinhole leak was discovered and was repaired as part of the pipe replacement that was already being done. Repairs were completed by pipe replacement on 11/4/2021.
Report Received Date 2021-10-05 00:00:00
Iyear 2021
Report Number 20210085
Supplemental Number 36330
Report Type Supplemental Final
Operator Id 39701 PHMSA Enforcement
Name Boardwalk Texas Intrastate, Llc
Operator Street Address 9 Greenway Plaza Suite 2800
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77046
Local Datetime 2021-09-14 18:10:00
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 28.308802 Google Maps OpenStreetMap
Location Longitude -97.299034 Google Maps OpenStreetMap
Nrc Rpt Num 1316767 NRC Report How to search
Nrc Rpt Datetime 2021-09-14 18:10:00
Additional Nrc Report Numbers 1317005
Commodity Released Type Natural Gas
Unintentional Release 1
Intentional Release 0
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Status When Identified Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind No
Shutdown Explain Minor Leak; Securing Temporary Gas To Keep 2 City Gates In Service
Communication State Fed Ind No
Ignite Ind No
Upstream Action Taken Operational Control
Upstream Oprtnl Cntrl Detail No Action Was Taken. This Is Minor Leak Only Reportable Because The Repair Cost Will Meet Threshold.
Downstream Action Taken Operational Control
Downstream Oprtnl Cntrl Detail No Action Was Taken. This Is Minor Leak Only Reportable Because The Repair Cost Will Meet Threshold.
Num Pub Evacuated 0
Incident Identified Datetime 2021-08-09 13:30:00
On Site Datetime 2021-08-09 13:30:00
On Off Shore Onshore
Onshore State Abbreviation Tx
Onshore Postal Code 78377
Onshore City Name Not Within A Municipality
Onshore County Name Refugio
Designated Location Survey Station No.
Designated Name 1592+13
Pipe Fac Name White Point Field To Refugio
Segment Name Index 46
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 40
Other Underground Facilities No
Crossing No
Pipe Facility Type Intrastate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Other
Item Involved Details Dresser Coupling
Installation Year 1927
Manufactured Year 1927
Material Involved Carbon Steel
Release Type Leak
Leak Type Connection Failure
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 201
Heat Damage Ind No
Non Heat Damage Ind No
Did Occur In Mca Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 4
Est Cost Intentional Release 0
Est Cost Prop Damage 463318
Est Cost Emergency 0
Est Cost Other 0
Gas Cost In Mcf 3.68
Prpty 463322
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Wildlife Impact Ind No
Accident Psig 250
Gas Flow In Pipe In Mcf 100
Mop Psig 310
Mop Cfr Section 192.619(C) View CFR 49 §192
Maop Established Date 1971-03-12 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Gas Required Odorized Ind No
Length Segment Isolated 26400
Internal Inspection Ind No
Other Inspection Ind Yes
Internal Inspection Details Dresser Coupling
Operation Complications Ind Yes
Other Complications Ind Yes
Inspect Comp Details Could Only Displace Gas To Atmosphere
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Threaded Connection/coupling Failure
Eq Failure Type Threaded Connection/coupling Failure
Other Stripped Ind Mechanical Coupling
Eq Additional Other Ind Yes
Eq Additional Other Details Dresser Seals Leaking
Preparer Name S****** M********
Preparer Title Pa Oq And Event Program Leader
Preparer Email S****************@b**********.com
Preparer Telephone 270-903-5764
Authorizer Name T*** B****
Authorizer Title Manager Compliance Services
Authorizer Telephone 270-314-6547
Authorizer Email T*********@b**********.com
Narrative On 8/9/2021, a gulf south technician who was taking routine rectifier readings in an area that had recently received rain, noticed minor bubbling on the pipeline right-of-way. The technician checked for and identified two minor leaks approximately 30 feet apart. On 9/14/2021, the site was excavated and the leaks were identified as grade 2 leaks. Gulf south anticipated installing weld over sleeves but, after excavating, determined to replace approximately 40 feet of pipe instead. Arrangements are currently being made to perform the pipe replacement; the leaks are being monitored. The line is not isolated because these are minor leaks and the line serves two city gates. Arrangements are being made to supply temporary gas during the pipe replacement. Part a, question 10 shows 1 mcf of gas loss but it was actually so minimal it could not be measured. 2/10/2022 update repair cost and submit final report. During the repair timeframe, a third pinhole leak was discovered and was repaired as part of the pipe replacement that was already being done. Repairs were completed by pipe replacement on 11/4/2021.

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