HL incident on 2020-11-29 — KS

Operator
Nustar Pipeline Operating Partnership L.p.
Cause
Notification Issue
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$5,000
Incident datetime
2020-11-29 11:40
Report number
Location
KS
Narrative
On 11/29/2020 at 1140, a farmer caused third-party damage and a reportable release with a plow/box scraper. The farmer called the control center when he observed a mist and small amount of pooling of x-grade product after hitting our line. The location was mp 118.28 on council bluffs to sioux falls line segment. Response activities were initiated. Local operations staff were dispatched and closed upstream and downstream valves from the affected area. The maintenance crew was also dispatched and was able to put a clamp over the damaged section of the pipe on 11/29/2020, stopping the further release of the product. The damaged pipeline section was cut out on 12/3/2020 and replaced. The line was restarted at 1600. 90 cubic yards of soil was remediated, and taken to pheasant point land fill near omaha, ne for disposal. The calculated volume of the release was 578.1 gallons (13.76 barrels). Proper notifications were made.
Detailed record list
Report Received Date
2020-12-15 00:00:00
Iyear
2020
Report Number
20200331
Supplemental Number
34703
Report Type
Supplemental Final
Operator Id
Name
Nustar Pipeline Operating Partnership L.p.
Operator Street Address
7340 W 21 St N
Operator City Name
Wichita
Operator State Abbreviation
KS
Operator Postal Code
67205
Local Datetime
2020-11-29 11:20:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
13.76
Recovered Bbls
13.76
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Third Party That Caused The Accident
Incident Identified Datetime
2020-11-29 11:40:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
The Line Was Not Running When It Was Struck
On Site Datetime
2020-11-29 13:12:00
Nrc Rpt Datetime
2020-11-29 12:39:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Sioux City Jct. - Hawarden Jct.
Segment Name
Whiskey Creek - Sioux Falls
Onshore State Abbreviation
Ia
Onshore Postal Code
51001
Onshore City Name
Akron
Onshore County Name
Plymouth
Designated Location
Milepost/valve Station
Designated Name
Mp 118.28
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
12
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
6
Pipe Wall Thickness
0.25
Pipe Smys
35000
Pipe Specification
Api 5l-B
Pipe Seam Type
Seamless
Pipe Manufacturer
Unknown
Pipe Coating Type
Coal Tar
Installation Year
1941
Manufactured Year
1941
Material Involved
Carbon Steel
Release Type
Mechanical Puncture
Puncture Axial
1
Puncture Circum
1
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
650
Est Cost Prop Damage
5000
Est Cost Emergency
9500
Est Cost Environmental
29850
Est Cost Other
0
Prpty
45000
Accident Psig
325
Mop Psig
1232
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
21226
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
No control center operator actions contributed to the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
No
Notify Cga Dirt
Yes
Private Row Ind
Yes
Private Subtype
Private Landowner
Pipeline Easement Row Ind
Yes
Excavator Type
Farmer
Excavator Equipment
Farm Equipment
Work Performed
Agriculture
One Call Notified Ind
No
Service Interruption
Unknown/other
Root Cause Category
Notification Issue
Root Cause Type
No Notification Made To The One-Call Center/811
Preparer Name
K*** P****
Preparer Title
Pipeline Safety Supervisor
Preparer Email
K*********@n***********.com
Preparer Telephone
13167217053
Prepared Date
2021-01-08 00:00:00
Authorizer Name
B*** F******
Authorizer Telephone
316-721-7066
Authorizer Title
General Manager - Central East Region
Authorizer Email
B***********@n***********.com
Narrative
On 11/29/2020 at 1140, a farmer caused third-party damage and a reportable release with a plow/box scraper. The farmer called the control center when he observed a mist and small amount of pooling of x-grade product after hitting our line. The location was mp 118.28 on council bluffs to sioux falls line segment. Response activities were initiated. Local operations staff were dispatched and closed upstream and downstream valves from the affected area. The maintenance crew was also dispatched and was able to put a clamp over the damaged section of the pipe on 11/29/2020, stopping the further release of the product. The damaged pipeline section was cut out on 12/3/2020 and replaced. The line was restarted at 1600. 90 cubic yards of soil was remediated, and taken to pheasant point land fill near omaha, ne for disposal. The calculated volume of the release was 578.1 gallons (13.76 barrels). Proper notifications were made.
