GD incident on 2020-12-09 — NY

Operator
Rochester Gas & Electric Corp
Cause
Other Outside Force Damage
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$100
Incident datetime
2020-12-09 18:27
Report number
Location
NY, MONROE
Narrative
Rg&e was notified by 911 about an explosion and fire on noel dr. In gates, ny and dispatched personnel to respond in accordance with company procedures. In accordance with rg&e control room notification procedures, the nrc was notified on 12/9/2020 at 22:59 (report #1293962). A follow up call to the nrc for the required 24 hour update was assigned report #1294363. There are no reports of injuries related to the incident and the structure was extensively damaged. Local police and fire investigators deemed the incident was caused from a natural gas leak within the residence where the company was not at fault rg&e performed a leak survey in proximity to the incident in accordance with company o&m procedures and no underground leaks were identified. There are no reports of odor complaints or leaks discovered during routine surveys in the vicinity of the incident prior to december 9, 2020. At the recommendation of an engineer - investigator in the accident investigation division, the cause is being changed to: nearby industrial, man-made, or other fire/explosion as primary cause of incident. The actions that led to the incident were not done with criminal intent.
Detailed record list
Occurred At
2020-12-09 18:27:00
Year
2020
Report Received Date
2021-01-08 00:00:00
Iyear
2020.0
Report Number
20210005.0
Supplemental Number
35951.0
Report Type
Supplemental Final
Operator Id
Name
Rochester Gas & Electric Corp
Operator Street Address
180 South Clinton Avenue
Operator City Name
Rochester
Operator State Abbreviation
NY
Operator Postal Code
14607
Local Datetime
2020-12-09 18:27:00
Time Zone
Eastern
Daylight Savings Ind
No
Location Street Address
51 Noel Dr
Location City Name
Gates
Location County Name
Monroe
Location State Abbreviation
NY
Location Postal Code
14606
Location Latitude
Location Longitude
-77.70871212
Flow Cont Service Valve Ind
Yes
Nrc Rpt Datetime
2020-12-09 22:59:00
Nrc Rpt Num
Additional Nrc Report Numbers
1294363
Commodity Released Type
Natural Gas
Unintentional Release
1.0
Intentional Release
0.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
Yes
Ignite Datetime
2020-12-09 18:27:00
How Extinguished
Local/state/federal Emergency Responder
Gas Consumed By Fire In Mcf
1
Explode Ind
Yes
Num Pub Evacuated
7.0
Incident Identified Datetime
2020-12-09 18:27:00
On Site Datetime
2020-12-09 18:38:00
Federal
No
Location Type
Private Property
Incident Area Type
Aboveground
Incident Area Subtype
Inside A Building
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Inside Meter/regulator Set
Installation Year
2005.0
Customer Type
Single Family Residential
Was Efv Installed Before Ind
No
Curb Valve Inst Before Inc Ind
Yes
Material Involved
Other
Material Details
Aluminium Gas Meter
Release Type
Other
Release Type Details
There Is No Indication That Any Failure Of Company Equipment Contributed To The Cause Of The Event. The Incident Was The Result Of Actions Taken By The Customer/resident On Company Equipment.
Class Location Type
Class 3 Location
Est Cost Oper Paid
144800.0
Est Cost Prop Damage
100.0
Est Cost Emergency
5000.0
Est Cost Other
0.0
Gas Cost In Mcf
10.0
Est Cost Unintentional Release
10.0
Est Cost Intentional Release
0.0
Prpty
149910.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
3.0
Num Persons Hosp Not Ovnght
0.0
Num Injured Treated By Emt
0.0
Num Resident Building Affctd
3.0
Num Business Building Affctd
0.0
Accident Psig
59.0
Normal Psig
59.0
Mop Psig
60.0
Mop Cfr Section
192.619(A)(4)
Maop Established Date
1996-12-31 00:00:00
Accident Pressure
Pressure Did Not Exceed Maop
Gas Odorized System Type
Injection Pump
Gas Odorized Level
3.6
Scada In Place Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
There are no reports of gas odors or any other abnormal operation conditions prior to the incident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Outside Force Damage
Cause Details
Nearby Industrial, Man-Made, Or Other Fire/explosion As Primary Cause Of Incident
Outside Force Type
Nearby Industrial, Man-Made, Or Other Fire/explosion As Primary Cause Of Incident
Preparer Name
B**** K********
Preparer Title
Gas Engineering Manager
Preparer Email
B**************@r**.com
Preparer Telephone
585-771-4143
Authorizer Name
B**** K********
Authorizer Title
Gas Engineering Manager
Authorizer Telephone
585-771-4143
Authorizer Email
B**************@r**.com
Narrative
Rg&e was notified by 911 about an explosion and fire on noel dr. In gates, ny and dispatched personnel to respond in accordance with company procedures. In accordance with rg&e control room notification procedures, the nrc was notified on 12/9/2020 at 22:59 (report #1293962). A follow up call to the nrc for the required 24 hour update was assigned report #1294363. There are no reports of injuries related to the incident and the structure was extensively damaged. Local police and fire investigators deemed the incident was caused from a natural gas leak within the residence where the company was not at fault rg&e performed a leak survey in proximity to the incident in accordance with company o&m procedures and no underground leaks were identified. There are no reports of odor complaints or leaks discovered during routine surveys in the vicinity of the incident prior to december 9, 2020. At the recommendation of an engineer - investigator in the accident investigation division, the cause is being changed to: nearby industrial, man-made, or other fire/explosion as primary cause of incident. The actions that led to the incident were not done with criminal intent.
