GTG incident on 2021-01-19 — TX

Operator
Atmos Pipeline - Texas
Cause
Locating Issue
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$161,563
Incident datetime
2021-01-19 10:03
Report number
Location
TX
Narrative
On january 19, 2021, a farmer struck a farm tap off of line kc 17 with a plow near hawley, texas. Atmos energy was notified of the incident at 10:03 am, at which point work began to determine how to make repairs. The decision was made to squeeze off the 1.25" steel riser and after the squeeze off occurred at approximately 1 pm, it was discovered that a threaded connection was leaking under the squeezed off section of the riser. Work then began on a bypass on kc17 to ensure continued service on the line. At the point it was determined a bypass would be needed to make the necessary repairs, it was anticipated that the cost associated with repairing the damage would exceed $50,000. A call was made to the national response center at 16:17 ct on 1/19/2021. Stopples were welded on for the bypass, which was completed on january 20, 2021. On january 21, 2021, 5 feet of 12" pipe was replaced and line kc17 was then returned to normal operation.
Detailed record list
Report Received Date
2021-02-18 00:00:00
Iyear
2021
Report Number
20210014
Supplemental Number
34873
Report Type
Original Final
Operator Id
Name
Atmos Pipeline - Texas
Operator Street Address
5420 Lbj Freeway, Suite 1500
Operator City Name
Dallas
Operator State Abbreviation
TX
Operator Postal Code
75240
Local Datetime
2021-01-19 15:20:00
Time Zone
Central
Daylight Savings Ind
No
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2021-01-19 16:17:00
Additional Nrc Report Numbers
1296448
Commodity Released Type
Natural Gas
Unintentional Release
1667.5
Intentional Release
0.89
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Status When Identified
Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind
No
Shutdown Explain
Installed Two 12 Inch Stopple Fittings And Built A By-Pass Between Them
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Initial Responder Com Datetime
2021-01-19 11:00:00
Ignite Ind
No
Upstream Action Taken
Operational Control
Upstream Oprtnl Cntrl Detail
No Action Required. Upstream Pipeline Pressure And Flow Were Adequate
Downstream Action Taken
Operational Control
Downstream Oprtnl Cntrl Detail
Used Steel Squeezers On 1 Inch Tap To Squeeze Off Leak
Num Pub Evacuated
0
Incident Identified Datetime
2021-01-19 10:03:00
On Site Datetime
2021-01-19 10:17:00
On Off Shore
Onshore
Onshore State Abbreviation
Tx
Onshore Postal Code
79525
Onshore City Name
Hawley
Onshore County Name
Jones
Designated Location
Survey Station No.
Designated Name
936+67
Pipe Fac Name
Kc 17 1" Farm Tap
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Transition Area
Incident Area Subtype
Soil/air Interface
Crossing
No
Pipe Facility Type
Intrastate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
1.25
Puddle Weld Ind
No
Pipe Wall Thickness
0.126
Pipe Smys
24000
Pipe Specification
Unknown
Pipe Seam Type
Other
Pipe Seam Details
Unknown
Pipe Manufacturer
Unknown
Pipe Coating Type
Coal Tar
Coating Applied Ind
Yes
Installation Year
1953
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Valve Knocked Off Of 1.25" Riser
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
24
Heat Damage Ind
No
Non Heat Damage Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
9785
Est Cost Intentional Release
5
Est Cost Prop Damage
161563
Est Cost Emergency
0
Est Cost Other
0
Gas Cost In Mcf
5.868
Prpty
171353
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Wildlife Impact Ind
No
Accident Psig
650
Gas Flow In Pipe In Mcf
0
Mop Psig
800
Mop Cfr Section
192.619(A)(1)
Maop Established Date
1953-12-14 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Gas Required Odorized Ind
Yes
Gas Odorized Ind
Yes
Length Segment Isolated
37561
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Notification From Third Party That Caused The Incident
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Leak was too small to be picked up by controllers
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
No
State Law Exempt Ind
Yes
State Law Exempt Type
Activity Is Exempt And Did Not Exceed The Limits Of The Exemption
State Law Exempt Authority
Railroad Commission Of Texas
State Law Exempt Criteria
Farmer Was Tilling At A Depth Of Less Than 16 Inches
Notify Cga Dirt
No
Pipeline Easement Row Ind
Yes
Excavator Type
Farmer
Excavator Equipment
Farm Equipment
Work Performed
Agriculture
One Call Notified Ind
No
Service Interruption
No
Root Cause Category
Locating Issue
Root Cause Type
Facility Not Marked Due To Abandoned Facility
Preparer Name
R***** O*****
Preparer Title
Operations Supervisor
Preparer Email
R***********@a**********.com
Preparer Telephone
325-280-1778
Authorizer Name
M**** S*****
Authorizer Title
Vice President - Technical Services
Authorizer Telephone
214-206-2033
Authorizer Email
M***********@a**********.com
Narrative
On january 19, 2021, a farmer struck a farm tap off of line kc 17 with a plow near hawley, texas. Atmos energy was notified of the incident at 10:03 am, at which point work began to determine how to make repairs. The decision was made to squeeze off the 1.25" steel riser and after the squeeze off occurred at approximately 1 pm, it was discovered that a threaded connection was leaking under the squeezed off section of the riser. Work then began on a bypass on kc17 to ensure continued service on the line. At the point it was determined a bypass would be needed to make the necessary repairs, it was anticipated that the cost associated with repairing the damage would exceed $50,000. A call was made to the national response center at 16:17 ct on 1/19/2021. Stopples were welded on for the bypass, which was completed on january 20, 2021. On january 21, 2021, 5 feet of 12" pipe was replaced and line kc17 was then returned to normal operation.