Report Received Date 2020-12-15 00:00:00
Iyear 2020
Report Number 20200331
Supplemental Number 34703
Report Type Supplemental Final
Operator Id 10012 PHMSA Enforcement
Name Nustar Pipeline Operating Partnership L.p.
Operator Street Address 7340 W 21 St N
Operator City Name Wichita
Operator State Abbreviation KS
Operator Postal Code 67205
Local Datetime 2020-11-29 11:20:00
Location Latitude 42.8288595 Google Maps OpenStreetMap
Location Longitude -96.4060063 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 13.76
Recovered Bbls 13.76
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Third Party That Caused The Accident
Incident Identified Datetime 2020-11-29 11:40:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain The Line Was Not Running When It Was Struck
On Site Datetime 2020-11-29 13:12:00
Nrc Rpt Datetime 2020-11-29 12:39:00
Nrc Rpt Num 1293188 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Sioux City Jct. - Hawarden Jct.
Segment Name Whiskey Creek - Sioux Falls
Onshore State Abbreviation Ia
Onshore Postal Code 51001
Onshore City Name Akron
Onshore County Name Plymouth
Designated Location Milepost/valve Station
Designated Name Mp 118.28
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 12
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 6
Pipe Wall Thickness 0.25
Pipe Smys 35000
Pipe Specification Api 5l-B
Pipe Seam Type Seamless
Pipe Manufacturer Unknown
Pipe Coating Type Coal Tar
Installation Year 1941
Manufactured Year 1941
Material Involved Carbon Steel
Release Type Mechanical Puncture
Puncture Axial 1
Puncture Circum 1
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 650
Est Cost Prop Damage 5000
Est Cost Emergency 9500
Est Cost Environmental 29850
Est Cost Other 0
Prpty 45000
Accident Psig 325
Mop Psig 1232
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 21226
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details No control center operator actions contributed to the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind No
Notify Cga Dirt Yes
Private Row Ind Yes
Private Subtype Private Landowner
Pipeline Easement Row Ind Yes
Excavator Type Farmer
Excavator Equipment Farm Equipment
Work Performed Agriculture
One Call Notified Ind No
Service Interruption Unknown/other
Root Cause Category Notification Issue
Root Cause Type No Notification Made To The One-Call Center/811
Preparer Name K*** P****
Preparer Title Pipeline Safety Supervisor
Preparer Email K*********@n***********.com
Preparer Telephone 13167217053
Prepared Date 2021-01-08 00:00:00
Authorizer Name B*** F******
Authorizer Telephone 316-721-7066
Authorizer Title General Manager - Central East Region
Authorizer Email B***********@n***********.com
Narrative On 11/29/2020 at 1140, a farmer caused third-party damage and a reportable release with a plow/box scraper. The farmer called the control center when he observed a mist and small amount of pooling of x-grade product after hitting our line. The location was mp 118.28 on council bluffs to sioux falls line segment. Response activities were initiated. Local operations staff were dispatched and closed upstream and downstream valves from the affected area. The maintenance crew was also dispatched and was able to put a clamp over the damaged section of the pipe on 11/29/2020, stopping the further release of the product. The damaged pipeline section was cut out on 12/3/2020 and replaced. The line was restarted at 1600. 90 cubic yards of soil was remediated, and taken to pheasant point land fill near omaha, ne for disposal. The calculated volume of the release was 578.1 gallons (13.76 barrels). Proper notifications were made.

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