GD incident on 2021-05-22 — NE

Operator
Black Hills Energy
Cause
Excavation Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$10,000
Incident datetime
2021-05-22 09:39
Report number
Location
NE, LANCASTER
Narrative
Road and bridge work were being done by k2 construction for the city of lincoln ne on the n 27th street bridge crossing salt creek. Black hills energy (bhe) has a 6-inch steel distribution main attached and supported under the bridge. K2 construction had an 811 locate ticket to do excavate at this location. This main was accurately located by bhe prior to the incident. The main transitioned from the bridge to go underground on the north side where it was hit. Prior to incident, bhe was preparing to install stopple fittings and valves on the north and south side of this bridge crossing. The intent was to be able to isolate the section of main on the bridge to allow a quick and safe way to stop gas flow if any damage occurred during bridge repair. K2 construction was aware of the gas main on the north side and bhe's effort to install valves did not wait for bhe to finish installation. On saturday may 22nd, k2 construction continued with this project and dug in the tolerance zone with an excavator directly over the pipeline. This punctured the 6-inch main causing a 1.5-inch by 3-inch hole allowing blowing natural gas to escape to atmosphere. 911 was called by the excavator and lincoln police and fire department came on scene to control traffic and offer support for bhe throughout the incident. Bhe arrived with personnel to safely monitor, control the blowing gas, and make repairs. A nebraska state fire marshal deputy inspector also responded to this incident to monitor and investigate. Stopple fittings were welded on the south and north side of the bridge to stop flow of gas. A bypass was installed to maintain gas supply to a large residential area north of the bridge. Once the bypass was completed, the stopples were inserted to stop the blowing gas. Gas blew for approximately 14 hours and the area was monitored by bhe and fire department personnel throughout the incident until repairs could be made. The damaged section of main was replaced, pipeline re-pressured and bypass removed. Poor excavation practices resulted in the incident.
Detailed record list
Occurred At
2021-05-22 09:39:00
Year
2021
Report Received Date
2021-06-22 00:00:00
Iyear
2021.0
Report Number
20210057.0
Supplemental Number
35419.0
Report Type
Original Final
Operator Id
Name
Black Hills Energy
Operator Street Address
2287 College Road Po Box 2006
Operator City Name
Council Bluffs
Operator State Abbreviation
IA
Operator Postal Code
51502
Local Datetime
2021-05-28 08:30:00
Time Zone
Central
Daylight Savings Ind
Yes
Location Street Address
N 27th St And Fairfield St
Location City Name
Lincoln
Location County Name
Lancaster
Location State Abbreviation
NE
Location Postal Code
68521
Location Latitude
Location Longitude
Flow Cont Stopple Fitng Ind
Yes
Nrc Rpt Datetime
2021-05-28 09:04:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
4033.49
Intentional Release
0.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Num Pub Evacuated
2.0
Incident Identified Datetime
2021-05-22 09:39:00
Communication State Fed Ind
Yes
Party Initiated Communication
Local/state/federal Emergency Responder
Initial Responder Com Datetime
2021-05-22 10:20:00
On Site Datetime
2021-05-22 10:20:00
Federal
No
Location Type
Public Property
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Depth Of Cover
36.0
Other Underground Facilities
No
Crossing
Yes
Bridge Crossing Ind
Yes
Bridge Type
Uncased
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
1986.0
Pipe Diameter
6.0
Pipe Specification
Unknown
Pipe Manufacturer
Unknown
Material Involved
Steel
Steel Seam Type
Seamless
Wt Steel
0.156
Release Type
Mechanical Puncture
Puncture Axial
1.5
Puncture Circum
3.0
Class Location Type
Class 3 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
10000.0
Est Cost Emergency
10000.0
Est Cost Other
1000.0
Est Cost Other Details
All Costs Of Repair Have Not Been Fully Estimated
Gas Cost In Mcf
4.3972
Est Cost Unintentional Release
17736.0
Est Cost Intentional Release
0.0
Prpty
38736.0
Commercial Affected
1.0
Industrial Affected
0.0
Residences Affected
9.0
Num Persons Hosp Not Ovnght
0.0
Num Injured Treated By Emt
0.0
Num Resident Building Affctd
0.0
Num Business Building Affctd
1.0
Accident Psig
70.0
Normal Psig
70.0
Mop Psig
74.0
Mop Cfr Section
192.619(A)(1)
Maop Established Date
1986-08-28 00:00:00
Accident Pressure
