GTG incident on 2021-02-26 — KY

Operator
Southern Star Central Gas Pipeline, Inc
Cause
Incorrect Operation
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 1 injury
Property damage (nominal)
$500,000
Incident datetime
2021-02-26 10:04
Report number
Location
KY
Narrative
On 2/26/2021 southern star center gas pipeline (sscgp) and a contractor were performing an inline inspection on line fm in jasper county, missouri. After the inline inspection tool (pig) was launched, it became lodged in the line. At 10:04 am, the pig dislodged and a pipeline rupture occurred. The mainline valves on line fm were already closed due to the inline inspection. The kicker valve at the pig launcher was being manned at the time and was immediately closed to stop gas flow. Line fm was completely blown down by 10:07 am. Two sscgp employees were present at the rupture location when the rupture occurred and one employee was injured. Other sscgp and contractor employees assisted and local emergency responders were notified at 10:05 am and were on site within 10 minutes. One sscgp employee was transported to the local hospital by ambulance and was admitted to the hospital for his injuries. Another sccgp employee was taken to the hospital by car as a precaution and was examined and released with no observed injuries. The employee that was admitted was released from the hospital on 2/28/2021. Repairs on line fm were completed and the line was returned to service on 3/1/2021 at 7:30 am. Note: edits contained in the final supplement incident report are in: part c, 3b, 3e, 3g, 3h, c6 part d, 7d, 7e, 13a part g7- incorrect operation please refer to the contributing factors, causal factors, and root causes contained in the kiefner report dated september 17, 2021.
Detailed record list
Report Received Date
2021-03-24 00:00:00
Iyear
2021
Report Number
20210030
Supplemental Number
36184
Report Type
Supplemental Final
Operator Id
Name
Southern Star Central Gas Pipeline, Inc
Operator Street Address
4700 State Route 56; Box 20010
Operator City Name
Owensboro
Operator State Abbreviation
KY
Operator Postal Code
42301
Local Datetime
2021-02-26 10:04:00
Time Zone
Central
Daylight Savings Ind
No
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2021-02-26 10:32:00
Additional Nrc Report Numbers
1299193
Commodity Released Type
Natural Gas
Unintentional Release
76
Intentional Release
0
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
Yes
Num Emp Injuries
1
Num Contr Injuries
0
Num Er Injuries
0
Num Worker Injuries
0
Num Gp Injuries
0
Injure
1
Status When Identified
Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2021-02-26 10:04:00
Restart Datetime
2021-03-01 07:30:00
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Initial Responder Com Datetime
2021-02-26 10:05:00
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Close Datetime
2021-02-26 10:04:00
Downstream Action Taken
Valve Closure
Downstream Vlv Close Datetime
2021-02-26 10:04:00
Num Pub Evacuated
0
Incident Identified Datetime
2021-02-26 10:04:00
On Site Datetime
2021-02-26 10:04:00
On Off Shore
Onshore
Onshore State Abbreviation
Mo
Onshore Postal Code
64834
Onshore City Name
Carl Junction
Onshore County Name
Jasper
Designated Location
Survey Station No.
Designated Name
110/484
Pipe Fac Name
Joplin-Lone Elm 10"
Segment Name
Line Fm
Federal
No
Location Type
Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
72
Other Underground Facilities
No
Crossing
No
Pipe Facility Type
Interstate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
10
Puddle Weld Ind
No
Pipe Wall Thickness
0.365
Pipe Smys
42000
Pipe Specification
Api 5l
Pipe Seam Type
Seamless
Pipe Manufacturer
Unknown
Pipe Coating Type
Cold Applied Tape
Coating Applied Ind
Yes
Installation Year
1991
Manufactured Year
1990
Material Involved
Carbon Steel
Release Type
Rupture
Rupture Orient
Other
Rupture Details
Outside Radius Of The Elbows Due To Ili Tool Impact.
