GD incident on 2021-05-14 — MD

Operator
Baltimore Gas And Electric Company
Cause
Incorrect Operation
Commodity
Natural Gas
Program
GD
Damage and Injuries
1 fatality 1 injury
Property damage (nominal)
$20,689
Incident datetime
2021-05-14 17:00
Report number
Location
MD, BALTIMORE COUNTY
Narrative
At approximately 4 p.M. On may 14, 2021, a bge crew member received significant burns from a fire while installing a weld-over sleeve over a gas main coupling on a dead-end bypass. The steel gas main bypass was located at 8407 stevenson road, pikesville, maryland. Gas and electric crews immediately responded to the scene to isolate the trouble, mitigate risks, make repairs and restore service to 216 gas customers and area electric customers. The gas main was isolated by closing an upstream valve. The main was quickly repaired by cutting out this section of pipe and replacing with new steel piping. After an internal investigation by the company, it appears that the dead-end bypass section was not blocked/braced prior to cutting the restraining straps to perform the weld-over sleeve weld operation. The gas pressure force caused the non-restraining coupling to give way, which resulted in an uncontrolled release of gas with subsequent ignition from the welding equipment. Mitigating actions to prevent future recurrence include enhanced training pertaining to proper blocking and bracing, as well as modifications to further clarify gas construction standards.
Detailed record list
Occurred At
2021-05-14 17:00:00
Year
2021
Report Received Date
2021-06-18 00:00:00
Iyear
2021.0
Report Number
20210054.0
Supplemental Number
36370.0
Report Type
Supplemental Final
Operator Id
Name
Baltimore Gas And Electric Company
Operator Street Address
110 W Fayette St
Operator City Name
Baltimore
Operator State Abbreviation
MD
Operator Postal Code
21201
Local Datetime
2021-05-14 16:07:00
Time Zone
Eastern
Daylight Savings Ind
Yes
Location Street Address
8407 Stevenson Rd
Location City Name
Pikesville
Location County Name
Baltimore County
Location State Abbreviation
MD
Location Postal Code
21208
Location Latitude
Location Longitude
Flow Cont Main Valve Ind
Yes
Nrc Rpt Datetime
2021-06-14 18:18:00
Nrc Rpt Num
Additional Nrc Report Numbers
1305192
Commodity Released Type
Natural Gas
Unintentional Release
1464.0
Intentional Release
0.0
Fatality Ind
Yes
Num Emp Fatalities
1
Num Contr Fatalities
0
Num Er Fatalities
0
Num Worker Fatalities
0
Num Gp Fatalities
0
Fatal
1
Injury Ind
Yes
Num Emp Injuries
1
Num Contr Injuries
0
Num Er Injuries
0
Num Worker Injuries
0
Num Gp Injuries
0
Injure
1
Ignite Ind
Yes
Ignite Datetime
2021-05-14 16:00:00
How Extinguished
Operator/contractor
Gas Consumed By Fire In Mcf
1464
Explode Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2021-05-14 17:00:00
Communication State Fed Ind
Yes
Party Initiated Communication
Local/state/federal Emergency Responder
Initial Responder Com Datetime
2021-05-14 16:07:00
On Site Datetime
2021-05-14 17:00:00
Federal
No
Location Type
Public Property
Incident Area Type
Underground
Incident Area Subtype
Under Pavement
Depth Of Cover
60.0
Other Underground Facilities
No
Crossing
No
Pipe Facility Type
Privately Owned
System Part Involved
Main
Installation Year
1964.0
Pipe Diameter
2.0
Pipe Specification
Api 5l
Pipe Manufacturer
Unknown
Material Involved
Steel
Steel Seam Type
Longitudinal Erw - Low Frequency
Release Type
Other
Release Type Details
Non-Restricting Coupling Failure
Class Location Type
Class 3 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
20689.0
Est Cost Emergency
0.0
Est Cost Other
0.0
Gas Cost In Mcf
4.45
Est Cost Unintentional Release
6515.0
Est Cost Intentional Release
0.0
Prpty
27204.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
216.0
Num Persons Hosp Not Ovnght
1.0
Num Injured Treated By Emt
2.0
Num Resident Building Affctd
0.0
Num Business Building Affctd
0.0
Accident Psig
90.0
Normal Psig
90.0
Mop Psig
99.0
Mop Cfr Section
192.619(A)(2)
Maop Established Date
1964-01-01 00:00:00
Accident Pressure
Pressure Did Not Exceed Maop
Gas Odorized System Type
Injection Pump
Gas Odorized Lvl Not Msrd Ind
Yes
Scada In Place Ind
No
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Other Incorrect Operation
Operation Type
Other Incorrect Operation
Operation Details
It Appears That The Dead-End Bypass Section Of The Steel Gas Main Was Not Blocked/braced Prior To Cutting The Restraining Straps To Perform The Weld-Over Sleeve Weld Operation. The Gas Pressure Force Caused The Non-Restraining Coupling To Give Way, Which Resulted In An Uncontrolled Release Of Gas With Subsequent Ignition From The Welding Equipment.
