HL incident on 2020-11-22 — PA

Operator
Buckeye Partners, Lp
Cause
Material Failure Of Pipe Or Weld
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$250,000
Incident datetime
2020-11-22 13:30
Report number
Location
PA
Narrative
At 13:30 on november 22, 2020 an employee of conoco phillips refinery, roxanna ill, notified several pipeline operators, including buckeye, of an odor and sheen on the water in the norfolk southern rail road drainage ditch. Buckeye's 180 line was on a scheduled shut down at the time the expected release was reported. Valves upstream and downstream of the refinery were immediately closed and potholing and exploratory investigation begun. Buckeye confirmed the leak was from our wo180xx, 6" pipeline at 11:35 on november 24, 2020. The nrc and was notified on november 24, 2020 at 12:28 (report number 1292933). Extensive booming and shoring was undertaken to insure leak containment. An estimated 47 bbls was released, to date 17, bbls have been recovered. The affected segment of pipe has been removed and sent for metallurgical analysis. A new section of pipe was installed and the pipeline returned to service on december 2, 2020. The root cause of the release is pending and will be provided by entering a supplemental report upon completion of the metallurgical analysis update 1/8/2020: discovery time and arrival time modified update 6/1/2020: metallurgical report - the results of the analysis indicate that the leak in the carrier pipe was caused by external corrosion, and the leak in side stream weld of the repair sleeve was caused by a crack in the weld metal. Misalignment at the sleeve edges contributed to inadequate penetration at the weld root and a stress concentrator at the weld root that caused the weld to crack when the sleeve became pressurized. The sleeve was presumably installed to mitigate the corrosion. The failure of the sleeve repair is the applicable cause associated with this incident. Buckeye started operating the pipe in 2004.
Detailed record list
Report Received Date
2020-12-23 00:00:00
Iyear
2020
Report Number
20200338
Supplemental Number
35729
Report Type
Supplemental Final
Operator Id
Name
Buckeye Partners, Lp
Operator Street Address
The Buckeye Building 6161 Hamilton Boulevar
Operator City Name
Allentown
Operator State Abbreviation
PA
Operator Postal Code
18106
Local Datetime
2020-11-22 13:30:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
47
Recovered Bbls
17
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2020-11-22 13:30:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Line Was Not Running At The Time Of Discovery,it Was Shut Down 2 Days Earlier
On Site Datetime
2020-11-23 07:00:00
Nrc Rpt Datetime
2020-11-24 12:28:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Wo180xx
Segment Name
Wo180xx
Onshore State Abbreviation
Il
Onshore Postal Code
62084
Onshore City Name
Roxanna
Onshore County Name
Madison
Designated Location
Milepost/valve Station
Designated Name
Wo180xx
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
48
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Weld, Including Heat-Affected Zone
Weld Subtype
Other Butt Weld
Installation Year
2014
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Surface Water Remed Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
Yes
Surface Contam Ind
Yes
Amount Released
17
Rel Water Name
Norfolk Southern Rail Road Drainage Ditch
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
1910
Est Cost Prop Damage
250000
Est Cost Emergency
500000
Est Cost Environmental
300000
Est Cost Other
0
Prpty
1051910
Accident Psig
125
Mop Psig
1425
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
15575
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Design-, Construction-, Installation-, Or Fabrication-Related
Metallurgical Ind
Yes
Failure Type
Design-, Construction-, Installation-, Or Fabrication-Related
Other Factor
Yes
Other Factor Details
Inadequate Root Bead Penetration
Additional Crack Ind
Yes
Pwf Addl Misalignment Ind
Yes
Collected Data Ind
Yes
Other Recent Year
2020
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
J**** P*****
Preparer Title
Regional Compliance Specialist
Preparer Email
J*******@b******.com
Preparer Telephone
219-796-8225
Prepared Date
2021-09-13 00:00:00
Authorizer Name
C****** P********
Authorizer Telephone
610-904-4113
Authorizer Title
Director - Regulatory Compliance
Authorizer Email
C*********@b******.com
Narrative
At 13:30 on november 22, 2020 an employee of conoco phillips refinery, roxanna ill, notified several pipeline operators, including buckeye, of an odor and sheen on the water in the norfolk southern rail road drainage ditch. Buckeye's 180 line was on a scheduled shut down at the time the expected release was reported. Valves upstream and downstream of the refinery were immediately closed and potholing and exploratory investigation begun. Buckeye confirmed the leak was from our wo180xx, 6" pipeline at 11:35 on november 24, 2020. The nrc and was notified on november 24, 2020 at 12:28 (report number 1292933). Extensive booming and shoring was undertaken to insure leak containment. An estimated 47 bbls was released, to date 17, bbls have been recovered. The affected segment of pipe has been removed and sent for metallurgical analysis. A new section of pipe was installed and the pipeline returned to service on december 2, 2020. The root cause of the release is pending and will be provided by entering a supplemental report upon completion of the metallurgical analysis update 1/8/2020: discovery time and arrival time modified update 6/1/2020: metallurgical report - the results of the analysis indicate that the leak in the carrier pipe was caused by external corrosion, and the leak in side stream weld of the repair sleeve was caused by a crack in the weld metal. Misalignment at the sleeve edges contributed to inadequate penetration at the weld root and a stress concentrator at the weld root that caused the weld to crack when the sleeve became pressurized. The sleeve was presumably installed to mitigate the corrosion. The failure of the sleeve repair is the applicable cause associated with this incident. Buckeye started operating the pipe in 2004.
