HL incident on 2020-12-03 — TX

Operator
Wink To Webster Pipeline, Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2020-12-03 13:44
Report number
Location
TX
Narrative
On december 3 at approximately 13:44 enterprise personnel notified the exxonmobil pipeline company (empco) occ of a spill at the wink to webster pipeline echo station which is located within the enterprise tank farm. Empco occ shut the pipeline down and isolated the facility at 13:58. Empco personnel arrived onsite at approximately 14:17 and confirmed the spill. Empco made the appropriate regulatory notifications. Empco responded and cleaned up the spill site. Empco has removed all similar flow switch devices from the wink to webster pipeline system pending the outcome of the investigation. Update: 1/15/2021 filed supplemental report with the following information. Please note, the cause of the bellows seal fail is still under investigation pending discussions with the vendor and an additional supplemental report will be filed once completed. Updated part g, selected g6 - equipment failure, other and listed "bellows seal on flow switch" updated part d, 8 with cost information. Update 2/10/21 -updated part g.6 #6 - additional factors that contributed to the equipment failure: excessive pulsation of the flow switch paddle caused the equipment failure, which was due to the location of the switch being downstream of a control valve, created excessive flow pulsation conditions. Updated information 2/10/21 - the flow switch was removed from the location and will not be replaced. Updated 10/5/2021 - updated section g6 to non-threaded connection per PHMSA's request. (please note: exxonmobil pipeline company is the contractual services provider for wink to webster pipeline, llc)
Detailed record list
Report Received Date
2020-12-18 00:00:00
Iyear
2020
Report Number
20200334
Supplemental Number
35824
Report Type
Supplemental Final
Operator Id
Name
Wink To Webster Pipeline, Llc
Operator Street Address
22777 Springwoods Village Parkway E2.2b-Emp
Operator City Name
Spring
Operator State Abbreviation
TX
Operator Postal Code
77389
Local Datetime
2020-12-03 13:44:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
1.2
Recovered Bbls
1.2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Other
Accident Details
Third Party Operator
Incident Identified Datetime
2020-12-03 13:44:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2020-12-03 13:42:00
Restart Datetime
2020-12-07 14:15:00
On Site Datetime
2020-12-03 14:17:00
Nrc Rpt Datetime
2020-12-03 15:08:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Echo Station
Segment Name
Wink To Webster 36" Pipeline At Echo Station
Onshore State Abbreviation
Tx
Onshore Postal Code
77034
Onshore City Name
Houston
Onshore County Name
Harris
Designated Location
Survey Station No.
Designated Name
6849 East Sam
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Other
Item Involved Details
Flow Switch
Installation Year
2020
Material Involved
Material Other Than Carbon Steel
Material Details
O" Ring
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
50
Est Cost Prop Damage
0
Est Cost Emergency
0
Est Cost Environmental
81000
Est Cost Other
0
Prpty
81050
Accident Psig
27
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Not occ related
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Other
Other Non Threaded Details
Bellows Seal On Flow Switch.
