GD incident on 2021-07-16 — GA

Operator
Atlanta Gas Light Co
Cause
Excavation Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$20,000
Incident datetime
2021-07-16 14:14
Report number
Location
GA, CHEROKEE
Narrative
A 2-inch steel natural gas main was ruptured near its tap on a 4-inch steel main by a t&j industries contract crew while installing sewer main by boring. Once the incident was made safe and the costs associated with the incident was being tallied it was determined that required milling and resurfacing repairs to the highway by the local government, repairs to the affected pipeline and emergency response would exceed the $122,000 threshold for reporting where the timeline for question a4 was met above and the national response center (nrc) was contacted at that time. Notification to the one-call center was made where the main was correctly located, however, the excavator failed to attempt to pothole where the facility was marked and damaged. Additional nrc report number 1311561 was created for the same event after a supplemental call was placed with the nrc to update the initial telephonic notice.
Detailed record list
Occurred At
2021-07-16 14:14:00
Year
2021
Report Received Date
2021-08-12 00:00:00
Iyear
2021.0
Report Number
20210069.0
Supplemental Number
36093.0
Report Type
Supplemental Final
Operator Id
Name
Atlanta Gas Light Co
Operator Street Address
10 Peachtree Place Ne
Operator City Name
Atlanta
Operator State Abbreviation
GA
Operator Postal Code
30309
Local Datetime
2021-07-16 14:14:00
Time Zone
Eastern
Daylight Savings Ind
Yes
Location Street Address
10385 Hickory Flat Highway
Location City Name
Woodstock
Location County Name
Cherokee
Location State Abbreviation
GA
Location Postal Code
30188
Location Latitude
Location Longitude
Flow Cont Key Crit Ind
Yes
Flow Cont Squeeze Off Ind
Yes
Nrc Rpt Datetime
2021-07-21 10:38:00
Nrc Rpt Num
Additional Nrc Report Numbers
1311561
Commodity Released Type
Natural Gas
Unintentional Release
4900.0
Intentional Release
0.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2021-07-16 14:14:00
On Site Datetime
2021-07-16 14:33:00
Federal
No
Location Type
Public Property
Incident Area Type
Underground
Incident Area Subtype
Under Pavement
Depth Of Cover
111.0
Other Underground Facilities
No
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
1979.0
Pipe Diameter
2.0
Pipe Specification
Api 5l
Pipe Manufacturer
Unknown
Material Involved
Steel
Steel Seam Type
Seamless
Wt Steel
0.154
Release Type
Mechanical Puncture
Puncture Axial
3.0
Puncture Circum
0.5
Class Location Type
Class 3 Location
Est Cost Oper Paid
100000.0
Est Cost Prop Damage
20000.0
Est Cost Emergency
20000.0
Est Cost Other
0.0
Gas Cost In Mcf
3.57
Est Cost Unintentional Release
17493.0
Est Cost Intentional Release
0.0
Prpty
157493.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
2.0
Num Persons Hosp Not Ovnght
0.0
Num Injured Treated By Emt
0.0
Num Resident Building Affctd
2.0
Num Business Building Affctd
0.0
Accident Psig
190.0
Normal Psig
230.0
Mop Psig
300.0
Mop Cfr Section
192.619(A)(2)
Maop Established Date
1979-08-08 00:00:00
Accident Pressure
Pressure Did Not Exceed Maop
Gas Odorized System Type
Injection Pump
Gas Odorized Level
11.3
Scada In Place Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
State Law Exempt Ind
No
Notify Cga Dirt
Yes
Public Row Ind
Yes
Public Subtype
County Road
Excavator Type
Contractor
Excavator Equipment
Boring
Work Performed
Sewer (Sanitary/storm)
One Call Notified Ind
Yes
One Call Ticket Num
2.10428e+11
Locator Type
Contract Locator
Visible Marks
Yes
Service Interruption
Yes
Service Interruption Hours
12.0
Root Cause Category
Excavation Issue
Root Cause Type
Improper Excavation Practice Not Listed Above
Preparer Name
R**** M*******
Preparer Title
Lead Compliance Engineer
Preparer Email
R*******@s*********.com
Preparer Telephone
(404) 584-3733
Preparer Fax
(404) 584-4710
Authorizer Name
R*** S*****
Authorizer Title
Director Compliance And Qa
Authorizer Telephone
(404) 584-4910
Authorizer Email
R******@s*********.com
Narrative
A 2-inch steel natural gas main was ruptured near its tap on a 4-inch steel main by a t&j industries contract crew while installing sewer main by boring. Once the incident was made safe and the costs associated with the incident was being tallied it was determined that required milling and resurfacing repairs to the highway by the local government, repairs to the affected pipeline and emergency response would exceed the $122,000 threshold for reporting where the timeline for question a4 was met above and the national response center (nrc) was contacted at that time. Notification to the one-call center was made where the main was correctly located, however, the excavator failed to attempt to pothole where the facility was marked and damaged. Additional nrc report number 1311561 was created for the same event after a supplemental call was placed with the nrc to update the initial telephonic notice.