Rupture Length
10
Rupture Width
10
Class Location Type
Class 3 Location
Could Be Hca
No
Pir Radius
138
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Did Occur In Mca Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
192
Est Cost Intentional Release
0
Est Cost Prop Damage
500000
Est Cost Emergency
3000
Est Cost Other
288619
Est Cost Other Details
Root Cause Failure Analysis, Shipping Of Pipe Samples, Ground Penetrating Radar
Gas Cost In Mcf
2.52
Prpty
791811
Num Persons Hosp Not Ovnght
1
Num Injured Treated By Emt
0
Num Resident Building Affctd
1145
Num Business Building Affctd
0
Wildlife Impact Ind
No
Accident Psig
350
Gas Flow In Pipe In Mcf
0
Mop Psig
400
Mop Cfr Section
192.619(A)(2)
Maop Established Date
1991-02-20 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Gas Required Odorized Ind
Yes
Gas Odorized Ind
Yes
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
11000
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
Yes
Num Employees Tested
11
Num Employees Failed
0
Num Contractors Tested
2
Num Contractors Failed
0
Cause
Incorrect Operation
Cause Details
Other Incorrect Operation
Operation Type
Other Incorrect Operation
Operation Details
Please Reference The Contributing Factors, Causal Factors And Root Causes Contained In The Kiefner Report Dated September 17,2021.
Related Inadequate Proc Ind
Yes
Category Type
Routine Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
E*** G****
Preparer Title
Pipeline Compliance Engineer
Preparer Email
E*********@s***********.com
Preparer Telephone
12702310561
Preparer Fax
2708525016
Local Contact Name
C**** T*****
Local Contact Email
C***********@s***********.com
Local Contact Telephone
2703138424
Authorizer Name
S**** P********
Authorizer Title
Vp Chief Operations Officer
Authorizer Telephone
12708524670
Authorizer Email
S**************@s***********.com
Narrative
On 2/26/2021 southern star center gas pipeline (sscgp) and a contractor were performing an inline inspection on line fm in jasper county, missouri. After the inline inspection tool (pig) was launched, it became lodged in the line. At 10:04 am, the pig dislodged and a pipeline rupture occurred. The mainline valves on line fm were already closed due to the inline inspection. The kicker valve at the pig launcher was being manned at the time and was immediately closed to stop gas flow. Line fm was completely blown down by 10:07 am. Two sscgp employees were present at the rupture location when the rupture occurred and one employee was injured. Other sscgp and contractor employees assisted and local emergency responders were notified at 10:05 am and were on site within 10 minutes. One sscgp employee was transported to the local hospital by ambulance and was admitted to the hospital for his injuries. Another sccgp employee was taken to the hospital by car as a precaution and was examined and released with no observed injuries. The employee that was admitted was released from the hospital on 2/28/2021. Repairs on line fm were completed and the line was returned to service on 3/1/2021 at 7:30 am. Note: edits contained in the final supplement incident report are in: part c, 3b, 3e, 3g, 3h, c6 part d, 7d, 7e, 13a part g7- incorrect operation please refer to the contributing factors, causal factors, and root causes contained in the kiefner report dated september 17, 2021.
Report Received Date 2021-03-24 00:00:00
Iyear 2021
Report Number 20210030
Supplemental Number 36184
Report Type Supplemental Final
Operator Id 31711 PHMSA Enforcement
Name Southern Star Central Gas Pipeline, Inc
Operator Street Address 4700 State Route 56; Box 20010
Operator City Name Owensboro
Operator State Abbreviation KY
Operator Postal Code 42301
Local Datetime 2021-02-26 10:04:00
Time Zone Central
Daylight Savings Ind No
Location Latitude 37.14227 Google Maps OpenStreetMap
Location Longitude -94.529067 Google Maps OpenStreetMap
Nrc Rpt Num 1299051 NRC Report How to search
Nrc Rpt Datetime 2021-02-26 10:32:00
Additional Nrc Report Numbers 1299193
Commodity Released Type Natural Gas
Unintentional Release 76
Intentional Release 0
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind Yes
Num Emp Injuries 1
Num Contr Injuries 0
Num Er Injuries 0
Num Worker Injuries 0
Num Gp Injuries 0
Injure 1
Status When Identified Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind Yes
Shutdown Datetime 2021-02-26 10:04:00
Restart Datetime 2021-03-01 07:30:00
Communication State Fed Ind Yes
Party Initiated Communication Operator
Initial Responder Com Datetime 2021-02-26 10:05:00
Ignite Ind No
Upstream Action Taken Valve Closure
Upstream Valve Close Datetime 2021-02-26 10:04:00
Downstream Action Taken Valve Closure
Downstream Vlv Close Datetime 2021-02-26 10:04:00
Num Pub Evacuated 0
Incident Identified Datetime 2021-02-26 10:04:00
On Site Datetime 2021-02-26 10:04:00
On Off Shore Onshore
Onshore State Abbreviation Mo
Onshore Postal Code 64834
Onshore City Name Carl Junction
Onshore County Name Jasper
Designated Location Survey Station No.
