GTG incident on 2020-12-08 — NC

Operator
Piedmont Natural Gas Co Inc
Cause
Notification Issue
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$5,600,000
Incident datetime
2020-12-08 09:28
Report number
Location
NC
Narrative
A third-party contractor was replacing a bridge using a pile driver when a 10" steel transmission line was struck approximately 30 feet deep below water surface. 25 residents were initially evacuated and relocated at the time of incident. On the first day 18 residents were allowed back into the homes and 7 remained relocated for the duration of the leak. As location of pipeline and damage is in drilled section below water, pipe was not exposed; therefore, actual size of mechanical puncture is unknown.
Detailed record list
Report Received Date
2021-01-08 00:00:00
Iyear
2020
Report Number
20210003
Supplemental Number
35195
Report Type
Supplemental Final
Operator Id
Name
Piedmont Natural Gas Co Inc
Operator Street Address
525 South Tryon Street
Operator City Name
Charlotte
Operator State Abbreviation
NC
Operator Postal Code
28202
Local Datetime
2020-12-08 08:46:00
Time Zone
Eastern
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2020-12-08 12:38:00
Additional Nrc Report Numbers
1293931
Commodity Released Type
Natural Gas
Unintentional Release
4000
Intentional Release
0
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Status When Identified
Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind
No
Shutdown Explain
Pipeline Was Placed On A Bypass To Maintain Service.
Communication State Fed Ind
No
Ignite Ind
No
Upstream Action Taken
Operational Control
Upstream Oprtnl Cntrl Detail
Pressure Reduction And Mainline Valve Monitoring Until Bypass Completed.
Downstream Action Taken
Operational Control
Downstream Oprtnl Cntrl Detail
Pressure Reduction And Mainline Valve Monitoring Until Bypass Completed.
Num Pub Evacuated
25
Incident Identified Datetime
2020-12-08 09:28:00
On Site Datetime
2020-12-08 09:28:00
On Off Shore
Onshore
Onshore State Abbreviation
Nc
Onshore Postal Code
27944
Onshore City Name
Hertford
Onshore County Name
Perquimans
Designated Location
Survey Station No.
Designated Name
2641+00
Pipe Fac Name
Transmission Line 208
Segment Name
Line 208
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Other
Incident Area Details
Belowground Underwater
Depth Of Cover
360
Other Underground Facilities
No
Crossing
Yes
Water Crossing Ind
Yes
Water Type
Uncased
Water Name
Racoon Creek
Water Depth
11
Water Subtype
Below Water, Pipe In Bored/drilled Crossing
Crossing 100 Feet
Yes
Pipe Facility Type
Intrastate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
10
Puddle Weld Ind
No
Pipe Wall Thickness
0.256
Pipe Smys
42000
Pipe Specification
10 Inch 256 Api5l Grade X42
Pipe Seam Type
Longitudinal Erw - Unknown Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Other
Pipe Coating Details
Fbe With Powercrete
Coating Applied Ind
Unknown
Installation Year
2002
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Mechanical Puncture
Puncture Axial
1
Puncture Circum
1
Class Location Type
Class 3 Location
Could Be Hca
Yes
Determination Method
Method2
Pir Radius
195
Heat Damage Ind
No
Non Heat Damage Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
10000
Est Cost Intentional Release
0
Est Cost Prop Damage
5600000
Est Cost Emergency
1500000
Est Cost Other
0
Gas Cost In Mcf
2.5
Prpty
7110000
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
7
Num Business Building Affctd
0
Wildlife Impact Ind
No
Accident Psig
400
Gas Flow In Pipe In Mcf
2520
Mop Psig
800
Mop Cfr Section
192.619(A)(1)
Maop Established Date
2002-06-17 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Gas Required Odorized Ind
Yes
Gas Odorized Ind
Yes
Length Segment Isolated
38500
Internal Inspection Ind
No
Other Restrictions Ind
Yes
Operation Complications Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
Yes
Accident Identifier
Notification From Third Party That Caused The Incident
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
3rd party line damage.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
No
State Law Exempt Ind
No
Notify Cga Dirt
No
Public Row Ind
Yes
Public Subtype
Other
Excavator Type
Contractor
Excavator Equipment
Unknown/other
Work Performed
Road Work
One Call Notified Ind
No
Service Interruption
No
Root Cause Category
Notification Issue
Root Cause Type
No Notification Made To The One-Call Center/811
Preparer Name
C********** R******
Preparer Title
Gas Regulatory Compliance Analyst
Preparer Email
C******************@d**********.com
Preparer Telephone
704-731-4680
Authorizer Name
F***** B****
Authorizer Title
Manager- Pipeline Safety
Authorizer Telephone
704-731-4618
Authorizer Email
F***********@d**********.com
Narrative
A third-party contractor was replacing a bridge using a pile driver when a 10" steel transmission line was struck approximately 30 feet deep below water surface. 25 residents were initially evacuated and relocated at the time of incident. On the first day 18 residents were allowed back into the homes and 7 remained relocated for the duration of the leak. As location of pipeline and damage is in drilled section below water, pipe was not exposed; therefore, actual size of mechanical puncture is unknown.
