HL incident on 2020-10-05 — TX

Operator
Phillips 66 Pipeline Llc
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$23,000
Incident datetime
2020-10-05 08:54
Report number
Location
TX
Narrative
Phillips 66 measurement technician was performing pycnometer densitometer verification on the ethane meter skid for sr-92 at the clemens meter station, a compression fitting connection suddenly failed and separated on the 1-inch stainless steel tubing run for the pycnometer. Pipeline was shutdown, system isolated and repaired. The investigation team determined that the end of the tubing in the failed connection was not sufficiently crimped to prevent the tubing end from pulling out of the ferrule/nut connection. All other area tubing connections were verified for proper installation. Supplemental update 11/5/20 as per PHMSA aid: the tubing installation was part of a new construction project, thus oq did not apply. The connection failure occurred due to the installer not following the correct tubing crimping verification procedure. Phillips 66 plans to implement a secondary pre-startup verification process on larger diameter tubing for new construction installations.
Detailed record list
Report Received Date
2020-11-03 00:00:00
Iyear
2020
Report Number
20200295
Supplemental Number
34486
Report Type
Supplemental Final
Operator Id
Name
Phillips 66 Pipeline Llc
Operator Street Address
2331 Citywest Blvd
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77042
Local Datetime
2020-10-05 08:54:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Ethane
Unintentional Release Bbls
371
Intentional Release Bbls
100
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2020-10-05 08:54:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2020-10-05 09:13:00
Restart Datetime
2020-10-06 00:30:00
On Site Datetime
2020-10-05 10:40:00
Nrc Rpt Datetime
2020-10-05 09:52:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Clemens Terminal
Segment Name
Sr-92 Meter Skid
Onshore State Abbreviation
Tx
Onshore Postal Code
77422
Onshore City Name
Not Within A Municipality
Onshore County Name
Brazoria
Designated Location
Milepost/valve Station
Designated Name
Station Pipe
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tubing
Installation Year
2020
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
5000
Est Cost Prop Damage
23000
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Est Cost Other Details
Cost Of Product Loss And Re-Installation Of Tubing And Valve Replacement.
Prpty
28000
Accident Psig
1550
Mop Psig
2160
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Incident occurred during maintenance activity and the pipeline was shutdown upon request.
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
1
Num Employees Failed
0
Cause
Equipment Failure
Cause Details
Defective Or Loose Tubing Or Fitting
Eq Failure Type
Defective Or Loose Tubing Or Fitting
Additional Installation Ind
Yes
Preparer Name
J*** S*****
Preparer Title
Dot Coordinator
Preparer Email
J************@p**.com
Preparer Telephone
832-765-1858
Prepared Date
2020-11-05 00:00:00
Authorizer Name
T*** F****
Authorizer Telephone
8327651632
Authorizer Title
Director Dot Operations Compliance
Authorizer Email
T***********@p**.com
Narrative
Phillips 66 measurement technician was performing pycnometer densitometer verification on the ethane meter skid for sr-92 at the clemens meter station, a compression fitting connection suddenly failed and separated on the 1-inch stainless steel tubing run for the pycnometer. Pipeline was shutdown, system isolated and repaired. The investigation team determined that the end of the tubing in the failed connection was not sufficiently crimped to prevent the tubing end from pulling out of the ferrule/nut connection. All other area tubing connections were verified for proper installation. Supplemental update 11/5/20 as per PHMSA aid: the tubing installation was part of a new construction project, thus oq did not apply. The connection failure occurred due to the installer not following the correct tubing crimping verification procedure. Phillips 66 plans to implement a secondary pre-startup verification process on larger diameter tubing for new construction installations.
Report Received Date 2020-11-03 00:00:00
Iyear 2020
Report Number 20200295
Supplemental Number 34486
Report Type Supplemental Final
Operator Id 31684 PHMSA Enforcement
Name Phillips 66 Pipeline Llc
Operator Street Address 2331 Citywest Blvd
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77042
Local Datetime 2020-10-05 08:54:00
Location Latitude 28.993423 Google Maps OpenStreetMap
Location Longitude -95.56372 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Ethane
Unintentional Release Bbls 371
Intentional Release Bbls 100
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2020-10-05 08:54:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2020-10-05 09:13:00
Restart Datetime 2020-10-06 00:30:00
On Site Datetime 2020-10-05 10:40:00
Nrc Rpt Datetime 2020-10-05 09:52:00
Nrc Rpt Num 1289010 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Clemens Terminal
Segment Name Sr-92 Meter Skid
Onshore State Abbreviation Tx
Onshore Postal Code 77422
Onshore City Name Not Within A Municipality
Onshore County Name Brazoria
Designated Location Milepost/valve Station
Designated Name Station Pipe
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Tubing
Installation Year 2020
Material Involved Carbon Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 5000
Est Cost Prop Damage 23000
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Est Cost Other Details Cost Of Product Loss And Re-Installation Of Tubing And Valve Replacement.
Prpty 28000
Accident Psig 1550
Mop Psig 2160
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Incident occurred during maintenance activity and the pipeline was shutdown upon request.
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 1
Num Employees Failed 0
Cause Equipment Failure
Cause Details Defective Or Loose Tubing Or Fitting
Eq Failure Type Defective Or Loose Tubing Or Fitting
Additional Installation Ind Yes
Preparer Name J*** S*****
Preparer Title Dot Coordinator
Preparer Email J************@p**.com
Preparer Telephone 832-765-1858
Prepared Date 2020-11-05 00:00:00
Authorizer Name T*** F****
Authorizer Telephone 8327651632
Authorizer Title Director Dot Operations Compliance
Authorizer Email T***********@p**.com
Narrative Phillips 66 measurement technician was performing pycnometer densitometer verification on the ethane meter skid for sr-92 at the clemens meter station, a compression fitting connection suddenly failed and separated on the 1-inch stainless steel tubing run for the pycnometer. Pipeline was shutdown, system isolated and repaired. The investigation team determined that the end of the tubing in the failed connection was not sufficiently crimped to prevent the tubing end from pulling out of the ferrule/nut connection. All other area tubing connections were verified for proper installation. Supplemental update 11/5/20 as per PHMSA aid: the tubing installation was part of a new construction project, thus oq did not apply. The connection failure occurred due to the installer not following the correct tubing crimping verification procedure. Phillips 66 plans to implement a secondary pre-startup verification process on larger diameter tubing for new construction installations.

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