HL incident on 2020-09-03 — TX

Operator
Kinder Morgan Liquid Terminals, Llc
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$50
Incident datetime
2020-09-03 14:30
Report number
Location
TX
Narrative
On september 3, 2020 at 14:30, 2.1 barrels of product was discovered near the e-valve of tank 150-65. The product was cleaned up immediately. The source of the leak was identified as a buried flange near the e-valve. The bolts on the flange were torqued and the leak stopped. The incident investigation showed the likely cause of the loose bolts was due to thermal pressure. The line has pressure relief valve. Tank 150-65 was out of service for API 653 and returned to service in march 2020. The thermal for the tank-lines were routed to tank 150-66. The thermal line that leaked was not rerouted to 150-65 until 18 september 2020 (13 days after incident). The gasket was replaced out of an abundance of caution. Plan for prevention: the flange will remain exposed and not reburied. On a go forward basis, the thermal relief system will be reviewed as the tanks is returned to service using the manway removal form.
Detailed record list
Report Received Date
2020-10-02 00:00:00
Iyear
2020
Report Number
20200270
Supplemental Number
34653
Report Type
Supplemental Final
Operator Id
Name
Kinder Morgan Liquid Terminals, Llc
Operator Street Address
1001 Louisiana St, Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2020-09-03 14:30:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Other
Commodity Details
Condensate
Unintentional Release Bbls
2.1
Recovered Bbls
2.1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2020-09-03 14:30:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
The Pipeline Was Not Active At The Time Of Discovery
On Site Datetime
2020-09-03 14:30:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Kinder Morgan Pasadena Terminal
Segment Name
Tank Line Of Tank 150-65
Onshore State Abbreviation
Tx
Onshore Postal Code
77506
Onshore City Name
Pasadena
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
12
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Flange Assembly
Installation Year
2007
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Commercially Nav Ind
Yes
Commercially Nav Yes No
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
70
Est Cost Prop Damage
50
Est Cost Emergency
0
Est Cost Environmental
24000
Est Cost Other
0
Prpty
24120
Accident Psig
23
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controllers actions were unrelated to the leak.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Gasket
Additional Thermal Ind
Yes
Preparer Name
D******* S*******
Preparer Title
Manager Compliance Code And Standards
Preparer Email
D****************@k***********.com
Preparer Telephone
713-420-6496
Prepared Date
2020-12-23 00:00:00
Authorizer Name
D******* S*******
Authorizer Telephone
713-420-6496
Authorizer Title
Manager - Compliance Codes And Standards
Authorizer Email
D****************@k***********.com
Narrative
On september 3, 2020 at 14:30, 2.1 barrels of product was discovered near the e-valve of tank 150-65. The product was cleaned up immediately. The source of the leak was identified as a buried flange near the e-valve. The bolts on the flange were torqued and the leak stopped. The incident investigation showed the likely cause of the loose bolts was due to thermal pressure. The line has pressure relief valve. Tank 150-65 was out of service for API 653 and returned to service in march 2020. The thermal for the tank-lines were routed to tank 150-66. The thermal line that leaked was not rerouted to 150-65 until 18 september 2020 (13 days after incident). The gasket was replaced out of an abundance of caution. Plan for prevention: the flange will remain exposed and not reburied. On a go forward basis, the thermal relief system will be reviewed as the tanks is returned to service using the manway removal form.
Report Received Date 2020-10-02 00:00:00
Iyear 2020
Report Number 20200270
Supplemental Number 34653
Report Type Supplemental Final
Operator Id 26041 PHMSA Enforcement
Name Kinder Morgan Liquid Terminals, Llc
Operator Street Address 1001 Louisiana St, Suite 1000
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2020-09-03 14:30:00
Location Latitude 29.733197 Google Maps OpenStreetMap
Location Longitude -95.202372 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Other
Commodity Details Condensate
Unintentional Release Bbls 2.1
Recovered Bbls 2.1
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2020-09-03 14:30:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain The Pipeline Was Not Active At The Time Of Discovery
On Site Datetime 2020-09-03 14:30:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Kinder Morgan Pasadena Terminal
Segment Name Tank Line Of Tank 150-65
Onshore State Abbreviation Tx
Onshore Postal Code 77506
Onshore City Name Pasadena
Onshore County Name Harris
Designated Location Milepost/valve Station
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 12
Crossing No
Pipe Facility Type Intrastate
Item Involved Flange Assembly
Installation Year 2007
Material Involved Carbon Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Commercially Nav Ind Yes
Commercially Nav Yes No Yes
High Pop Ind Yes
High Pop Yes No Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 70
Est Cost Prop Damage 50
Est Cost Emergency 0
Est Cost Environmental 24000
Est Cost Other 0
Prpty 24120
Accident Psig 23
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Controllers actions were unrelated to the leak.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Gasket
Additional Thermal Ind Yes
Preparer Name D******* S*******
Preparer Title Manager Compliance Code And Standards
Preparer Email D****************@k***********.com
Preparer Telephone 713-420-6496
Prepared Date 2020-12-23 00:00:00
Authorizer Name D******* S*******
Authorizer Telephone 713-420-6496
Authorizer Title Manager - Compliance Codes And Standards
Authorizer Email D****************@k***********.com
Narrative On september 3, 2020 at 14:30, 2.1 barrels of product was discovered near the e-valve of tank 150-65. The product was cleaned up immediately. The source of the leak was identified as a buried flange near the e-valve. The bolts on the flange were torqued and the leak stopped. The incident investigation showed the likely cause of the loose bolts was due to thermal pressure. The line has pressure relief valve. Tank 150-65 was out of service for API 653 and returned to service in march 2020. The thermal for the tank-lines were routed to tank 150-66. The thermal line that leaked was not rerouted to 150-65 until 18 september 2020 (13 days after incident). The gasket was replaced out of an abundance of caution. Plan for prevention: the flange will remain exposed and not reburied. On a go forward basis, the thermal relief system will be reviewed as the tanks is returned to service using the manway removal form.

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