GD incident on 2020-12-25 — PA

Operator
Ugi Utilities, Inc
Cause
Pipe, Weld, Or Joint Failure
Commodity
Natural Gas
Program
GD
Damage and Injuries
1 fatality 2 injuries
Property damage (nominal)
$39,310
Incident datetime
2020-12-25 01:44
Report number
Location
PA, MONROE
Narrative
At approximately 1:44 am december 25, 2020, ugi employees responded to a call from monroe county 911 reporting an incident involving the release of natural gas. It was discovered that the 12-inch hdpe, 100 psig maop distribution pipeline had separated at the butt fusion interface from an unknown cause. There was one confirmed fatality and two injuries requiring hospitalization from an overturned vehicle. In response to the incident, the pipeline was repaired and placed back in operation. The pipeline operating pressure has been lowered from 94 psig to 60 psig as a precautionary measure. Ugi is filing this supplemental and final report after a third-party lab completed testing on the failed butt fusion joint and a root cause analysis. The root cause was determined to be a combination of the following factors: 1) inadequate interfacial pressure applied during the joining phase of the fusion process and/or excessive dwell time between heat soak and joining phases; and 2) the failure to follow appropriate installation and inspection procedures.
Detailed record list
Occurred At
2020-12-25 01:44:00
Year
2020
Report Received Date
2021-01-24 00:00:00
Iyear
2020.0
Report Number
20210013.0
Supplemental Number
36706.0
Report Type
Supplemental Final
Operator Id
Name
Ugi Utilities, Inc
Operator Street Address
1 Ugi Drive
Operator City Name
Denver
Operator State Abbreviation
PA
Operator Postal Code
17517
Local Datetime
2020-12-25 01:30:00
Time Zone
Eastern
Daylight Savings Ind
No
Location Street Address
117 Lower Swiftwater Road
Location City Name
Swiftwater
Location County Name
Monroe
Location State Abbreviation
PA
Location Postal Code
18370
Location Latitude
Location Longitude
Flow Cont Key Crit Ind
Yes
Nrc Rpt Datetime
2020-12-25 04:58:00
Nrc Rpt Num
Additional Nrc Report Numbers
1295037
Commodity Released Type
Natural Gas
Unintentional Release
975.0
Intentional Release
0.0
Fatality Ind
Yes
Num Emp Fatalities
0
Num Contr Fatalities
0
Num Er Fatalities
0
Num Worker Fatalities
0
Num Gp Fatalities
1
Fatal
1
Injury Ind
Yes
Num Emp Injuries
0
Num Contr Injuries
0
Num Er Injuries
0
Num Worker Injuries
0
Num Gp Injuries
2
Injure
2
Ignite Ind
No
Num Pub Evacuated
2.0
Incident Identified Datetime
2020-12-25 01:44:00
On Site Datetime
2020-12-25 02:07:00
Federal
No
Location Type
Public Property
Incident Area Type
Underground
Incident Area Subtype
Under Pavement
Depth Of Cover
36.0
Other Underground Facilities
No
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
2019.0
Manufactured Year
2017.0
Pipe Diameter
12.0
Pipe Specification
Astm D2513
Pipe Manufacturer
Charter Plastics, Inc.
