GD incident on 2021-01-14 — OH

Operator
Columbia Gas Of Ohio Inc
Cause
Excavation Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$35,987
Incident datetime
2021-01-14 09:30
Report number
Location
OH, LUCAS
Narrative
On january 13, 2021 a third party excavator operating a bull dozer damaged a properly located and marked 16" steel main line. Columbia gas of ohio inc. (columbia) took immediate action to repair the leak and set up a perimeter and began monitoring the leak. Columbia monitored the leak as it remained non-hazardous and welded a 16inch stopple fitting on the main line and utilized another two critical valves to shut the line down for permanent repairs. The permanent repairs were made and the line was placed back in service on january 16, 2021 at 10:30 am. Please consider this a final report.
Detailed record list
Occurred At
2021-01-14 09:30:00
Year
2021
Report Received Date
2021-02-13 00:00:00
Iyear
2021.0
Report Number
20210018.0
Supplemental Number
34862.0
Report Type
Original Final
Operator Id
Name
Columbia Gas Of Ohio Inc
Operator Street Address
290 W Nationwide Blvd
Operator City Name
Columbus
Operator State Abbreviation
OH
Operator Postal Code
43215
Local Datetime
2021-01-14 09:30:00
Time Zone
Eastern
Daylight Savings Ind
Yes
Location Street Address
820 S 15th St
Location City Name
Toledo
Location County Name
Lucas
Location State Abbreviation
OH
Location Postal Code
43604
Location Latitude
Location Longitude
Flow Cont Key Crit Ind
Yes
Flow Cont Stopple Fitng Ind
Yes
Nrc Rpt Datetime
2021-01-14 09:56:00
Nrc Rpt Num
Additional Nrc Report Numbers
1296109
Commodity Released Type
Natural Gas
Unintentional Release
40395.7
Intentional Release
101.7
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2021-01-14 09:30:00
On Site Datetime
2021-01-13 21:45:00
Federal
No
Location Type
Utility Right-Of-Way / Easement
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Depth Of Cover
1.0
Other Underground Facilities
No
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
1965.0
Pipe Diameter
16.0
Pipe Specification
Unknown
Pipe Manufacturer
Unknown
Material Involved
Steel
Steel Seam Type
Other
Steel Seam Type Details
Unknown
Wt Steel
0.241
Release Type
Mechanical Puncture
Puncture Axial
3.0
Puncture Circum
10.0
Class Location Type
Class 4 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
35987.0
Est Cost Emergency
278911.0
Est Cost Other
0.0
Est Cost Other Details
0
Gas Cost In Mcf
2.45
Est Cost Unintentional Release
98969.0
Est Cost Intentional Release
249.0
Prpty
414116.0
Commercial Affected
2.0
Industrial Affected
0.0
Residences Affected
0.0
Num Persons Hosp Not Ovnght
0.0
Num Injured Treated By Emt
0.0
Num Resident Building Affctd
0.0
Num Business Building Affctd
2.0
Accident Psig
48.0
Normal Psig
48.0
Mop Psig
58.0
Mop Cfr Section
192.619(A)(3)
Maop Established Date
1971-04-01 00:00:00
Accident Pressure
Pressure Did Not Exceed Maop
Gas Odorized System Type
Combination Of Odorization Types
Gas Odorized Lvl Not Msrd Ind
Yes
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The release of gas was insufficient to cause a pressure alert for the controller to act on.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
State Law Exempt Ind
No
Notify Cga Dirt
Yes
Public Row Ind
Yes
Public Subtype
State Highway
Unknown Row Ind
Yes
Excavator Type
Contractor
Excavator Equipment
Unknown/other
Work Performed
Road Work
One Call Notified Ind
Yes
One Call Ticket Num
B100400793
One Call Center Name
Ohio Utilities Protection Service
Locator Type
Contract Locator
Visible Marks
Yes
Service Interruption
Yes
Service Interruption Hours
65.0
Root Cause Category
Excavation Issue
Root Cause Type
Excavator Failed To Maintain Clearance After Verifying Marks
Preparer Name
R** S****
Preparer Title
Manager Operations Compliance
Preparer Email
R******@n*******.com
Preparer Telephone
6144605491
Local Contact Name
R** S****
Local Contact Email
R******@n*******.com
Local Contact Telephone
6144605491
Authorizer Name
R** S****
Authorizer Title
Manager Operations Compliance
Authorizer Telephone
6144605491
Authorizer Email
R******@n*******.com
Narrative
On january 13, 2021 a third party excavator operating a bull dozer damaged a properly located and marked 16" steel main line. Columbia gas of ohio inc. (columbia) took immediate action to repair the leak and set up a perimeter and began monitoring the leak. Columbia monitored the leak as it remained non-hazardous and welded a 16inch stopple fitting on the main line and utilized another two critical valves to shut the line down for permanent repairs. The permanent repairs were made and the line was placed back in service on january 16, 2021 at 10:30 am. Please consider this a final report.