Report Received Date 2021-02-18 00:00:00
Iyear 2021
Report Number 20210014
Supplemental Number 34873
Report Type Original Final
Operator Id 31978 PHMSA Enforcement
Name Atmos Pipeline - Texas
Operator Street Address 5420 Lbj Freeway, Suite 1500
Operator City Name Dallas
Operator State Abbreviation TX
Operator Postal Code 75240
Local Datetime 2021-01-19 15:20:00
Time Zone Central
Daylight Savings Ind No
Location Latitude 32.68141 Google Maps OpenStreetMap
Location Longitude -99.80307 Google Maps OpenStreetMap
Nrc Rpt Num 1296316 NRC Report How to search
Nrc Rpt Datetime 2021-01-19 16:17:00
Additional Nrc Report Numbers 1296448
Commodity Released Type Natural Gas
Unintentional Release 1667.5
Intentional Release 0.89
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Status When Identified Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind No
Shutdown Explain Installed Two 12 Inch Stopple Fittings And Built A By-Pass Between Them
Communication State Fed Ind Yes
Party Initiated Communication Operator
Initial Responder Com Datetime 2021-01-19 11:00:00
Ignite Ind No
Upstream Action Taken Operational Control
Upstream Oprtnl Cntrl Detail No Action Required. Upstream Pipeline Pressure And Flow Were Adequate
Downstream Action Taken Operational Control
Downstream Oprtnl Cntrl Detail Used Steel Squeezers On 1 Inch Tap To Squeeze Off Leak
Num Pub Evacuated 0
Incident Identified Datetime 2021-01-19 10:03:00
On Site Datetime 2021-01-19 10:17:00
On Off Shore Onshore
Onshore State Abbreviation Tx
Onshore Postal Code 79525
Onshore City Name Hawley
Onshore County Name Jones
Designated Location Survey Station No.
Designated Name 936+67
Pipe Fac Name Kc 17 1" Farm Tap
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Transition Area
Incident Area Subtype Soil/air Interface
Crossing No
Pipe Facility Type Intrastate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 1.25
Puddle Weld Ind No
Pipe Wall Thickness 0.126
Pipe Smys 24000
Pipe Specification Unknown
Pipe Seam Type Other
Pipe Seam Details Unknown
Pipe Manufacturer Unknown
Pipe Coating Type Coal Tar
Coating Applied Ind Yes
Installation Year 1953
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Other
Release Type Details Valve Knocked Off Of 1.25" Riser
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 24
Heat Damage Ind No
Non Heat Damage Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 9785
Est Cost Intentional Release 5
Est Cost Prop Damage 161563
Est Cost Emergency 0
Est Cost Other 0
Gas Cost In Mcf 5.868
Prpty 171353
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Wildlife Impact Ind No
Accident Psig 650
Gas Flow In Pipe In Mcf 0
Mop Psig 800
Mop Cfr Section 192.619(A)(1) View CFR 49 §192
Maop Established Date 1953-12-14 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Gas Required Odorized Ind Yes
Gas Odorized Ind Yes
Length Segment Isolated 37561
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Notification From Third Party That Caused The Incident
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Leak was too small to be picked up by controllers
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind No
State Law Exempt Ind Yes
State Law Exempt Type Activity Is Exempt And Did Not Exceed The Limits Of The Exemption
State Law Exempt Authority Railroad Commission Of Texas
State Law Exempt Criteria Farmer Was Tilling At A Depth Of Less Than 16 Inches
Notify Cga Dirt No
Pipeline Easement Row Ind Yes
Excavator Type Farmer
Excavator Equipment Farm Equipment
Work Performed Agriculture
One Call Notified Ind No
Service Interruption No
Root Cause Category Locating Issue
Root Cause Type Facility Not Marked Due To Abandoned Facility
Preparer Name R***** O*****
Preparer Title Operations Supervisor
Preparer Email R***********@a**********.com
Preparer Telephone 325-280-1778
Authorizer Name M**** S*****
Authorizer Title Vice President - Technical Services
Authorizer Telephone 214-206-2033
Authorizer Email M***********@a**********.com
Narrative On january 19, 2021, a farmer struck a farm tap off of line kc 17 with a plow near hawley, texas. Atmos energy was notified of the incident at 10:03 am, at which point work began to determine how to make repairs. The decision was made to squeeze off the 1.25" steel riser and after the squeeze off occurred at approximately 1 pm, it was discovered that a threaded connection was leaking under the squeezed off section of the riser. Work then began on a bypass on kc17 to ensure continued service on the line. At the point it was determined a bypass would be needed to make the necessary repairs, it was anticipated that the cost associated with repairing the damage would exceed $50,000. A call was made to the national response center at 16:17 ct on 1/19/2021. Stopples were welded on for the bypass, which was completed on january 20, 2021. On january 21, 2021, 5 feet of 12" pipe was replaced and line kc17 was then returned to normal operation.

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