GD incident on 2021-08-26 — AZ

Operator
Southwest Gas Corp
Cause
Pipe, Weld, Or Joint Failure
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 4 injuries
Property damage (nominal)
$43,129
Incident datetime
2021-08-26 09:55
Report number
Location
AZ, MARICOPA
Narrative
Pl 2021-0128 southwest gas corporation (swg) responded to a reported fire at 4940 west ray road in chandler called in by the fire department at 09:30. Swg construction technician responded to find a strip-mall that appeared to be damaged by an explosion. Fire department reported that four people were transported to the hospital with injuries. Swg crews responded and controlled the flow of gas by squeezing the 2-inch plastic pipeline that supplies gas to the commercial property resulting in an outage of seven active accounts (six commercial and one residential). Notification was made to PHMSA via the national response center (nrc) on august 26, 2021 at 11:09 and was given nrc report #1314811. An update was provided to the nrc on august 27, 2021 at 11:31 and was given nrc report #1314910. Notification was made to chemical safety and hazard investigation board (csb) on august 26,2021 at 12:05. The apparent leak cause is listed as g5 - pipe, weld, or joint failure. The incident investigation is still ongoing, and a supplemental report will be submitted upon completion of the investigation by swg. Note: for part a, #10, the estimated volume of gas released that is identified represents an estimate that presumes a crack that is leaking at 56 psi, beginning at the time of the initial report of the incident and ending at the time the pipeline was shut down. However, the actual amount of gas loss is unknown because the time the gas pipeline began leaking is unknown. Supplemental report: laboratory data analysis shows the leak was caused by thermal-oxidative degradation extending from the inner wall to the mid-wall of the tubing that resulted in a through-wall axial crack. Section g5 was updated from "slit crack" to "thermal-oxidative degradation".
Detailed record list
Occurred At
2021-08-26 09:55:00
Year
2021
Report Received Date
2021-09-20 00:00:00
Iyear
2021.0
Report Number
20210080.0
Supplemental Number
37226.0
Report Type
Supplemental Final
Operator Id
Name
Southwest Gas Corp
Operator Street Address
8360 S. Durango Drive
Operator City Name
Las Vegas
Operator State Abbreviation
NV
Operator Postal Code
89113
Local Datetime
2021-08-26 09:30:00
Time Zone
Mountain
Daylight Savings Ind
No
Location Street Address
4940 West Ray Road
Location City Name
Chandler
Location County Name
Maricopa
Location State Abbreviation
AZ
Location Postal Code
85226
Location Latitude
Location Longitude
Flow Cont Squeeze Off Ind
Yes
Nrc Rpt Datetime
2021-08-26 00:00:00
Nrc Rpt Num
Additional Nrc Report Numbers
1314910
Commodity Released Type
Natural Gas
Unintentional Release
7.0
Intentional Release
0.0
Fatality Ind
No
Fatal
0
Injury Ind
Yes
Num Emp Injuries
0
Num Contr Injuries
0
Num Er Injuries
0
Num Worker Injuries
0
Num Gp Injuries
4
Injure
4
Ignite Ind
Yes
Ignite Datetime
2021-08-26 09:30:00
How Extinguished
Allowed To Burn Out
Gas Consumed By Fire In Mcf
7
Explode Ind
Yes
Num Pub Evacuated
20.0
Incident Identified Datetime
2021-08-26 09:55:00
On Site Datetime
2021-08-26 09:55:00
Federal
No
Location Type
Private Property
Incident Area Type
Underground
Incident Area Subtype
Under Pavement
Depth Of Cover
44.0
Other Underground Facilities
No
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Service
Installation Year
1999.0
Customer Type
Non-Residential With Meter Capacity Less Than 1,000 Scfh
Was Efv Installed Before Ind
No
Curb Valve Inst Before Inc Ind
No
Pipe Diameter
1.0
Pipe Specification
Astm D2513
Pipe Manufacturer
Phillips
Material Involved
Plastic
Plastic Type
Polyethylene (Pe)
Plastic Sdr
11
Material Pe Pipe Code
3408
Release Type
Leak
Leak Type
Crack
Class Location Type
Class 3 Location
Est Cost Oper Paid
5000000.0
Est Cost Prop Damage
43129.0
Est Cost Emergency
4000.0
Est Cost Other
0.0
Gas Cost In Mcf
38.57
Est Cost Unintentional Release
270.0
Est Cost Intentional Release
0.0
Prpty
5047399.0