Designated Name 110/484
Pipe Fac Name Joplin-Lone Elm 10"
Segment Name Line Fm
Federal No
Location Type Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 72
Other Underground Facilities No
Crossing No
Pipe Facility Type Interstate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 10
Puddle Weld Ind No
Pipe Wall Thickness 0.365
Pipe Smys 42000
Pipe Specification Api 5l
Pipe Seam Type Seamless
Pipe Manufacturer Unknown
Pipe Coating Type Cold Applied Tape
Coating Applied Ind Yes
Installation Year 1991
Manufactured Year 1990
Material Involved Carbon Steel
Release Type Rupture
Rupture Orient Other
Rupture Details Outside Radius Of The Elbows Due To Ili Tool Impact.
Rupture Length 10
Rupture Width 10
Class Location Type Class 3 Location
Could Be Hca No
Pir Radius 138
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Did Occur In Mca Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 192
Est Cost Intentional Release 0
Est Cost Prop Damage 500000
Est Cost Emergency 3000
Est Cost Other 288619
Est Cost Other Details Root Cause Failure Analysis, Shipping Of Pipe Samples, Ground Penetrating Radar
Gas Cost In Mcf 2.52
Prpty 791811
Num Persons Hosp Not Ovnght 1
Num Injured Treated By Emt 0
Num Resident Building Affctd 1145
Num Business Building Affctd 0
Wildlife Impact Ind No
Accident Psig 350
Gas Flow In Pipe In Mcf 0
Mop Psig 400
Mop Cfr Section 192.619(A)(2) View CFR 49 §192
Maop Established Date 1991-02-20 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Gas Required Odorized Ind Yes
Gas Odorized Ind Yes
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Length Segment Isolated 11000
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind Yes
Contractor Drug Test Ind Yes
Num Employees Tested 11
Num Employees Failed 0
Num Contractors Tested 2
Num Contractors Failed 0
Cause Incorrect Operation
Cause Details Other Incorrect Operation
Operation Type Other Incorrect Operation
Operation Details Please Reference The Contributing Factors, Causal Factors And Root Causes Contained In The Kiefner Report Dated September 17,2021.
Related Inadequate Proc Ind Yes
Category Type Routine Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name E*** G****
Preparer Title Pipeline Compliance Engineer
Preparer Email E*********@s***********.com
Preparer Telephone 12702310561
Preparer Fax 2708525016
Local Contact Name C**** T*****
Local Contact Email C***********@s***********.com
Local Contact Telephone 2703138424
Authorizer Name S**** P********
Authorizer Title Vp Chief Operations Officer
Authorizer Telephone 12708524670
Authorizer Email S**************@s***********.com
Narrative On 2/26/2021 southern star center gas pipeline (sscgp) and a contractor were performing an inline inspection on line fm in jasper county, missouri. After the inline inspection tool (pig) was launched, it became lodged in the line. At 10:04 am, the pig dislodged and a pipeline rupture occurred. The mainline valves on line fm were already closed due to the inline inspection. The kicker valve at the pig launcher was being manned at the time and was immediately closed to stop gas flow. Line fm was completely blown down by 10:07 am. Two sscgp employees were present at the rupture location when the rupture occurred and one employee was injured. Other sscgp and contractor employees assisted and local emergency responders were notified at 10:05 am and were on site within 10 minutes. One sscgp employee was transported to the local hospital by ambulance and was admitted to the hospital for his injuries. Another sccgp employee was taken to the hospital by car as a precaution and was examined and released with no observed injuries. The employee that was admitted was released from the hospital on 2/28/2021. Repairs on line fm were completed and the line was returned to service on 3/1/2021 at 7:30 am. Note: edits contained in the final supplement incident report are in: part c, 3b, 3e, 3g, 3h, c6 part d, 7d, 7e, 13a part g7- incorrect operation please refer to the contributing factors, causal factors, and root causes contained in the kiefner report dated september 17, 2021.

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