HL incident on 2020-09-16 — TX

Operator
Kinder Morgan Co2 Co. Lp
Cause
Equipment Failure
Commodity
Co2 (Carbon Dioxide)
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$550
Incident datetime
2020-09-16 18:16
Report number
Location
TX
Narrative
On 9/16/20, a third party operator reported a CO2 leak on a 2" insulating flange gasket on the burnett ranch meter site. The control center was contacted, and the meter run was isolated. Local personnel were dispatched to the site. The meter run was blown down, and the insulating flange gasket was replaced. The insulating flange gasket was sent to a lab for a material assessment. The gasket failure can be attributed to improper gasket installed by a contractor during the initial construction of this pipeline.
Detailed record list
Report Received Date
2020-10-15 00:00:00
Iyear
2020
Report Number
20200281
Supplemental Number
37523
Report Type
Supplemental Final
Operator Id
Name
Kinder Morgan Co2 Co. Lp
Operator Street Address
1001 Louisiana St, Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2020-09-16 18:16:00
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
-100.0642161
Commodity Released Type
Co2 (Carbon Dioxide)
Unintentional Release Bbls
0.2
Intentional Release Bbls
2.8
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Other
Accident Details
Third Party Operator
Incident Identified Datetime
2020-09-16 18:16:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Communication State Fed Ind
No
On Site Datetime
2020-09-16 21:10:00
Confirmed Discovery Datetime
2020-09-16 18:16:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Burnett Ranch Station
Segment Name
Burnett Ranch
Onshore State Abbreviation
Tx
Onshore Postal Code
79529
Onshore City Name
Knox City
Onshore County Name
King
Designated Location
Milepost
Designated Name
Mp 97
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Other
Item Involved Details
Insulating Flange Gasket
Installation Year
2014
Manufactured Year
Unknown
Material Involved
Material Other Than Carbon Steel
Material Details
G10 Glass Reinforced Epoxy, Teflon Seal
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
6
Est Cost Prop Damage
550
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
556
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
1741
Mop Psig
2220
Mop Cfr Section
Component Design Pressure �195.406(A)(2)
Maop Established Date
2014-02-01 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Gasket
Additional Installation Ind
Yes
Additional Mismatch Ind
Yes
Preparer Name
J*** J****
Preparer Title
Supervisor - Regulatory
Preparer Email
J*********@k***********.com
Preparer Telephone
713-369-8078
Prepared Date
2023-01-03 00:00:00
Authorizer Name
M***** L*******
Authorizer Telephone
713-420-4649
Authorizer Title
Director-Operations And Engineering
Authorizer Email
M**************@k***********.com
Narrative
On 9/16/20, a third party operator reported a CO2 leak on a 2" insulating flange gasket on the burnett ranch meter site. The control center was contacted, and the meter run was isolated. Local personnel were dispatched to the site. The meter run was blown down, and the insulating flange gasket was replaced. The insulating flange gasket was sent to a lab for a material assessment. The gasket failure can be attributed to improper gasket installed by a contractor during the initial construction of this pipeline.
Report Received Date 2020-10-15 00:00:00
Iyear 2020
Report Number 20200281
Supplemental Number 37523
Report Type Supplemental Final
Operator Id 31555 PHMSA Enforcement
Name Kinder Morgan Co2 Co. Lp
Operator Street Address 1001 Louisiana St, Suite 1000
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2020-09-16 18:16:00
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 33.4720558 Google Maps OpenStreetMap
Location Longitude -100.0642161 Google Maps OpenStreetMap
Commodity Released Type Co2 (Carbon Dioxide)
Unintentional Release Bbls 0.2
Intentional Release Bbls 2.8
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Other
Accident Details Third Party Operator
Incident Identified Datetime 2020-09-16 18:16:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Communication State Fed Ind No
On Site Datetime 2020-09-16 21:10:00
Confirmed Discovery Datetime 2020-09-16 18:16:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Num Pub Evacuated 0
Pipe Fac Name Burnett Ranch Station
Segment Name Burnett Ranch
Onshore State Abbreviation Tx
Onshore Postal Code 79529
Onshore City Name Knox City
Onshore County Name King
Designated Location Milepost
Designated Name Mp 97
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Other
Item Involved Details Insulating Flange Gasket
Installation Year 2014
Manufactured Year Unknown
Material Involved Material Other Than Carbon Steel
Material Details G10 Glass Reinforced Epoxy, Teflon Seal
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 6
Est Cost Prop Damage 550
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 556
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 1741
Mop Psig 2220
Mop Cfr Section Component Design Pressure �195.406(A)(2) View CFR 49 §192
Maop Established Date 2014-02-01 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Gasket
Additional Installation Ind Yes
Additional Mismatch Ind Yes
Preparer Name J*** J****
Preparer Title Supervisor - Regulatory
Preparer Email J*********@k***********.com
Preparer Telephone 713-369-8078
Prepared Date 2023-01-03 00:00:00
Authorizer Name M***** L*******
Authorizer Telephone 713-420-4649
Authorizer Title Director-Operations And Engineering
Authorizer Email M**************@k***********.com
Narrative On 9/16/20, a third party operator reported a CO2 leak on a 2" insulating flange gasket on the burnett ranch meter site. The control center was contacted, and the meter run was isolated. Local personnel were dispatched to the site. The meter run was blown down, and the insulating flange gasket was replaced. The insulating flange gasket was sent to a lab for a material assessment. The gasket failure can be attributed to improper gasket installed by a contractor during the initial construction of this pipeline.

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