Eq Additional Other Ind
Yes
Eq Additional Other Details
Excessive Pulsation On Flow Switch Paddle
Preparer Name
R***** P S**********
Preparer Title
Pipeline Safety Advisor
Preparer Email
R*******************@e*********.com
Preparer Telephone
832-625-3838
Prepared Date
2021-10-05 00:00:00
Authorizer Name
C******* B* H********
Authorizer Telephone
832-624-7920
Authorizer Title
Empco Sshe Manager
Authorizer Email
C*******************@e*********.com
Narrative
On december 3 at approximately 13:44 enterprise personnel notified the exxonmobil pipeline company (empco) occ of a spill at the wink to webster pipeline echo station which is located within the enterprise tank farm. Empco occ shut the pipeline down and isolated the facility at 13:58. Empco personnel arrived onsite at approximately 14:17 and confirmed the spill. Empco made the appropriate regulatory notifications. Empco responded and cleaned up the spill site. Empco has removed all similar flow switch devices from the wink to webster pipeline system pending the outcome of the investigation. Update: 1/15/2021 filed supplemental report with the following information. Please note, the cause of the bellows seal fail is still under investigation pending discussions with the vendor and an additional supplemental report will be filed once completed. Updated part g, selected g6 - equipment failure, other and listed "bellows seal on flow switch" updated part d, 8 with cost information. Update 2/10/21 -updated part g.6 #6 - additional factors that contributed to the equipment failure: excessive pulsation of the flow switch paddle caused the equipment failure, which was due to the location of the switch being downstream of a control valve, created excessive flow pulsation conditions. Updated information 2/10/21 - the flow switch was removed from the location and will not be replaced. Updated 10/5/2021 - updated section g6 to non-threaded connection per PHMSA's request. (please note: exxonmobil pipeline company is the contractual services provider for wink to webster pipeline, llc)
Report Received Date 2020-12-18 00:00:00
Iyear 2020
Report Number 20200334
Supplemental Number 35824
Report Type Supplemental Final
Operator Id 40026 PHMSA Enforcement
Name Wink To Webster Pipeline, Llc
Operator Street Address 22777 Springwoods Village Parkway E2.2b-Emp
Operator City Name Spring
Operator State Abbreviation TX
Operator Postal Code 77389
Local Datetime 2020-12-03 13:44:00
Location Latitude 29.6121071 Google Maps OpenStreetMap
Location Longitude -95.186078 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 1.2
Recovered Bbls 1.2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Other
Accident Details Third Party Operator
Incident Identified Datetime 2020-12-03 13:44:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2020-12-03 13:42:00
Restart Datetime 2020-12-07 14:15:00
On Site Datetime 2020-12-03 14:17:00
Nrc Rpt Datetime 2020-12-03 15:08:00
Nrc Rpt Num 1293469 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Echo Station
Segment Name Wink To Webster 36" Pipeline At Echo Station
Onshore State Abbreviation Tx
Onshore Postal Code 77034
Onshore City Name Houston
Onshore County Name Harris
Designated Location Survey Station No.
Designated Name 6849 East Sam
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Other
Item Involved Details Flow Switch
Installation Year 2020
Material Involved Material Other Than Carbon Steel
Material Details O" Ring
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 50
Est Cost Prop Damage 0
Est Cost Emergency 0
Est Cost Environmental 81000
Est Cost Other 0
Prpty 81050
Accident Psig 27
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Not occ related
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Other
Other Non Threaded Details Bellows Seal On Flow Switch.
Eq Additional Other Ind Yes
Eq Additional Other Details Excessive Pulsation On Flow Switch Paddle
Preparer Name R***** P S**********
Preparer Title Pipeline Safety Advisor
Preparer Email R*******************@e*********.com
Preparer Telephone 832-625-3838
Prepared Date 2021-10-05 00:00:00
Authorizer Name C******* B* H********
Authorizer Telephone 832-624-7920
Authorizer Title Empco Sshe Manager
Authorizer Email C*******************@e*********.com
Narrative On december 3 at approximately 13:44 enterprise personnel notified the exxonmobil pipeline company (empco) occ of a spill at the wink to webster pipeline echo station which is located within the enterprise tank farm. Empco occ shut the pipeline down and isolated the facility at 13:58. Empco personnel arrived onsite at approximately 14:17 and confirmed the spill. Empco made the appropriate regulatory notifications. Empco responded and cleaned up the spill site. Empco has removed all similar flow switch devices from the wink to webster pipeline system pending the outcome of the investigation. Update: 1/15/2021 filed supplemental report with the following information. Please note, the cause of the bellows seal fail is still under investigation pending discussions with the vendor and an additional supplemental report will be filed once completed. Updated part g, selected g6 - equipment failure, other and listed "bellows seal on flow switch" updated part d, 8 with cost information. Update 2/10/21 -updated part g.6 #6 - additional factors that contributed to the equipment failure: excessive pulsation of the flow switch paddle caused the equipment failure, which was due to the location of the switch being downstream of a control valve, created excessive flow pulsation conditions. Updated information 2/10/21 - the flow switch was removed from the location and will not be replaced. Updated 10/5/2021 - updated section g6 to non-threaded connection per PHMSA's request. (please note: exxonmobil pipeline company is the contractual services provider for wink to webster pipeline, llc)

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