Occurred At 2021-07-16 14:14:00
Year 2021
Report Received Date 2021-08-12 00:00:00
Iyear 2021.0
Report Number 20210069.0
Supplemental Number 36093.0
Report Type Supplemental Final
Operator Id 792 PHMSA Enforcement
Name Atlanta Gas Light Co
Operator Street Address 10 Peachtree Place Ne
Operator City Name Atlanta
Operator State Abbreviation GA
Operator Postal Code 30309
Local Datetime 2021-07-16 14:14:00
Time Zone Eastern
Daylight Savings Ind Yes
Location Street Address 10385 Hickory Flat Highway
Location City Name Woodstock
Location County Name Cherokee
Location State Abbreviation GA
Location Postal Code 30188
Location Latitude 34.12315 Google Maps OpenStreetMap
Location Longitude -84.392014 Google Maps OpenStreetMap
Flow Cont Key Crit Ind Yes
Flow Cont Squeeze Off Ind Yes
Nrc Rpt Datetime 2021-07-21 10:38:00
Nrc Rpt Num 1311350 NRC Report How to search
Additional Nrc Report Numbers 1311561
Commodity Released Type Natural Gas
Unintentional Release 4900.0
Intentional Release 0.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2021-07-16 14:14:00
On Site Datetime 2021-07-16 14:33:00
Federal No
Location Type Public Property
Incident Area Type Underground
Incident Area Subtype Under Pavement
Depth Of Cover 111.0
Other Underground Facilities No
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Main
Installation Year 1979.0
Pipe Diameter 2.0
Pipe Specification Api 5l
Pipe Manufacturer Unknown
Material Involved Steel
Steel Seam Type Seamless
Wt Steel 0.154
Release Type Mechanical Puncture
Puncture Axial 3.0
Puncture Circum 0.5
Class Location Type Class 3 Location
Est Cost Oper Paid 100000.0
Est Cost Prop Damage 20000.0
Est Cost Emergency 20000.0
Est Cost Other 0.0
Gas Cost In Mcf 3.57
Est Cost Unintentional Release 17493.0
Est Cost Intentional Release 0.0
Prpty 157493.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 2.0
Num Persons Hosp Not Ovnght 0.0
Num Injured Treated By Emt 0.0
Num Resident Building Affctd 2.0
Num Business Building Affctd 0.0
Accident Psig 190.0
Normal Psig 230.0
Mop Psig 300.0
Mop Cfr Section 192.619(A)(2) View CFR 49 §192
Maop Established Date 1979-08-08 00:00:00
Accident Pressure Pressure Did Not Exceed Maop
Gas Odorized System Type Injection Pump
Gas Odorized Level 11.3
Scada In Place Ind No
Accident Identifier Notification From Emergency Responder
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind Yes
One Call System Ind Yes
State Law Exempt Ind No
Notify Cga Dirt Yes
Public Row Ind Yes
Public Subtype County Road
Excavator Type Contractor
Excavator Equipment Boring
Work Performed Sewer (Sanitary/storm)
One Call Notified Ind Yes
One Call Ticket Num 2.10428e+11
Locator Type Contract Locator
Visible Marks Yes
Service Interruption Yes
Service Interruption Hours 12.0
Root Cause Category Excavation Issue
Root Cause Type Improper Excavation Practice Not Listed Above
Preparer Name R**** M*******
Preparer Title Lead Compliance Engineer
Preparer Email R*******@s*********.com
Preparer Telephone (404) 584-3733
Preparer Fax (404) 584-4710
Authorizer Name R*** S*****
Authorizer Title Director Compliance And Qa
Authorizer Telephone (404) 584-4910
Authorizer Email R******@s*********.com
Narrative A 2-inch steel natural gas main was ruptured near its tap on a 4-inch steel main by a t&j industries contract crew while installing sewer main by boring. Once the incident was made safe and the costs associated with the incident was being tallied it was determined that required milling and resurfacing repairs to the highway by the local government, repairs to the affected pipeline and emergency response would exceed the $122,000 threshold for reporting where the timeline for question a4 was met above and the national response center (nrc) was contacted at that time. Notification to the one-call center was made where the main was correctly located, however, the excavator failed to attempt to pothole where the facility was marked and damaged. Additional nrc report number 1311561 was created for the same event after a supplemental call was placed with the nrc to update the initial telephonic notice.

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