Occurred At 2020-12-09 18:27:00
Year 2020
Report Received Date 2021-01-08 00:00:00
Iyear 2020.0
Report Number 20210005.0
Supplemental Number 35951.0
Report Type Supplemental Final
Operator Id 17570 PHMSA Enforcement
Name Rochester Gas & Electric Corp
Operator Street Address 180 South Clinton Avenue
Operator City Name Rochester
Operator State Abbreviation NY
Operator Postal Code 14607
Local Datetime 2020-12-09 18:27:00
Time Zone Eastern
Daylight Savings Ind No
Location Street Address 51 Noel Dr
Location City Name Gates
Location County Name Monroe
Location State Abbreviation NY
Location Postal Code 14606
Location Latitude 43.16177787 Google Maps OpenStreetMap
Location Longitude -77.70871212 Google Maps OpenStreetMap
Flow Cont Service Valve Ind Yes
Nrc Rpt Datetime 2020-12-09 22:59:00
Nrc Rpt Num 1293962 NRC Report How to search
Additional Nrc Report Numbers 1294363
Commodity Released Type Natural Gas
Unintentional Release 1.0
Intentional Release 0.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind Yes
Ignite Datetime 2020-12-09 18:27:00
How Extinguished Local/state/federal Emergency Responder
Gas Consumed By Fire In Mcf 1
Explode Ind Yes
Num Pub Evacuated 7.0
Incident Identified Datetime 2020-12-09 18:27:00
On Site Datetime 2020-12-09 18:38:00
Federal No
Location Type Private Property
Incident Area Type Aboveground
Incident Area Subtype Inside A Building
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Inside Meter/regulator Set
Installation Year 2005.0
Customer Type Single Family Residential
Was Efv Installed Before Ind No
Curb Valve Inst Before Inc Ind Yes
Material Involved Other
Material Details Aluminium Gas Meter
Release Type Other
Release Type Details There Is No Indication That Any Failure Of Company Equipment Contributed To The Cause Of The Event. The Incident Was The Result Of Actions Taken By The Customer/resident On Company Equipment.
Class Location Type Class 3 Location
Est Cost Oper Paid 144800.0
Est Cost Prop Damage 100.0
Est Cost Emergency 5000.0
Est Cost Other 0.0
Gas Cost In Mcf 10.0
Est Cost Unintentional Release 10.0
Est Cost Intentional Release 0.0
Prpty 149910.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 3.0
Num Persons Hosp Not Ovnght 0.0
Num Injured Treated By Emt 0.0
Num Resident Building Affctd 3.0
Num Business Building Affctd 0.0
Accident Psig 59.0
Normal Psig 59.0
Mop Psig 60.0
Mop Cfr Section 192.619(A)(4) View CFR 49 §192
Maop Established Date 1996-12-31 00:00:00
Accident Pressure Pressure Did Not Exceed Maop
Gas Odorized System Type Injection Pump
Gas Odorized Level 3.6
Scada In Place Ind No
Accident Identifier Notification From Emergency Responder
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details There are no reports of gas odors or any other abnormal operation conditions prior to the incident.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Outside Force Damage
Cause Details Nearby Industrial, Man-Made, Or Other Fire/explosion As Primary Cause Of Incident
Outside Force Type Nearby Industrial, Man-Made, Or Other Fire/explosion As Primary Cause Of Incident
Preparer Name B**** K********
Preparer Title Gas Engineering Manager
Preparer Email B**************@r**.com
Preparer Telephone 585-771-4143
Authorizer Name B**** K********
Authorizer Title Gas Engineering Manager
Authorizer Telephone 585-771-4143
Authorizer Email B**************@r**.com
Narrative Rg&e was notified by 911 about an explosion and fire on noel dr. In gates, ny and dispatched personnel to respond in accordance with company procedures. In accordance with rg&e control room notification procedures, the nrc was notified on 12/9/2020 at 22:59 (report #1293962). A follow up call to the nrc for the required 24 hour update was assigned report #1294363. There are no reports of injuries related to the incident and the structure was extensively damaged. Local police and fire investigators deemed the incident was caused from a natural gas leak within the residence where the company was not at fault rg&e performed a leak survey in proximity to the incident in accordance with company o&m procedures and no underground leaks were identified. There are no reports of odor complaints or leaks discovered during routine surveys in the vicinity of the incident prior to december 9, 2020. At the recommendation of an engineer - investigator in the accident investigation division, the cause is being changed to: nearby industrial, man-made, or other fire/explosion as primary cause of incident. The actions that led to the incident were not done with criminal intent.

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