Commercial Affected
6.0
Industrial Affected
0.0
Residences Affected
1.0
Num Persons Hosp Not Ovnght
0.0
Num Injured Treated By Emt
0.0
Num Resident Building Affctd
1.0
Num Business Building Affctd
6.0
Accident Psig
56.0
Normal Psig
56.0
Mop Psig
60.0
Mop Cfr Section
192.619(A)(2)
Maop Established Date
1999-07-12 00:00:00
Accident Pressure
Pressure Did Not Exceed Maop
Gas Odorized System Type
None
Gas Odorized Level
0.3
Scada In Place Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Pipe, Weld, Or Joint Failure
Cause Details
Body Of Pipe
Pwjf Failure Type
Body Of Pipe
Pipe Body Subtype
Crack
Additional Crack Ind
Yes
Result Material Ind
Yes
Result Material Subtype
Other
Result Material Details
Thermal-Oxidative Degradation
Hydrotest Conducted Ind
No
Preparer Name
S**** B****
Preparer Title
Administrator Division Compliance
Preparer Email
S**********@s****.com
Preparer Telephone
602-484-5489
Preparer Fax
602-484-5322
Local Contact Name
S**** B****
Local Contact Email
S**********@s****.com
Local Contact Telephone
602-484-5489
Authorizer Name
R***** M****
Authorizer Title
Director Central Support
Authorizer Telephone
602-484-5367
Authorizer Email
R***********@s****.com
Narrative
Pl 2021-0128 southwest gas corporation (swg) responded to a reported fire at 4940 west ray road in chandler called in by the fire department at 09:30. Swg construction technician responded to find a strip-mall that appeared to be damaged by an explosion. Fire department reported that four people were transported to the hospital with injuries. Swg crews responded and controlled the flow of gas by squeezing the 2-inch plastic pipeline that supplies gas to the commercial property resulting in an outage of seven active accounts (six commercial and one residential). Notification was made to PHMSA via the national response center (nrc) on august 26, 2021 at 11:09 and was given nrc report #1314811. An update was provided to the nrc on august 27, 2021 at 11:31 and was given nrc report #1314910. Notification was made to chemical safety and hazard investigation board (csb) on august 26,2021 at 12:05. The apparent leak cause is listed as g5 - pipe, weld, or joint failure. The incident investigation is still ongoing, and a supplemental report will be submitted upon completion of the investigation by swg. Note: for part a, #10, the estimated volume of gas released that is identified represents an estimate that presumes a crack that is leaking at 56 psi, beginning at the time of the initial report of the incident and ending at the time the pipeline was shut down. However, the actual amount of gas loss is unknown because the time the gas pipeline began leaking is unknown. Supplemental report: laboratory data analysis shows the leak was caused by thermal-oxidative degradation extending from the inner wall to the mid-wall of the tubing that resulted in a through-wall axial crack. Section g5 was updated from "slit crack" to "thermal-oxidative degradation".
Occurred At 2021-08-26 09:55:00
Year 2021
Report Received Date 2021-09-20 00:00:00
Iyear 2021.0
Report Number 20210080.0
Supplemental Number 37226.0
Report Type Supplemental Final
Operator Id 18536 PHMSA Enforcement
Name Southwest Gas Corp
Operator Street Address 8360 S. Durango Drive
Operator City Name Las Vegas
Operator State Abbreviation NV
Operator Postal Code 89113
Local Datetime 2021-08-26 09:30:00
Time Zone Mountain
Daylight Savings Ind No
Location Street Address 4940 West Ray Road
Location City Name Chandler
Location County Name Maricopa
Location State Abbreviation AZ
Location Postal Code 85226
Location Latitude 33.32135 Google Maps OpenStreetMap
Location Longitude -111.92575 Google Maps OpenStreetMap
Flow Cont Squeeze Off Ind Yes
Nrc Rpt Datetime 2021-08-26 00:00:00
Nrc Rpt Num 1314811 NRC Report How to search
Additional Nrc Report Numbers 1314910
Commodity Released Type Natural Gas
Unintentional Release 7.0
Intentional Release 0.0
Fatality Ind No
Fatal 0
Injury Ind Yes
Num Emp Injuries 0
Num Contr Injuries 0
Num Er Injuries 0
Num Worker Injuries 0
Num Gp Injuries 4
Injure 4
Ignite Ind Yes
Ignite Datetime 2021-08-26 09:30:00
