HL incident on 2020-11-03 — TX

Operator
Oryx Delaware Oil Transport Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$68,000
Incident datetime
2020-11-03 10:20
Report number
Location
TX
Narrative
On november 3rd, 2020 at approximately 0930 a 3rd party producer notified oryx midstream services of a leak on the pipeline system. Operators were immediately dispatched to the location of the leak and arrived at 1020. The leak was found on a mainline gate valve. This gate valve is part of the pig launching assembly and is the first mainline block valve on the pipeline. The cause of the leak was the seal between the body and bonnet of the mainline block valve. The pipeline was shut down at 1530 on november 3rd, 2020 to begin de-inventorying the pipeline to start repair. On november 4th, 2020 at 1000 the pipeline was de-inventoried and valve replacement was started. It was decided to replace the valve rather than repair due to repair parts local availability and timely contractor availability in the area. Repair and the purging of the pipeline were completed at 1726 and pipeline was returned to normal operating conditions.
Detailed record list
Report Received Date
2020-11-11 00:00:00
Iyear
2020
Report Number
20200305
Supplemental Number
34524
Report Type
Supplemental Final
Operator Id
Name
Oryx Delaware Oil Transport Llc
Operator Street Address
333 Clay St. Suite 1900
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2020-11-03 10:20:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
1
Recovered Bbls
1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Other
Accident Details
3rd Party - Producer
Incident Identified Datetime
2020-11-03 10:20:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2020-11-03 15:30:00
Restart Datetime
2020-11-04 17:26:00
On Site Datetime
2020-11-03 10:20:00
Nrc Rpt Datetime
2020-11-03 11:28:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Northwest A 12" Launcher
Segment Name
Northwest A 12"
Onshore State Abbreviation
Tx
Onshore Postal Code
79772
Onshore City Name
Not Within A Municipality
Onshore County Name
Reeves
Designated Location
Milepost/valve Station
Designated Name
Launcher
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Mainline
Valve Mainline Type
Gate
Valve Manufacturer
Williams Valve Corp
Installation Year
2016
Manufactured Year
2016
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
No
Est Cost Oper Paid
0
Est Cost Gas Released
40
Est Cost Prop Damage
68000
Est Cost Emergency
0
Est Cost Environmental
10000
Est Cost Other
0
Prpty
78040
Accident Psig
150
Mop Psig
740
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
10000
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
This leak was not detectable by control room.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Seal (Not Pump Seal) Or Packing
Additional Valve Ind
Yes
Preparer Name
G****** H****
Preparer Title
Sr. Regulatory Compliance
Preparer Email
G******@o************.com
Preparer Telephone
4322542238
Prepared Date
2020-11-12 00:00:00
Authorizer Name
M***** M*****
Authorizer Telephone
4322537774
Authorizer Title
Coo
Authorizer Email
M*****@o************.com
Narrative
On november 3rd, 2020 at approximately 0930 a 3rd party producer notified oryx midstream services of a leak on the pipeline system. Operators were immediately dispatched to the location of the leak and arrived at 1020. The leak was found on a mainline gate valve. This gate valve is part of the pig launching assembly and is the first mainline block valve on the pipeline. The cause of the leak was the seal between the body and bonnet of the mainline block valve. The pipeline was shut down at 1530 on november 3rd, 2020 to begin de-inventorying the pipeline to start repair. On november 4th, 2020 at 1000 the pipeline was de-inventoried and valve replacement was started. It was decided to replace the valve rather than repair due to repair parts local availability and timely contractor availability in the area. Repair and the purging of the pipeline were completed at 1726 and pipeline was returned to normal operating conditions.
Report Received Date 2020-11-11 00:00:00
Iyear 2020
Report Number 20200305
Supplemental Number 34524
Report Type Supplemental Final
Operator Id 39654 PHMSA Enforcement
Name Oryx Delaware Oil Transport Llc
Operator Street Address 333 Clay St. Suite 1900
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2020-11-03 10:20:00
Location Latitude 31.367009 Google Maps OpenStreetMap
Location Longitude -103.442867 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 1
Recovered Bbls 1
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Other
Accident Details 3rd Party - Producer
Incident Identified Datetime 2020-11-03 10:20:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2020-11-03 15:30:00
Restart Datetime 2020-11-04 17:26:00
On Site Datetime 2020-11-03 10:20:00
Nrc Rpt Datetime 2020-11-03 11:28:00
Nrc Rpt Num 1291297 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Northwest A 12" Launcher
Segment Name Northwest A 12"
Onshore State Abbreviation Tx
Onshore Postal Code 79772
Onshore City Name Not Within A Municipality
Onshore County Name Reeves
Designated Location Milepost/valve Station
Designated Name Launcher
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Mainline
Valve Mainline Type Gate
Valve Manufacturer Williams Valve Corp
Installation Year 2016
Manufactured Year 2016
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Usa Ecological Ind Yes
Usa Ecological Yes No No
Est Cost Oper Paid 0
Est Cost Gas Released 40
Est Cost Prop Damage 68000
Est Cost Emergency 0
Est Cost Environmental 10000
Est Cost Other 0
Prpty 78040
Accident Psig 150
Mop Psig 740
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 10000
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details This leak was not detectable by control room.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Seal (Not Pump Seal) Or Packing
Additional Valve Ind Yes
Preparer Name G****** H****
Preparer Title Sr. Regulatory Compliance
Preparer Email G******@o************.com
Preparer Telephone 4322542238
Prepared Date 2020-11-12 00:00:00
Authorizer Name M***** M*****
Authorizer Telephone 4322537774
Authorizer Title Coo
Authorizer Email M*****@o************.com
Narrative On november 3rd, 2020 at approximately 0930 a 3rd party producer notified oryx midstream services of a leak on the pipeline system. Operators were immediately dispatched to the location of the leak and arrived at 1020. The leak was found on a mainline gate valve. This gate valve is part of the pig launching assembly and is the first mainline block valve on the pipeline. The cause of the leak was the seal between the body and bonnet of the mainline block valve. The pipeline was shut down at 1530 on november 3rd, 2020 to begin de-inventorying the pipeline to start repair. On november 4th, 2020 at 1000 the pipeline was de-inventoried and valve replacement was started. It was decided to replace the valve rather than repair due to repair parts local availability and timely contractor availability in the area. Repair and the purging of the pipeline were completed at 1726 and pipeline was returned to normal operating conditions.

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