Related Failure Follow Ind
Yes
Category Type
Normal Operating Conditions
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Eqf Non Threaded Ind
Yes
Preparer Name
R***** R**
Preparer Title
Manager -Gas Engineering And Standards
Preparer Email
R*********@b**.com
Preparer Telephone
410-470-6933
Preparer Fax
410-470-9549
Authorizer Name
D***** A* N*****
Authorizer Title
Manager -Gas Engineering And Program Management
Authorizer Telephone
410-470-4365
Authorizer Email
D**************@b**.com
Narrative
At approximately 4 p.M. On may 14, 2021, a bge crew member received significant burns from a fire while installing a weld-over sleeve over a gas main coupling on a dead-end bypass. The steel gas main bypass was located at 8407 stevenson road, pikesville, maryland. Gas and electric crews immediately responded to the scene to isolate the trouble, mitigate risks, make repairs and restore service to 216 gas customers and area electric customers. The gas main was isolated by closing an upstream valve. The main was quickly repaired by cutting out this section of pipe and replacing with new steel piping. After an internal investigation by the company, it appears that the dead-end bypass section was not blocked/braced prior to cutting the restraining straps to perform the weld-over sleeve weld operation. The gas pressure force caused the non-restraining coupling to give way, which resulted in an uncontrolled release of gas with subsequent ignition from the welding equipment. Mitigating actions to prevent future recurrence include enhanced training pertaining to proper blocking and bracing, as well as modifications to further clarify gas construction standards.
Occurred At 2021-05-14 17:00:00
Year 2021
Report Received Date 2021-06-18 00:00:00
Iyear 2021.0
Report Number 20210054.0
Supplemental Number 36370.0
Report Type Supplemental Final
Operator Id 1088 PHMSA Enforcement
Name Baltimore Gas And Electric Company
Operator Street Address 110 W Fayette St
Operator City Name Baltimore
Operator State Abbreviation MD
Operator Postal Code 21201
Local Datetime 2021-05-14 16:07:00
Time Zone Eastern
Daylight Savings Ind Yes
Location Street Address 8407 Stevenson Rd
Location City Name Pikesville
Location County Name Baltimore County
Location State Abbreviation MD
Location Postal Code 21208
Location Latitude 39.4005646 Google Maps OpenStreetMap
Location Longitude -76.7124795 Google Maps OpenStreetMap
Flow Cont Main Valve Ind Yes
Nrc Rpt Datetime 2021-06-14 18:18:00
Nrc Rpt Num 1305085 NRC Report How to search
Additional Nrc Report Numbers 1305192
Commodity Released Type Natural Gas
Unintentional Release 1464.0
Intentional Release 0.0
Fatality Ind Yes
Num Emp Fatalities 1
Num Contr Fatalities 0
Num Er Fatalities 0
Num Worker Fatalities 0
Num Gp Fatalities 0
Fatal 1
Injury Ind Yes
Num Emp Injuries 1
Num Contr Injuries 0
Num Er Injuries 0
Num Worker Injuries 0
Num Gp Injuries 0
Injure 1
Ignite Ind Yes
Ignite Datetime 2021-05-14 16:00:00
How Extinguished Operator/contractor
Gas Consumed By Fire In Mcf 1464
Explode Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2021-05-14 17:00:00
Communication State Fed Ind Yes
Party Initiated Communication Local/state/federal Emergency Responder
Initial Responder Com Datetime 2021-05-14 16:07:00
On Site Datetime 2021-05-14 17:00:00
Federal No
Location Type Public Property
