HL incident on 2020-10-14 — TX

Operator
Sunoco Pipeline L.p.
Cause
Corrosion Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$100
Incident datetime
2020-10-14 10:30
Report number
Location
TX
Narrative
A company maintenance technician was in the process of conducting a valve inspection at mlv 83 near the intersection of lake ave and goodman xing roads in scotch plains twp., nj. Mlv 83 is a manual valve that is normally open. Upon operating the valve as part of the inspection, the maintenance technician observed a small leak coming from the grease fitting extension nipple. Further assessment determined there was diesel product in the valve vault. Notifications were made to supervisor and responders. The free product/water mixture was collected from the vault via vacuum truck. A total of 13.7 gallons was recovered. It was determined that the nipple had a pinhole corrosion leak that was not apparent until actuating the valve thereby increasing pressure on the nipple. The grease fitting extension nipple was replaced.
Detailed record list
Report Received Date
2020-11-11 00:00:00
Iyear
2020
Report Number
20200306
Supplemental Number
34522
Report Type
Original Final
Operator Id
Name
Sunoco Pipeline L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2020-10-14 10:30:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
0.3
Recovered Bbls
0.3
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2020-10-14 10:30:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Pipeline Was Not Operating / Not Scheduled To Operate.
On Site Datetime
2020-10-14 10:30:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
11010 Twin Oaks To Newark 14inch Pipeline
Segment Name
Valve Section 0083a
Onshore State Abbreviation
Nj
Onshore Postal Code
07076
Onshore City Name
Scotch Plains Twp.
Onshore County Name
Union
Designated Location
Milepost/valve Station
Designated Name
Mlv-83
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
In Underground Enclosed Space (E.g. Vault)
Depth Of Cover
96
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Other
Item Involved Details
Pipe Nipple
Installation Year
1956
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
17
Est Cost Prop Damage
100
Est Cost Emergency
2000
Est Cost Environmental
0
Est Cost Other
0
Prpty
2117
Accident Psig
235
Mop Psig
1200
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
1
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
Localized Pitting
Atmosphere Corrosion Ind
Yes
Field Exam Basis Ind
Yes
Underground Location
No
Externally Coated
Yes
Prior Damage
Yes
Preparer Name
T*** N*******
Preparer Title
Director - Regulatory Compliance
Preparer Email
T************@e*************.com
Preparer Telephone
7139897126
Prepared Date
2020-11-11 00:00:00
Authorizer Name
T*** N*******
Authorizer Telephone
7139897126
Authorizer Title
Director - Regulatory Compliance
Authorizer Email
T************@e*************.com
Narrative
A company maintenance technician was in the process of conducting a valve inspection at mlv 83 near the intersection of lake ave and goodman xing roads in scotch plains twp., nj. Mlv 83 is a manual valve that is normally open. Upon operating the valve as part of the inspection, the maintenance technician observed a small leak coming from the grease fitting extension nipple. Further assessment determined there was diesel product in the valve vault. Notifications were made to supervisor and responders. The free product/water mixture was collected from the vault via vacuum truck. A total of 13.7 gallons was recovered. It was determined that the nipple had a pinhole corrosion leak that was not apparent until actuating the valve thereby increasing pressure on the nipple. The grease fitting extension nipple was replaced.
Report Received Date 2020-11-11 00:00:00
Iyear 2020
Report Number 20200306
Supplemental Number 34522
Report Type Original Final
Operator Id 18718 PHMSA Enforcement
Name Sunoco Pipeline L.p.
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2020-10-14 10:30:00
Location Latitude 40.616076 Google Maps OpenStreetMap
Location Longitude -74.340111 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 0.3
Recovered Bbls 0.3
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2020-10-14 10:30:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Pipeline Was Not Operating / Not Scheduled To Operate.
On Site Datetime 2020-10-14 10:30:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name 11010 Twin Oaks To Newark 14inch Pipeline
Segment Name Valve Section 0083a
Onshore State Abbreviation Nj
Onshore Postal Code 07076
Onshore City Name Scotch Plains Twp.
Onshore County Name Union
Designated Location Milepost/valve Station
Designated Name Mlv-83
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype In Underground Enclosed Space (E.g. Vault)
Depth Of Cover 96
Crossing No
Pipe Facility Type Interstate
Item Involved Other
Item Involved Details Pipe Nipple
Installation Year 1956
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 17
Est Cost Prop Damage 100
Est Cost Emergency 2000
Est Cost Environmental 0
Est Cost Other 0
Prpty 2117
Accident Psig 235
Mop Psig 1200
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 1
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results Localized Pitting
Atmosphere Corrosion Ind Yes
Field Exam Basis Ind Yes
Underground Location No
Externally Coated Yes
Prior Damage Yes
Preparer Name T*** N*******
Preparer Title Director - Regulatory Compliance
Preparer Email T************@e*************.com
Preparer Telephone 7139897126
Prepared Date 2020-11-11 00:00:00
Authorizer Name T*** N*******
Authorizer Telephone 7139897126
Authorizer Title Director - Regulatory Compliance
Authorizer Email T************@e*************.com
Narrative A company maintenance technician was in the process of conducting a valve inspection at mlv 83 near the intersection of lake ave and goodman xing roads in scotch plains twp., nj. Mlv 83 is a manual valve that is normally open. Upon operating the valve as part of the inspection, the maintenance technician observed a small leak coming from the grease fitting extension nipple. Further assessment determined there was diesel product in the valve vault. Notifications were made to supervisor and responders. The free product/water mixture was collected from the vault via vacuum truck. A total of 13.7 gallons was recovered. It was determined that the nipple had a pinhole corrosion leak that was not apparent until actuating the valve thereby increasing pressure on the nipple. The grease fitting extension nipple was replaced.

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