Report Received Date 2021-01-08 00:00:00
Iyear 2020
Report Number 20210003
Supplemental Number 35195
Report Type Supplemental Final
Operator Id 15518 PHMSA Enforcement
Name Piedmont Natural Gas Co Inc
Operator Street Address 525 South Tryon Street
Operator City Name Charlotte
Operator State Abbreviation NC
Operator Postal Code 28202
Local Datetime 2020-12-08 08:46:00
Time Zone Eastern
Daylight Savings Ind Yes
Location Latitude 36.173117 Google Maps OpenStreetMap
Location Longitude -76.472405 Google Maps OpenStreetMap
Nrc Rpt Num 1293797 NRC Report How to search
Nrc Rpt Datetime 2020-12-08 12:38:00
Additional Nrc Report Numbers 1293931
Commodity Released Type Natural Gas
Unintentional Release 4000
Intentional Release 0
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Status When Identified Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind No
Shutdown Explain Pipeline Was Placed On A Bypass To Maintain Service.
Communication State Fed Ind No
Ignite Ind No
Upstream Action Taken Operational Control
Upstream Oprtnl Cntrl Detail Pressure Reduction And Mainline Valve Monitoring Until Bypass Completed.
Downstream Action Taken Operational Control
Downstream Oprtnl Cntrl Detail Pressure Reduction And Mainline Valve Monitoring Until Bypass Completed.
Num Pub Evacuated 25
Incident Identified Datetime 2020-12-08 09:28:00
On Site Datetime 2020-12-08 09:28:00
On Off Shore Onshore
Onshore State Abbreviation Nc
Onshore Postal Code 27944
Onshore City Name Hertford
Onshore County Name Perquimans
Designated Location Survey Station No.
Designated Name 2641+00
Pipe Fac Name Transmission Line 208
Segment Name Line 208
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Other
Incident Area Details Belowground Underwater
Depth Of Cover 360
Other Underground Facilities No
Crossing Yes
Water Crossing Ind Yes
Water Type Uncased
Water Name Racoon Creek
Water Depth 11
Water Subtype Below Water, Pipe In Bored/drilled Crossing
Crossing 100 Feet Yes
Pipe Facility Type Intrastate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 10
Puddle Weld Ind No
Pipe Wall Thickness 0.256
Pipe Smys 42000
Pipe Specification 10 Inch 256 Api5l Grade X42
Pipe Seam Type Longitudinal Erw - Unknown Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Other
Pipe Coating Details Fbe With Powercrete
Coating Applied Ind Unknown
Installation Year 2002
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Mechanical Puncture
Puncture Axial 1
Puncture Circum 1
Class Location Type Class 3 Location
Could Be Hca Yes
Determination Method Method2
Pir Radius 195
Heat Damage Ind No
Non Heat Damage Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 10000
Est Cost Intentional Release 0
Est Cost Prop Damage 5600000
Est Cost Emergency 1500000
Est Cost Other 0
Gas Cost In Mcf 2.5
Prpty 7110000
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 7
Num Business Building Affctd 0
Wildlife Impact Ind No
Accident Psig 400
Gas Flow In Pipe In Mcf 2520
Mop Psig 800
Mop Cfr Section 192.619(A)(1) View CFR 49 §192
Maop Established Date 2002-06-17 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Gas Required Odorized Ind Yes
Gas Odorized Ind Yes
Length Segment Isolated 38500
Internal Inspection Ind No
Other Restrictions Ind Yes
Operation Complications Ind No
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind Yes
Accident Identifier Notification From Third Party That Caused The Incident
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details 3rd party line damage.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind No
State Law Exempt Ind No
Notify Cga Dirt No
Public Row Ind Yes
Public Subtype Other
Excavator Type Contractor
Excavator Equipment Unknown/other
Work Performed Road Work
One Call Notified Ind No
Service Interruption No
Root Cause Category Notification Issue
Root Cause Type No Notification Made To The One-Call Center/811
Preparer Name C********** R******
Preparer Title Gas Regulatory Compliance Analyst
Preparer Email C******************@d**********.com
Preparer Telephone 704-731-4680
Authorizer Name F***** B****
Authorizer Title Manager- Pipeline Safety
Authorizer Telephone 704-731-4618
Authorizer Email F***********@d**********.com
Narrative A third-party contractor was replacing a bridge using a pile driver when a 10" steel transmission line was struck approximately 30 feet deep below water surface. 25 residents were initially evacuated and relocated at the time of incident. On the first day 18 residents were allowed back into the homes and 7 remained relocated for the duration of the leak. As location of pipeline and damage is in drilled section below water, pipe was not exposed; therefore, actual size of mechanical puncture is unknown.

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