How Extinguished Allowed To Burn Out
Gas Consumed By Fire In Mcf 7
Explode Ind Yes
Num Pub Evacuated 20.0
Incident Identified Datetime 2021-08-26 09:55:00
On Site Datetime 2021-08-26 09:55:00
Federal No
Location Type Private Property
Incident Area Type Underground
Incident Area Subtype Under Pavement
Depth Of Cover 44.0
Other Underground Facilities No
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Service
Installation Year 1999.0
Customer Type Non-Residential With Meter Capacity Less Than 1,000 Scfh
Was Efv Installed Before Ind No
Curb Valve Inst Before Inc Ind No
Pipe Diameter 1.0
Pipe Specification Astm D2513
Pipe Manufacturer Phillips
Material Involved Plastic
Plastic Type Polyethylene (Pe)
Plastic Sdr 11
Material Pe Pipe Code 3408
Release Type Leak
Leak Type Crack
Class Location Type Class 3 Location
Est Cost Oper Paid 5000000.0
Est Cost Prop Damage 43129.0
Est Cost Emergency 4000.0
Est Cost Other 0.0
Gas Cost In Mcf 38.57
Est Cost Unintentional Release 270.0
Est Cost Intentional Release 0.0
Prpty 5047399.0
Commercial Affected 6.0
Industrial Affected 0.0
Residences Affected 1.0
Num Persons Hosp Not Ovnght 0.0
Num Injured Treated By Emt 0.0
Num Resident Building Affctd 1.0
Num Business Building Affctd 6.0
Accident Psig 56.0
Normal Psig 56.0
Mop Psig 60.0
Mop Cfr Section 192.619(A)(2) View CFR 49 §192
Maop Established Date 1999-07-12 00:00:00
Accident Pressure Pressure Did Not Exceed Maop
Gas Odorized System Type None
Gas Odorized Level 0.3
Scada In Place Ind No
Accident Identifier Notification From Emergency Responder
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Pipe, Weld, Or Joint Failure
Cause Details Body Of Pipe
Pwjf Failure Type Body Of Pipe
Pipe Body Subtype Crack
Additional Crack Ind Yes
Result Material Ind Yes
Result Material Subtype Other
Result Material Details Thermal-Oxidative Degradation
Hydrotest Conducted Ind No
Preparer Name S**** B****
Preparer Title Administrator Division Compliance
Preparer Email S**********@s****.com
Preparer Telephone 602-484-5489
Preparer Fax 602-484-5322
Local Contact Name S**** B****
Local Contact Email S**********@s****.com
Local Contact Telephone 602-484-5489
Authorizer Name R***** M****
Authorizer Title Director Central Support
Authorizer Telephone 602-484-5367
Authorizer Email R***********@s****.com
Narrative Pl 2021-0128 southwest gas corporation (swg) responded to a reported fire at 4940 west ray road in chandler called in by the fire department at 09:30. Swg construction technician responded to find a strip-mall that appeared to be damaged by an explosion. Fire department reported that four people were transported to the hospital with injuries. Swg crews responded and controlled the flow of gas by squeezing the 2-inch plastic pipeline that supplies gas to the commercial property resulting in an outage of seven active accounts (six commercial and one residential). Notification was made to PHMSA via the national response center (nrc) on august 26, 2021 at 11:09 and was given nrc report #1314811. An update was provided to the nrc on august 27, 2021 at 11:31 and was given nrc report #1314910. Notification was made to chemical safety and hazard investigation board (csb) on august 26,2021 at 12:05. The apparent leak cause is listed as g5 - pipe, weld, or joint failure. The incident investigation is still ongoing, and a supplemental report will be submitted upon completion of the investigation by swg. Note: for part a, #10, the estimated volume of gas released that is identified represents an estimate that presumes a crack that is leaking at 56 psi, beginning at the time of the initial report of the incident and ending at the time the pipeline was shut down. However, the actual amount of gas loss is unknown because the time the gas pipeline began leaking is unknown. Supplemental report: laboratory data analysis shows the leak was caused by thermal-oxidative degradation extending from the inner wall to the mid-wall of the tubing that resulted in a through-wall axial crack. Section g5 was updated from "slit crack" to "thermal-oxidative degradation".

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