Pressure Did Not Exceed Maop
Gas Odorized System Type
Combination Of Odorization Types
Gas Odorized Lvl Not Msrd Ind
Yes
Scada In Place Ind
No
Accident Identifier
Notification From Third Party That Caused The Incident
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The control room was not a factor in this excavation damage
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
Excavator Ind
Yes
State Law Exempt Ind
No
Notify Cga Dirt
No
Public Row Ind
Yes
Public Subtype
City Street
Excavator Type
Contractor
Excavator Equipment
Backhoe/trackhoe
Work Performed
Road Work
One Call Notified Ind
Yes
One Call Ticket Num
211303017
Locator Type
Contract Locator
Visible Marks
Yes
Service Interruption
Yes
Service Interruption Hours
12.0
Root Cause Category
Excavation Issue
Root Cause Type
Excavator Failed To Maintain Clearance After Verifying Marks
Preparer Name
T** D********
Preparer Title
Pipeline Safety Professional
Preparer Email
T************@b*************.com
Preparer Telephone
402 858 3602
Local Contact Name
S*** A* P*******
Authorizer Name
T** D********
Authorizer Title
Pipeline Safety Professional
Authorizer Telephone
402 858 3602
Authorizer Email
T************@b*************.com
Narrative
Road and bridge work were being done by k2 construction for the city of lincoln ne on the n 27th street bridge crossing salt creek. Black hills energy (bhe) has a 6-inch steel distribution main attached and supported under the bridge. K2 construction had an 811 locate ticket to do excavate at this location. This main was accurately located by bhe prior to the incident. The main transitioned from the bridge to go underground on the north side where it was hit. Prior to incident, bhe was preparing to install stopple fittings and valves on the north and south side of this bridge crossing. The intent was to be able to isolate the section of main on the bridge to allow a quick and safe way to stop gas flow if any damage occurred during bridge repair. K2 construction was aware of the gas main on the north side and bhe's effort to install valves did not wait for bhe to finish installation. On saturday may 22nd, k2 construction continued with this project and dug in the tolerance zone with an excavator directly over the pipeline. This punctured the 6-inch main causing a 1.5-inch by 3-inch hole allowing blowing natural gas to escape to atmosphere. 911 was called by the excavator and lincoln police and fire department came on scene to control traffic and offer support for bhe throughout the incident. Bhe arrived with personnel to safely monitor, control the blowing gas, and make repairs. A nebraska state fire marshal deputy inspector also responded to this incident to monitor and investigate. Stopple fittings were welded on the south and north side of the bridge to stop flow of gas. A bypass was installed to maintain gas supply to a large residential area north of the bridge. Once the bypass was completed, the stopples were inserted to stop the blowing gas. Gas blew for approximately 14 hours and the area was monitored by bhe and fire department personnel throughout the incident until repairs could be made. The damaged section of main was replaced, pipeline re-pressured and bypass removed. Poor excavation practices resulted in the incident.
Occurred At 2021-05-22 09:39:00
Year 2021
Report Received Date 2021-06-22 00:00:00
Iyear 2021.0
Report Number 20210057.0
Supplemental Number 35419.0
Report Type Original Final
Operator Id 15359 PHMSA Enforcement
Name Black Hills Energy
Operator Street Address 2287 College Road Po Box 2006
Operator City Name Council Bluffs
Operator State Abbreviation IA
Operator Postal Code 51502
Local Datetime 2021-05-28 08:30:00
Time Zone Central
Daylight Savings Ind Yes
Location Street Address N 27th St And Fairfield St
Location City Name Lincoln
Location County Name Lancaster
Location State Abbreviation NE
Location Postal Code 68521
Location Latitude 40.8473585 Google Maps OpenStreetMap
Location Longitude -96.6822531 Google Maps OpenStreetMap
Flow Cont Stopple Fitng Ind Yes
Nrc Rpt Datetime 2021-05-28 09:04:00
Nrc Rpt Num 1306246 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 4033.49
Intentional Release 0.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Num Pub Evacuated 2.0
Incident Identified Datetime 2021-05-22 09:39:00
Communication State Fed Ind Yes
Party Initiated Communication Local/state/federal Emergency Responder
Initial Responder Com Datetime 2021-05-22 10:20:00
On Site Datetime 2021-05-22 10:20:00
Federal No
