HL incident on 2020-09-16 — TX

Operator
Targa Downstream Llc
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2020-09-16 22:40
Report number
Location
TX
Narrative
At 20:00 hours (09/16/2020), controllers received alarm indicating esd870001 at pump station 12 had closed (un-commanded). Controllers dispatched technicians to site to investigate. Upon arrival, technicians discovered issue with transmitter. Technicians diverted flow around the esd valve (through pig launcher) to maintain safe operating pressure on system. Once transmitter was repaired, technicians attempted to equalize the differential pressure across esd870001 through the pig trap to resume product flow. Small leak on 1/2" stainless steel tubing was found on the trap kicker valve. Technicians were unable to close valve before tubing fitting failed, creating a vapor cloud that forced evacuation of the site. Valves upstream and downstream of the pump station were closed to limit product release. As a precaution, emergency responders were called to site and briefly closed hwy 150 to traffic when vapor cloud shifted direction toward the highway (09/17/2020: 02:45 - 03:00). Once product release ended, technicians were able to return product flow to normal and repair tubing on mov at the launcher kicker valve. The tubing failure appeared to be caused by an over-tightening of the fitting.
Detailed record list
Report Received Date
2020-10-08 00:00:00
Iyear
2020
Report Number
20200274
Supplemental Number
34392
Report Type
Supplemental Final
Operator Id
Name
Targa Downstream Llc
Operator Street Address
811 Louisiana St. Suite 2100
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2020-09-16 22:40:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Raw Product / Y-Grade
Unintentional Release Bbls
214
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2020-09-16 22:40:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2020-09-16 22:40:00
Restart Datetime
2020-09-17 08:45:00
On Site Datetime
2020-09-16 21:30:00
Nrc Rpt Datetime
2020-09-17 03:19:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Grand Prix Pipeline South (Gpx-S)
Segment Name
Pump Station 12
Onshore State Abbreviation
Tx
Onshore Postal Code
77371
Onshore City Name
Not Within A Municipality
Onshore County Name
San Jacinto
Designated Location
Milepost/valve Station
Designated Name
Valve Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tubing
Installation Year
2019
Material Involved
Material Other Than Carbon Steel
Material Details
Stainless Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
4044
Est Cost Prop Damage
0
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
4044
Accident Psig
744
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
No
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Technicians were dispatched to site in response to a faulty transmitter. Release occurred after technicians were on site.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Other Control Relief Ind
Yes
Other Control Relief Details
Tubing Fitting Failure
Additional Installation Ind
Yes
Preparer Name
S** G*****
Preparer Title
Compliance Specialist
Preparer Email
S******@t*************.com
Preparer Telephone
337-794-8247
Preparer Fax
337-583-4630
Prepared Date
2020-10-16 00:00:00
Authorizer Name
S** G*****
Authorizer Telephone
337-794-8247
Authorizer Title
Compliance Specialist
Authorizer Email
S******@t*************.com
Narrative
At 20:00 hours (09/16/2020), controllers received alarm indicating esd870001 at pump station 12 had closed (un-commanded). Controllers dispatched technicians to site to investigate. Upon arrival, technicians discovered issue with transmitter. Technicians diverted flow around the esd valve (through pig launcher) to maintain safe operating pressure on system. Once transmitter was repaired, technicians attempted to equalize the differential pressure across esd870001 through the pig trap to resume product flow. Small leak on 1/2" stainless steel tubing was found on the trap kicker valve. Technicians were unable to close valve before tubing fitting failed, creating a vapor cloud that forced evacuation of the site. Valves upstream and downstream of the pump station were closed to limit product release. As a precaution, emergency responders were called to site and briefly closed hwy 150 to traffic when vapor cloud shifted direction toward the highway (09/17/2020: 02:45 - 03:00). Once product release ended, technicians were able to return product flow to normal and repair tubing on mov at the launcher kicker valve. The tubing failure appeared to be caused by an over-tightening of the fitting.
Report Received Date 2020-10-08 00:00:00
Iyear 2020
Report Number 20200274
Supplemental Number 34392
Report Type Supplemental Final
Operator Id 39823 PHMSA Enforcement
Name Targa Downstream Llc
Operator Street Address 811 Louisiana St. Suite 2100
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2020-09-16 22:40:00
Location Latitude 30.52542 Google Maps OpenStreetMap
Location Longitude -95.064933 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Raw Product / Y-Grade
Unintentional Release Bbls 214
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2020-09-16 22:40:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2020-09-16 22:40:00
Restart Datetime 2020-09-17 08:45:00
On Site Datetime 2020-09-16 21:30:00
Nrc Rpt Datetime 2020-09-17 03:19:00
Nrc Rpt Num 1287564 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Grand Prix Pipeline South (Gpx-S)
Segment Name Pump Station 12
Onshore State Abbreviation Tx
Onshore Postal Code 77371
Onshore City Name Not Within A Municipality
Onshore County Name San Jacinto
Designated Location Milepost/valve Station
Designated Name Valve Station
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Tubing
Installation Year 2019
Material Involved Material Other Than Carbon Steel
Material Details Stainless Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 4044
Est Cost Prop Damage 0
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 4044
Accident Psig 744
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind No
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Technicians were dispatched to site in response to a faulty transmitter. Release occurred after technicians were on site.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Other Control Relief Ind Yes
Other Control Relief Details Tubing Fitting Failure
Additional Installation Ind Yes
Preparer Name S** G*****
Preparer Title Compliance Specialist
Preparer Email S******@t*************.com
Preparer Telephone 337-794-8247
Preparer Fax 337-583-4630
Prepared Date 2020-10-16 00:00:00
Authorizer Name S** G*****
Authorizer Telephone 337-794-8247
Authorizer Title Compliance Specialist
Authorizer Email S******@t*************.com
Narrative At 20:00 hours (09/16/2020), controllers received alarm indicating esd870001 at pump station 12 had closed (un-commanded). Controllers dispatched technicians to site to investigate. Upon arrival, technicians discovered issue with transmitter. Technicians diverted flow around the esd valve (through pig launcher) to maintain safe operating pressure on system. Once transmitter was repaired, technicians attempted to equalize the differential pressure across esd870001 through the pig trap to resume product flow. Small leak on 1/2" stainless steel tubing was found on the trap kicker valve. Technicians were unable to close valve before tubing fitting failed, creating a vapor cloud that forced evacuation of the site. Valves upstream and downstream of the pump station were closed to limit product release. As a precaution, emergency responders were called to site and briefly closed hwy 150 to traffic when vapor cloud shifted direction toward the highway (09/17/2020: 02:45 - 03:00). Once product release ended, technicians were able to return product flow to normal and repair tubing on mov at the launcher kicker valve. The tubing failure appeared to be caused by an over-tightening of the fitting.

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