Occurred At 2021-01-14 09:30:00
Year 2021
Report Received Date 2021-02-13 00:00:00
Iyear 2021.0
Report Number 20210018.0
Supplemental Number 34862.0
Report Type Original Final
Operator Id 2596 PHMSA Enforcement
Name Columbia Gas Of Ohio Inc
Operator Street Address 290 W Nationwide Blvd
Operator City Name Columbus
Operator State Abbreviation OH
Operator Postal Code 43215
Local Datetime 2021-01-14 09:30:00
Time Zone Eastern
Daylight Savings Ind Yes
Location Street Address 820 S 15th St
Location City Name Toledo
Location County Name Lucas
Location State Abbreviation OH
Location Postal Code 43604
Location Latitude 41.651319 Google Maps OpenStreetMap
Location Longitude -83.548099 Google Maps OpenStreetMap
Flow Cont Key Crit Ind Yes
Flow Cont Stopple Fitng Ind Yes
Nrc Rpt Datetime 2021-01-14 09:56:00
Nrc Rpt Num 1296041 NRC Report How to search
Additional Nrc Report Numbers 1296109
Commodity Released Type Natural Gas
Unintentional Release 40395.7
Intentional Release 101.7
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2021-01-14 09:30:00
On Site Datetime 2021-01-13 21:45:00
Federal No
Location Type Utility Right-Of-Way / Easement
Incident Area Type Underground
Incident Area Subtype Exposed Due To Excavation
Depth Of Cover 1.0
Other Underground Facilities No
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Main
Installation Year 1965.0
Pipe Diameter 16.0
Pipe Specification Unknown
Pipe Manufacturer Unknown
Material Involved Steel
Steel Seam Type Other
Steel Seam Type Details Unknown
Wt Steel 0.241
Release Type Mechanical Puncture
Puncture Axial 3.0
Puncture Circum 10.0
Class Location Type Class 4 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 35987.0
Est Cost Emergency 278911.0
Est Cost Other 0.0
Est Cost Other Details 0
Gas Cost In Mcf 2.45
Est Cost Unintentional Release 98969.0
Est Cost Intentional Release 249.0
Prpty 414116.0
Commercial Affected 2.0
Industrial Affected 0.0
Residences Affected 0.0
Num Persons Hosp Not Ovnght 0.0
Num Injured Treated By Emt 0.0
Num Resident Building Affctd 0.0
Num Business Building Affctd 2.0
Accident Psig 48.0
Normal Psig 48.0
Mop Psig 58.0
Mop Cfr Section 192.619(A)(3) View CFR 49 §192
Maop Established Date 1971-04-01 00:00:00
Accident Pressure Pressure Did Not Exceed Maop
Gas Odorized System Type Combination Of Odorization Types
Gas Odorized Lvl Not Msrd Ind Yes
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Notification From Emergency Responder
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The release of gas was insufficient to cause a pressure alert for the controller to act on.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind Yes
One Call System Ind Yes
State Law Exempt Ind No
Notify Cga Dirt Yes
Public Row Ind Yes
Public Subtype State Highway
Unknown Row Ind Yes
Excavator Type Contractor
Excavator Equipment Unknown/other
Work Performed Road Work
One Call Notified Ind Yes
One Call Ticket Num B100400793
One Call Center Name Ohio Utilities Protection Service
Locator Type Contract Locator
Visible Marks Yes
Service Interruption Yes
Service Interruption Hours 65.0
Root Cause Category Excavation Issue
Root Cause Type Excavator Failed To Maintain Clearance After Verifying Marks
Preparer Name R** S****
Preparer Title Manager Operations Compliance
Preparer Email R******@n*******.com
Preparer Telephone 6144605491
Local Contact Name R** S****
Local Contact Email R******@n*******.com
Local Contact Telephone 6144605491
Authorizer Name R** S****
Authorizer Title Manager Operations Compliance
Authorizer Telephone 6144605491
Authorizer Email R******@n*******.com
Narrative On january 13, 2021 a third party excavator operating a bull dozer damaged a properly located and marked 16" steel main line. Columbia gas of ohio inc. (columbia) took immediate action to repair the leak and set up a perimeter and began monitoring the leak. Columbia monitored the leak as it remained non-hazardous and welded a 16inch stopple fitting on the main line and utilized another two critical valves to shut the line down for permanent repairs. The permanent repairs were made and the line was placed back in service on january 16, 2021 at 10:30 am. Please consider this a final report.

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