HL incident on 2020-09-02 — TX

Operator
Plains Pipeline, L.p.
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$7,000
Incident datetime
2020-09-02 12:28
Report number
Location
TX
Narrative
Approximately 279 barrels of crude oil were released from a tank mixer at wolfbone ranch station. The date and time of the release (part a q4) is indicative of the earliest possible time the release could have started, as it was the last time the station had been visited and confirmed crude oil was not being released. The national response center (nrc) was contacted on the basis of estimated costs exceeding $50,000 (initial nrc report #: 1286874, and 48-hour nrc follow-up report #: 1287079). The cause of the incident was determined to be equipment failure of the seal as a result of a manufacturing defect on the bolts and bearings. To prevent future releases, plains has replaced the seal, bolts, and bearings as recommended by the manufacturer, and is conducting further investigations to determine if other mixers of this brand and model require new bolts and bearings. 09/24/2024 - updated by PHMSA per operator approval.
Detailed record list
Report Received Date
2020-10-02 00:00:00
Iyear
2020
Report Number
20200269
Supplemental Number
34331
Report Type
Original Final
Operator Id
Name
Plains Pipeline, L.p.
Operator Street Address
333 Clay Street, Suite 1900
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2020-09-02 07:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
279
Recovered Bbls
190
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2020-09-02 12:28:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2020-09-02 12:30:00
Restart Datetime
2020-09-02 16:40:00
On Site Datetime
2020-09-02 12:28:00
Nrc Rpt Datetime
2020-09-09 10:40:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Wolfbone Ranch Station
Segment Name
Wolfbone Ranch Station Tank Mixer
Onshore State Abbreviation
Tx
Onshore Postal Code
79772
Onshore City Name
Pecos
Onshore County Name
Reeves
Designated Location
Milepost/valve Station
Designated Name
0+00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Tank/vessel
Tank Vessel Subtype
Mixer
Tank Type
Atmospheric
Item Involved Details
Tank Mixer
Installation Year
2015
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
2670
Est Cost Prop Damage
7000
Est Cost Emergency
68000
Est Cost Environmental
0
Est Cost Other
0
Prpty
77670
Accident Psig
7
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Seal (Not Pump Seal) Or Packing
Additional Defect Ind
Yes
Eq Additional Other Ind
Yes
Eq Additional Other Details
Bolts And Bearings
Preparer Name
N****** G*******
Preparer Title
Hse Compliance Specialist
Preparer Email
N*********@p****.com
Preparer Telephone
7136464376
Prepared Date
2020-10-02 00:00:00
Authorizer Name
N***** G*****
Authorizer Telephone
7136464336
Authorizer Title
Hse Compliance Director
Authorizer Email
N******@p****.com
Narrative
Approximately 279 barrels of crude oil were released from a tank mixer at wolfbone ranch station. The date and time of the release (part a q4) is indicative of the earliest possible time the release could have started, as it was the last time the station had been visited and confirmed crude oil was not being released. The national response center (nrc) was contacted on the basis of estimated costs exceeding $50,000 (initial nrc report #: 1286874, and 48-hour nrc follow-up report #: 1287079). The cause of the incident was determined to be equipment failure of the seal as a result of a manufacturing defect on the bolts and bearings. To prevent future releases, plains has replaced the seal, bolts, and bearings as recommended by the manufacturer, and is conducting further investigations to determine if other mixers of this brand and model require new bolts and bearings. 09/24/2024 - updated by PHMSA per operator approval.
Report Received Date 2020-10-02 00:00:00
Iyear 2020
Report Number 20200269
Supplemental Number 34331
Report Type Original Final
Operator Id 300 PHMSA Enforcement
Name Plains Pipeline, L.p.
Operator Street Address 333 Clay Street, Suite 1900
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2020-09-02 07:00:00
Location Latitude 31.279649 Google Maps OpenStreetMap
Location Longitude -103.370868 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 279
Recovered Bbls 190
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2020-09-02 12:28:00
System Part Involved Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2020-09-02 12:30:00
Restart Datetime 2020-09-02 16:40:00
On Site Datetime 2020-09-02 12:28:00
Nrc Rpt Datetime 2020-09-09 10:40:00
Nrc Rpt Num 1286874 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Wolfbone Ranch Station
Segment Name Wolfbone Ranch Station Tank Mixer
Onshore State Abbreviation Tx
Onshore Postal Code 79772
Onshore City Name Pecos
Onshore County Name Reeves
Designated Location Milepost/valve Station
Designated Name 0+00
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Tank/vessel
Tank Vessel Subtype Mixer
Tank Type Atmospheric
Item Involved Details Tank Mixer
Installation Year 2015
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 2670
Est Cost Prop Damage 7000
Est Cost Emergency 68000
Est Cost Environmental 0
Est Cost Other 0
Prpty 77670
Accident Psig 7
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Seal (Not Pump Seal) Or Packing
Additional Defect Ind Yes
Eq Additional Other Ind Yes
Eq Additional Other Details Bolts And Bearings
Preparer Name N****** G*******
Preparer Title Hse Compliance Specialist
Preparer Email N*********@p****.com
Preparer Telephone 7136464376
Prepared Date 2020-10-02 00:00:00
Authorizer Name N***** G*****
Authorizer Telephone 7136464336
Authorizer Title Hse Compliance Director
Authorizer Email N******@p****.com
Narrative Approximately 279 barrels of crude oil were released from a tank mixer at wolfbone ranch station. The date and time of the release (part a q4) is indicative of the earliest possible time the release could have started, as it was the last time the station had been visited and confirmed crude oil was not being released. The national response center (nrc) was contacted on the basis of estimated costs exceeding $50,000 (initial nrc report #: 1286874, and 48-hour nrc follow-up report #: 1287079). The cause of the incident was determined to be equipment failure of the seal as a result of a manufacturing defect on the bolts and bearings. To prevent future releases, plains has replaced the seal, bolts, and bearings as recommended by the manufacturer, and is conducting further investigations to determine if other mixers of this brand and model require new bolts and bearings. 09/24/2024 - updated by PHMSA per operator approval.

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