Incident Area Type Underground
Incident Area Subtype Under Pavement
Depth Of Cover 60.0
Other Underground Facilities No
Crossing No
Pipe Facility Type Privately Owned
System Part Involved Main
Installation Year 1964.0
Pipe Diameter 2.0
Pipe Specification Api 5l
Pipe Manufacturer Unknown
Material Involved Steel
Steel Seam Type Longitudinal Erw - Low Frequency
Release Type Other
Release Type Details Non-Restricting Coupling Failure
Class Location Type Class 3 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 20689.0
Est Cost Emergency 0.0
Est Cost Other 0.0
Gas Cost In Mcf 4.45
Est Cost Unintentional Release 6515.0
Est Cost Intentional Release 0.0
Prpty 27204.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 216.0
Num Persons Hosp Not Ovnght 1.0
Num Injured Treated By Emt 2.0
Num Resident Building Affctd 0.0
Num Business Building Affctd 0.0
Accident Psig 90.0
Normal Psig 90.0
Mop Psig 99.0
Mop Cfr Section 192.619(A)(2) View CFR 49 §192
Maop Established Date 1964-01-01 00:00:00
Accident Pressure Pressure Did Not Exceed Maop
Gas Odorized System Type Injection Pump
Gas Odorized Lvl Not Msrd Ind Yes
Scada In Place Ind No
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Other Incorrect Operation
Operation Type Other Incorrect Operation
Operation Details It Appears That The Dead-End Bypass Section Of The Steel Gas Main Was Not Blocked/braced Prior To Cutting The Restraining Straps To Perform The Weld-Over Sleeve Weld Operation. The Gas Pressure Force Caused The Non-Restraining Coupling To Give Way, Which Resulted In An Uncontrolled Release Of Gas With Subsequent Ignition From The Welding Equipment.
Related Failure Follow Ind Yes
Category Type Normal Operating Conditions
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Eqf Non Threaded Ind Yes
Preparer Name R***** R**
Preparer Title Manager -Gas Engineering And Standards
Preparer Email R*********@b**.com
Preparer Telephone 410-470-6933
Preparer Fax 410-470-9549
Authorizer Name D***** A* N*****
Authorizer Title Manager -Gas Engineering And Program Management
Authorizer Telephone 410-470-4365
Authorizer Email D**************@b**.com
Narrative At approximately 4 p.M. On may 14, 2021, a bge crew member received significant burns from a fire while installing a weld-over sleeve over a gas main coupling on a dead-end bypass. The steel gas main bypass was located at 8407 stevenson road, pikesville, maryland. Gas and electric crews immediately responded to the scene to isolate the trouble, mitigate risks, make repairs and restore service to 216 gas customers and area electric customers. The gas main was isolated by closing an upstream valve. The main was quickly repaired by cutting out this section of pipe and replacing with new steel piping. After an internal investigation by the company, it appears that the dead-end bypass section was not blocked/braced prior to cutting the restraining straps to perform the weld-over sleeve weld operation. The gas pressure force caused the non-restraining coupling to give way, which resulted in an uncontrolled release of gas with subsequent ignition from the welding equipment. Mitigating actions to prevent future recurrence include enhanced training pertaining to proper blocking and bracing, as well as modifications to further clarify gas construction standards.

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