Report Received Date 2020-12-23 00:00:00
Iyear 2020
Report Number 20200338
Supplemental Number 35729
Report Type Supplemental Final
Operator Id 1845 PHMSA Enforcement
Name Buckeye Partners, Lp
Operator Street Address The Buckeye Building 6161 Hamilton Boulevar
Operator City Name Allentown
Operator State Abbreviation PA
Operator Postal Code 18106
Local Datetime 2020-11-22 13:30:00
Location Latitude 38.8412019 Google Maps OpenStreetMap
Location Longitude -90.0764591 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 47
Recovered Bbls 17
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2020-11-22 13:30:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Line Was Not Running At The Time Of Discovery,it Was Shut Down 2 Days Earlier
On Site Datetime 2020-11-23 07:00:00
Nrc Rpt Datetime 2020-11-24 12:28:00
Nrc Rpt Num 1292933 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Wo180xx
Segment Name Wo180xx
Onshore State Abbreviation Il
Onshore Postal Code 62084
Onshore City Name Roxanna
Onshore County Name Madison
Designated Location Milepost/valve Station
Designated Name Wo180xx
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 48
Crossing No
Pipe Facility Type Interstate
Item Involved Weld, Including Heat-Affected Zone
Weld Subtype Other Butt Weld
Installation Year 2014
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Surface Water Remed Ind Yes
Soil Remed Ind Yes
Water Contam Ind Yes
Surface Contam Ind Yes
Amount Released 17
Rel Water Name Norfolk Southern Rail Road Drainage Ditch
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 1910
Est Cost Prop Damage 250000
Est Cost Emergency 500000
Est Cost Environmental 300000
Est Cost Other 0
Prpty 1051910
Accident Psig 125
Mop Psig 1425
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 15575
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Design-, Construction-, Installation-, Or Fabrication-Related
Metallurgical Ind Yes
Failure Type Design-, Construction-, Installation-, Or Fabrication-Related
Other Factor Yes
Other Factor Details Inadequate Root Bead Penetration
Additional Crack Ind Yes
Pwf Addl Misalignment Ind Yes
Collected Data Ind Yes
Other Recent Year 2020
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name J**** P*****
Preparer Title Regional Compliance Specialist
Preparer Email J*******@b******.com
Preparer Telephone 219-796-8225
Prepared Date 2021-09-13 00:00:00
Authorizer Name C****** P********
Authorizer Telephone 610-904-4113
Authorizer Title Director - Regulatory Compliance
Authorizer Email C*********@b******.com
Narrative At 13:30 on november 22, 2020 an employee of conoco phillips refinery, roxanna ill, notified several pipeline operators, including buckeye, of an odor and sheen on the water in the norfolk southern rail road drainage ditch. Buckeye's 180 line was on a scheduled shut down at the time the expected release was reported. Valves upstream and downstream of the refinery were immediately closed and potholing and exploratory investigation begun. Buckeye confirmed the leak was from our wo180xx, 6" pipeline at 11:35 on november 24, 2020. The nrc and was notified on november 24, 2020 at 12:28 (report number 1292933). Extensive booming and shoring was undertaken to insure leak containment. An estimated 47 bbls was released, to date 17, bbls have been recovered. The affected segment of pipe has been removed and sent for metallurgical analysis. A new section of pipe was installed and the pipeline returned to service on december 2, 2020. The root cause of the release is pending and will be provided by entering a supplemental report upon completion of the metallurgical analysis update 1/8/2020: discovery time and arrival time modified update 6/1/2020: metallurgical report - the results of the analysis indicate that the leak in the carrier pipe was caused by external corrosion, and the leak in side stream weld of the repair sleeve was caused by a crack in the weld metal. Misalignment at the sleeve edges contributed to inadequate penetration at the weld root and a stress concentrator at the weld root that caused the weld to crack when the sleeve became pressurized. The sleeve was presumably installed to mitigate the corrosion. The failure of the sleeve repair is the applicable cause associated with this incident. Buckeye started operating the pipe in 2004.

All rights reserved. Copyright © by ClearPHMSA