Location Type Public Property
Incident Area Type Underground
Incident Area Subtype Exposed Due To Excavation
Depth Of Cover 36.0
Other Underground Facilities No
Crossing Yes
Bridge Crossing Ind Yes
Bridge Type Uncased
Pipe Facility Type Investor Owned
System Part Involved Main
Installation Year 1986.0
Pipe Diameter 6.0
Pipe Specification Unknown
Pipe Manufacturer Unknown
Material Involved Steel
Steel Seam Type Seamless
Wt Steel 0.156
Release Type Mechanical Puncture
Puncture Axial 1.5
Puncture Circum 3.0
Class Location Type Class 3 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 10000.0
Est Cost Emergency 10000.0
Est Cost Other 1000.0
Est Cost Other Details All Costs Of Repair Have Not Been Fully Estimated
Gas Cost In Mcf 4.3972
Est Cost Unintentional Release 17736.0
Est Cost Intentional Release 0.0
Prpty 38736.0
Commercial Affected 1.0
Industrial Affected 0.0
Residences Affected 9.0
Num Persons Hosp Not Ovnght 0.0
Num Injured Treated By Emt 0.0
Num Resident Building Affctd 0.0
Num Business Building Affctd 1.0
Accident Psig 70.0
Normal Psig 70.0
Mop Psig 74.0
Mop Cfr Section 192.619(A)(1) View CFR 49 §192
Maop Established Date 1986-08-28 00:00:00
Accident Pressure Pressure Did Not Exceed Maop
Gas Odorized System Type Combination Of Odorization Types
Gas Odorized Lvl Not Msrd Ind Yes
Scada In Place Ind No
Accident Identifier Notification From Third Party That Caused The Incident
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The control room was not a factor in this excavation damage
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind Yes
One Call System Ind Yes
Excavator Ind Yes
State Law Exempt Ind No
Notify Cga Dirt No
Public Row Ind Yes
Public Subtype City Street
Excavator Type Contractor
Excavator Equipment Backhoe/trackhoe
Work Performed Road Work
One Call Notified Ind Yes
One Call Ticket Num 211303017
Locator Type Contract Locator
Visible Marks Yes
Service Interruption Yes
Service Interruption Hours 12.0
Root Cause Category Excavation Issue
Root Cause Type Excavator Failed To Maintain Clearance After Verifying Marks
Preparer Name T** D********
Preparer Title Pipeline Safety Professional
Preparer Email T************@b*************.com
Preparer Telephone 402 858 3602
Local Contact Name S*** A* P*******
Authorizer Name T** D********
Authorizer Title Pipeline Safety Professional
Authorizer Telephone 402 858 3602
Authorizer Email T************@b*************.com
Narrative Road and bridge work were being done by k2 construction for the city of lincoln ne on the n 27th street bridge crossing salt creek. Black hills energy (bhe) has a 6-inch steel distribution main attached and supported under the bridge. K2 construction had an 811 locate ticket to do excavate at this location. This main was accurately located by bhe prior to the incident. The main transitioned from the bridge to go underground on the north side where it was hit. Prior to incident, bhe was preparing to install stopple fittings and valves on the north and south side of this bridge crossing. The intent was to be able to isolate the section of main on the bridge to allow a quick and safe way to stop gas flow if any damage occurred during bridge repair. K2 construction was aware of the gas main on the north side and bhe's effort to install valves did not wait for bhe to finish installation. On saturday may 22nd, k2 construction continued with this project and dug in the tolerance zone with an excavator directly over the pipeline. This punctured the 6-inch main causing a 1.5-inch by 3-inch hole allowing blowing natural gas to escape to atmosphere. 911 was called by the excavator and lincoln police and fire department came on scene to control traffic and offer support for bhe throughout the incident. Bhe arrived with personnel to safely monitor, control the blowing gas, and make repairs. A nebraska state fire marshal deputy inspector also responded to this incident to monitor and investigate. Stopple fittings were welded on the south and north side of the bridge to stop flow of gas. A bypass was installed to maintain gas supply to a large residential area north of the bridge. Once the bypass was completed, the stopples were inserted to stop the blowing gas. Gas blew for approximately 14 hours and the area was monitored by bhe and fire department personnel throughout the incident until repairs could be made. The damaged section of main was replaced, pipeline re-pressured and bypass removed. Poor excavation practices resulted in the incident.

All rights reserved. Copyright © by ClearPHMSA