HL incident on 2020-10-14 — TX

Operator
Enterprise Products Operating Llc
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$200
Incident datetime
2020-10-14 07:44
Report number
Location
TX
Narrative
At 07:11 am, houston control center (hcc) received a hazardous gas alarm at the sulphur pump station. Hcc contacted field operations who were in the area performing other activities. At 07:44 am, enterprise field personnel arrived on site at the sulphur ngl pump station and found a leak near the sulphur ngl pump. Field personnel contacted hcc and the station was shut down at 07:46 am. Hcc then closed the valves upstream and downstream of the station. State police closed highway 1133 as a pre-caution due to potential product migration. The highway was reopened when the area was made safe at 08:50 am. At approximately 09:15 am, upon determination the event was considered significant due to the road closure, enterprise notified the nrc. Visual examination determined there was vibration induced by product flowing back through the check valve. The vibration cycling was resolved by flushing and greasing the valve, allowing it to seal properly; additionally, the failed tubing was replaced. The nrc 48 hour notification took place on october 15, 2020 at 20:06 central time, #1289911
Detailed record list
Report Received Date
2020-11-10 00:00:00
Iyear
2020
Report Number
20200303
Supplemental Number
34515
Report Type
Original Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2020-10-14 07:11:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Isobutane
Unintentional Release Bbls
60
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2020-10-14 07:44:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2020-10-14 07:46:00
Restart Datetime
2020-10-14 16:27:00
On Site Datetime
2020-10-14 07:44:00
Nrc Rpt Datetime
2020-10-14 09:41:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Loutex 12" Ngl
Segment Name
24740
Onshore State Abbreviation
La
Onshore Postal Code
70665
Onshore City Name
Sulphur
Onshore County Name
Calcasieu
Designated Location
Milepost/valve Station
Designated Name
Mp 102.2
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tubing
Installation Year
2000
Material Involved
Material Other Than Carbon Steel
Material Details
Stainless Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
1600
Est Cost Prop Damage
200
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
1800
Accident Psig
1220
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controller action did not contribute to the accident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Threaded Connection/coupling Failure
Eq Failure Type
Threaded Connection/coupling Failure
Other Stripped Ind
Threaded Fitting
Additional Vibration Ind
Yes
Preparer Name
N***** L* G*** J**
Preparer Title
Pipeline Compliance Specialist
Preparer Email
N****@e****.com
Preparer Telephone
985 493 4629
Prepared Date
2020-11-10 00:00:00
Authorizer Name
N*** T*****
Authorizer Telephone
713 381 2493
Authorizer Title
Compliance Manager
Authorizer Email
N*******@e****.com
Narrative
At 07:11 am, houston control center (hcc) received a hazardous gas alarm at the sulphur pump station. Hcc contacted field operations who were in the area performing other activities. At 07:44 am, enterprise field personnel arrived on site at the sulphur ngl pump station and found a leak near the sulphur ngl pump. Field personnel contacted hcc and the station was shut down at 07:46 am. Hcc then closed the valves upstream and downstream of the station. State police closed highway 1133 as a pre-caution due to potential product migration. The highway was reopened when the area was made safe at 08:50 am. At approximately 09:15 am, upon determination the event was considered significant due to the road closure, enterprise notified the nrc. Visual examination determined there was vibration induced by product flowing back through the check valve. The vibration cycling was resolved by flushing and greasing the valve, allowing it to seal properly; additionally, the failed tubing was replaced. The nrc 48 hour notification took place on october 15, 2020 at 20:06 central time, #1289911
Report Received Date 2020-11-10 00:00:00
Iyear 2020
Report Number 20200303
Supplemental Number 34515
Report Type Original Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2020-10-14 07:11:00
Location Latitude 30.164743 Google Maps OpenStreetMap
Location Longitude -93.351383 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Isobutane
Unintentional Release Bbls 60
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2020-10-14 07:44:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2020-10-14 07:46:00
Restart Datetime 2020-10-14 16:27:00
On Site Datetime 2020-10-14 07:44:00
Nrc Rpt Datetime 2020-10-14 09:41:00
Nrc Rpt Num 1289719 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Loutex 12" Ngl
Segment Name 24740
Onshore State Abbreviation La
Onshore Postal Code 70665
Onshore City Name Sulphur
Onshore County Name Calcasieu
Designated Location Milepost/valve Station
Designated Name Mp 102.2
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Tubing
Installation Year 2000
Material Involved Material Other Than Carbon Steel
Material Details Stainless Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 1600
Est Cost Prop Damage 200
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 1800
Accident Psig 1220
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Controller action did not contribute to the accident.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Threaded Connection/coupling Failure
Eq Failure Type Threaded Connection/coupling Failure
Other Stripped Ind Threaded Fitting
Additional Vibration Ind Yes
Preparer Name N***** L* G*** J**
Preparer Title Pipeline Compliance Specialist
Preparer Email N****@e****.com
Preparer Telephone 985 493 4629
Prepared Date 2020-11-10 00:00:00
Authorizer Name N*** T*****
Authorizer Telephone 713 381 2493
Authorizer Title Compliance Manager
Authorizer Email N*******@e****.com
Narrative At 07:11 am, houston control center (hcc) received a hazardous gas alarm at the sulphur pump station. Hcc contacted field operations who were in the area performing other activities. At 07:44 am, enterprise field personnel arrived on site at the sulphur ngl pump station and found a leak near the sulphur ngl pump. Field personnel contacted hcc and the station was shut down at 07:46 am. Hcc then closed the valves upstream and downstream of the station. State police closed highway 1133 as a pre-caution due to potential product migration. The highway was reopened when the area was made safe at 08:50 am. At approximately 09:15 am, upon determination the event was considered significant due to the road closure, enterprise notified the nrc. Visual examination determined there was vibration induced by product flowing back through the check valve. The vibration cycling was resolved by flushing and greasing the valve, allowing it to seal properly; additionally, the failed tubing was replaced. The nrc 48 hour notification took place on october 15, 2020 at 20:06 central time, #1289911

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