HL incident on 2020-11-17 — TX

Operator
Enterprise Products Operating Llc
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$184,000
Incident datetime
2020-11-17 08:23
Report number
Location
TX
Narrative
On 11/17/2020 at 08:08 ct, houston control center (hcc) was contacted by an enterprise technician reporting that a third party observed vapor at linn station. Hcc shut down the pump units while the technician was in-route to the station. Once on site at 08:23 ct the technician discovered frost on the ground above lid 428 pipeline inside the station. At 08:34 ct houston control center reduced the pressure and isolated the pipeline. After discussions with operations and onsite technician, at 09:40 ct it was determined that the estimated repair cost would likely exceed the $50,000 reporting threshold for nrc. An estimated 25 gallons of propane leaked from the pipeline with 50 barrels flared from the line prior to the nitrogen purge allowing for excavation and repair. Once excavated a stopple split tee fitting was found to be the source of the leak and was cut out and replaced with 40 feet of pipe. The pipeline was returned to service on 11/22/2020 at 17:00 ct. Initial call to nrc was made on 11/17/2020 at 10:17 ct (nrc#1292452). The call was made based on repair cost estimates exceeding $50,000. 48hr update call to nrc was made on 11/19/2020 (nrc#1292636). The update provided an estimated product release of 25 gallons.
Detailed record list
Report Received Date
2020-12-14 00:00:00
Iyear
2020
Report Number
20200329
Supplemental Number
34723
Report Type
Supplemental Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2020-11-17 08:08:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
0.6
Intentional Release Bbls
50
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2020-11-17 08:23:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2020-11-17 08:34:00
Restart Datetime
2020-11-22 17:00:00
On Site Datetime
2020-11-17 08:23:00
Nrc Rpt Datetime
2020-11-17 10:17:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
West Leg Loop
Segment Name
428
Onshore State Abbreviation
Ks
Onshore Postal Code
66953
Onshore City Name
Not Within A Municipality
Onshore County Name
Washington
Designated Location
Milepost/valve Station
Designated Name
Linn Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
48
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tap Fitting(Stopple, Thread-O-Ring, Weld-O-Let, Etc.)
Installation Year
Unknown
Material Involved
Material Other Than Carbon Steel
Material Details
Buna N O-Ring
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
1120
Est Cost Prop Damage
184000
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
185120
Accident Psig
1220
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
47857
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Pl controller did not contribute to the cause of this incident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
O-Ring
Eq Additional Other Ind
Yes
Eq Additional Other Details
Deterioration Of The O-Ring
Preparer Name
H*** D***
Preparer Title
Sr. Pipeline Compliance Engineer
Preparer Email
H****@e****.com
Preparer Telephone
713-381-4277
Prepared Date
2021-01-14 00:00:00
Authorizer Name
H*** D***
Authorizer Telephone
713-381-4277
Authorizer Title
Sr. Pipeline Compliance Engineer
Authorizer Email
H****@e****.com
Narrative
On 11/17/2020 at 08:08 ct, houston control center (hcc) was contacted by an enterprise technician reporting that a third party observed vapor at linn station. Hcc shut down the pump units while the technician was in-route to the station. Once on site at 08:23 ct the technician discovered frost on the ground above lid 428 pipeline inside the station. At 08:34 ct houston control center reduced the pressure and isolated the pipeline. After discussions with operations and onsite technician, at 09:40 ct it was determined that the estimated repair cost would likely exceed the $50,000 reporting threshold for nrc. An estimated 25 gallons of propane leaked from the pipeline with 50 barrels flared from the line prior to the nitrogen purge allowing for excavation and repair. Once excavated a stopple split tee fitting was found to be the source of the leak and was cut out and replaced with 40 feet of pipe. The pipeline was returned to service on 11/22/2020 at 17:00 ct. Initial call to nrc was made on 11/17/2020 at 10:17 ct (nrc#1292452). The call was made based on repair cost estimates exceeding $50,000. 48hr update call to nrc was made on 11/19/2020 (nrc#1292636). The update provided an estimated product release of 25 gallons.
Report Received Date 2020-12-14 00:00:00
Iyear 2020
Report Number 20200329
Supplemental Number 34723
Report Type Supplemental Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2020-11-17 08:08:00
Location Latitude 39.63882 Google Maps OpenStreetMap
Location Longitude -97.04227 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 0.6
Intentional Release Bbls 50
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
Incident Identified Datetime 2020-11-17 08:23:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2020-11-17 08:34:00
Restart Datetime 2020-11-22 17:00:00
On Site Datetime 2020-11-17 08:23:00
Nrc Rpt Datetime 2020-11-17 10:17:00
Nrc Rpt Num 1292452 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name West Leg Loop
Segment Name 428
Onshore State Abbreviation Ks
Onshore Postal Code 66953
Onshore City Name Not Within A Municipality
Onshore County Name Washington
Designated Location Milepost/valve Station
Designated Name Linn Station
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 48
Crossing No
Pipe Facility Type Interstate
Item Involved Tap Fitting(Stopple, Thread-O-Ring, Weld-O-Let, Etc.)
Installation Year Unknown
Material Involved Material Other Than Carbon Steel
Material Details Buna N O-Ring
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 1120
Est Cost Prop Damage 184000
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 185120
Accident Psig 1220
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 47857
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Pl controller did not contribute to the cause of this incident.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind O-Ring
Eq Additional Other Ind Yes
Eq Additional Other Details Deterioration Of The O-Ring
Preparer Name H*** D***
Preparer Title Sr. Pipeline Compliance Engineer
Preparer Email H****@e****.com
Preparer Telephone 713-381-4277
Prepared Date 2021-01-14 00:00:00
Authorizer Name H*** D***
Authorizer Telephone 713-381-4277
Authorizer Title Sr. Pipeline Compliance Engineer
Authorizer Email H****@e****.com
Narrative On 11/17/2020 at 08:08 ct, houston control center (hcc) was contacted by an enterprise technician reporting that a third party observed vapor at linn station. Hcc shut down the pump units while the technician was in-route to the station. Once on site at 08:23 ct the technician discovered frost on the ground above lid 428 pipeline inside the station. At 08:34 ct houston control center reduced the pressure and isolated the pipeline. After discussions with operations and onsite technician, at 09:40 ct it was determined that the estimated repair cost would likely exceed the $50,000 reporting threshold for nrc. An estimated 25 gallons of propane leaked from the pipeline with 50 barrels flared from the line prior to the nitrogen purge allowing for excavation and repair. Once excavated a stopple split tee fitting was found to be the source of the leak and was cut out and replaced with 40 feet of pipe. The pipeline was returned to service on 11/22/2020 at 17:00 ct. Initial call to nrc was made on 11/17/2020 at 10:17 ct (nrc#1292452). The call was made based on repair cost estimates exceeding $50,000. 48hr update call to nrc was made on 11/19/2020 (nrc#1292636). The update provided an estimated product release of 25 gallons.

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