Material Involved
Plastic
Plastic Type
Polyethylene (Pe)
Plastic Sdr
11
Material Pe Pipe Code
4710
Release Type
Rupture
Rupture Orient
Circumferential
Rupture Length
12
Rupture Width
1.5
Class Location Type
Class 3 Location
Est Cost Oper Paid
40000.0
Est Cost Prop Damage
39310.0
Est Cost Emergency
4615.0
Est Cost Other
0.0
Gas Cost In Mcf
2.2207
Est Cost Unintentional Release
2165.0
Est Cost Intentional Release
0.0
Prpty
86090.0
Commercial Affected
5.0
Industrial Affected
0.0
Residences Affected
0.0
Num Persons Hosp Not Ovnght
0.0
Num Injured Treated By Emt
0.0
Num Resident Building Affctd
0.0
Num Business Building Affctd
5.0
Accident Psig
95.0
Normal Psig
94.0
Mop Psig
100.0
Mop Cfr Section
192.619(A)(2)
Maop Established Date
2019-09-17 00:00:00
Accident Pressure
Pressure Did Not Exceed Maop
Gas Odorized System Type
Combination Of Odorization Types
Gas Odorized Level
5.2
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The pressure and flow rates were within normal ranges leading up to the incident and at the time the incident occurred. Actions by the control room did not impact the incident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Pipe, Weld, Or Joint Failure
Cause Details
Fusion Joint
Pwjf Failure Type
Fusion Joint
Plastic Joint Subtype
Butt, Heat Fusion
Fpw Installed Year
2019
Fpw First Plastic Type
Polyethylene (Pe)
Fpw Second Plastic Type
Polyethylene (Pe)
Additional Other Ind
Yes
Additional Factor Details
Inadequate Interfacial Pressure Being Applied During The Joining Phase Of The Fusion Process And/or Excessive Dwell Time Between Heat Soak And Joining Phases.
Result Construction Ind
Yes
Result Construction Subtype
Poor Workmanship
Hydrotest Conducted Ind
No
Io Follow Procedure Ind
Yes
Preparer Name
R**** H***
Preparer Title
Senior Engineer Standards
Preparer Email
R****@u**.com
Preparer Telephone
484-332-8402
Authorizer Name
T** A*******
Authorizer Title
Vp Operations
Authorizer Telephone
484-256-0345
Authorizer Email
T********@u**.com
Narrative
At approximately 1:44 am december 25, 2020, ugi employees responded to a call from monroe county 911 reporting an incident involving the release of natural gas. It was discovered that the 12-inch hdpe, 100 psig maop distribution pipeline had separated at the butt fusion interface from an unknown cause. There was one confirmed fatality and two injuries requiring hospitalization from an overturned vehicle. In response to the incident, the pipeline was repaired and placed back in operation. The pipeline operating pressure has been lowered from 94 psig to 60 psig as a precautionary measure. Ugi is filing this supplemental and final report after a third-party lab completed testing on the failed butt fusion joint and a root cause analysis. The root cause was determined to be a combination of the following factors: 1) inadequate interfacial pressure applied during the joining phase of the fusion process and/or excessive dwell time between heat soak and joining phases; and 2) the failure to follow appropriate installation and inspection procedures.
Occurred At 2020-12-25 01:44:00
Year 2020
Report Received Date 2021-01-24 00:00:00
Iyear 2020.0
Report Number 20210013.0
Supplemental Number 36706.0
Report Type Supplemental Final
Operator Id 20010 PHMSA Enforcement
Name Ugi Utilities, Inc
Operator Street Address 1 Ugi Drive
Operator City Name Denver
Operator State Abbreviation PA
Operator Postal Code 17517
Local Datetime 2020-12-25 01:30:00
Time Zone Eastern
Daylight Savings Ind No
Location Street Address 117 Lower Swiftwater Road
Location City Name Swiftwater
Location County Name Monroe
Location State Abbreviation PA
Location Postal Code 18370
Location Latitude 41.095368 Google Maps OpenStreetMap
Location Longitude -75.326474 Google Maps OpenStreetMap
Flow Cont Key Crit Ind Yes
Nrc Rpt Datetime 2020-12-25 04:58:00
Nrc Rpt Num 1294953 NRC Report How to search
Additional Nrc Report Numbers 1295037
Commodity Released Type Natural Gas
Unintentional Release 975.0
Intentional Release 0.0
Fatality Ind Yes
Num Emp Fatalities 0
Num Contr Fatalities 0
Num Er Fatalities 0
Num Worker Fatalities 0
Num Gp Fatalities 1
Fatal 1
Injury Ind Yes
Num Emp Injuries 0
Num Contr Injuries 0
Num Er Injuries 0
Num Worker Injuries 0
Num Gp Injuries 2
Injure 2
Ignite Ind No
Num Pub Evacuated 2.0
Incident Identified Datetime 2020-12-25 01:44:00
On Site Datetime 2020-12-25 02:07:00
Federal No
Location Type Public Property
Incident Area Type Underground
Incident Area Subtype Under Pavement
Depth Of Cover 36.0
Other Underground Facilities No
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Main
Installation Year 2019.0
Manufactured Year 2017.0
Pipe Diameter 12.0
Pipe Specification Astm D2513
Pipe Manufacturer Charter Plastics, Inc.
Material Involved Plastic
Plastic Type Polyethylene (Pe)
Plastic Sdr 11
Material Pe Pipe Code 4710
Release Type Rupture
Rupture Orient Circumferential
Rupture Length 12
Rupture Width 1.5
Class Location Type Class 3 Location
Est Cost Oper Paid 40000.0
Est Cost Prop Damage 39310.0
Est Cost Emergency 4615.0
Est Cost Other 0.0
Gas Cost In Mcf 2.2207
Est Cost Unintentional Release 2165.0
Est Cost Intentional Release 0.0
Prpty 86090.0
Commercial Affected 5.0
Industrial Affected 0.0
Residences Affected 0.0
Num Persons Hosp Not Ovnght 0.0
Num Injured Treated By Emt 0.0
Num Resident Building Affctd 0.0
Num Business Building Affctd 5.0
Accident Psig 95.0
Normal Psig 94.0
Mop Psig 100.0
Mop Cfr Section 192.619(A)(2) View CFR 49 §192
Maop Established Date 2019-09-17 00:00:00
Accident Pressure Pressure Did Not Exceed Maop
Gas Odorized System Type Combination Of Odorization Types
Gas Odorized Level 5.2
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Notification From Emergency Responder
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The pressure and flow rates were within normal ranges leading up to the incident and at the time the incident occurred. Actions by the control room did not impact the incident.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Pipe, Weld, Or Joint Failure
Cause Details Fusion Joint
Pwjf Failure Type Fusion Joint
Plastic Joint Subtype Butt, Heat Fusion
Fpw Installed Year 2019
Fpw First Plastic Type Polyethylene (Pe)
Fpw Second Plastic Type Polyethylene (Pe)
Additional Other Ind Yes
Additional Factor Details Inadequate Interfacial Pressure Being Applied During The Joining Phase Of The Fusion Process And/or Excessive Dwell Time Between Heat Soak And Joining Phases.
Result Construction Ind Yes
Result Construction Subtype Poor Workmanship
Hydrotest Conducted Ind No
Io Follow Procedure Ind Yes
Preparer Name R**** H***
Preparer Title Senior Engineer Standards
Preparer Email R****@u**.com
Preparer Telephone 484-332-8402
Authorizer Name T** A*******
Authorizer Title Vp Operations
Authorizer Telephone 484-256-0345
Authorizer Email T********@u**.com
Narrative At approximately 1:44 am december 25, 2020, ugi employees responded to a call from monroe county 911 reporting an incident involving the release of natural gas. It was discovered that the 12-inch hdpe, 100 psig maop distribution pipeline had separated at the butt fusion interface from an unknown cause. There was one confirmed fatality and two injuries requiring hospitalization from an overturned vehicle. In response to the incident, the pipeline was repaired and placed back in operation. The pipeline operating pressure has been lowered from 94 psig to 60 psig as a precautionary measure. Ugi is filing this supplemental and final report after a third-party lab completed testing on the failed butt fusion joint and a root cause analysis. The root cause was determined to be a combination of the following factors: 1) inadequate interfacial pressure applied during the joining phase of the fusion process and/or excessive dwell time between heat soak and joining phases; and 2) the failure to follow appropriate installation and inspection procedures.

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