HL incident on 2020-08-31 — TX

Operator
Kinder Morgan Co2 Co. Lp
Cause
Incorrect Operation
Commodity
Co2 (Carbon Dioxide)
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$510
Incident datetime
2020-08-31 11:45
Report number
Location
TX
Narrative
On 8/31/2020, a kinder morgan operator discovered a leak on a stopple fitting flange at the poquita station. The operator notified the km manager who then notified the control room. Km operations team blew down the space between the completion plug and blind flange using a 1/4" valve. The blind flange was then re-torqued to a higher torque value to stop the leak. As a result of our root cause analysis, two new procedures are being developed to be included as CO2 construction standards. In addition to the new procedures, a listing will be created that will include location and maintenance requirements for identified flanges and will be maintained as a site specific procedure.
Detailed record list
Report Received Date
2020-09-29 00:00:00
Iyear
2020
Report Number
20200264
Supplemental Number
34456
Report Type
Supplemental Final
Operator Id
Name
Kinder Morgan Co2 Co. Lp
Operator Street Address
1001 Louisiana St, Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2020-08-31 11:45:00
Location Latitude
Location Longitude
Commodity Released Type
Co2 (Carbon Dioxide)
Unintentional Release Bbls
0.47
Intentional Release Bbls
4.38
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2020-08-31 11:45:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Due To The Nature Of The Release, Shutting Down Would Not Have Been Effective
On Site Datetime
2020-08-31 11:45:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
0
Pipe Fac Name
Poquita Station
Segment Name
Placitas To Poquita
Onshore State Abbreviation
Nm
Onshore Postal Code
88201
Onshore City Name
Roswell
Onshore County Name
Chaves
Designated Location
Milepost/valve Station
Designated Name
Mp378
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tap Fitting(Stopple, Thread-O-Ring, Weld-O-Let, Etc.)
Installation Year
2016
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Stopple Fitting Flange Gasket
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
17
Est Cost Prop Damage
510
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
527
Accident Psig
1973
Mop Psig
2000
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
Unknown
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The control center operations were normal at the time of the incident. There were no scada indications of a release.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Other Incorrect Operation
Operation Type
Other Incorrect Operation
Operation Details
Bolt Load Used On Blind Flange Was Inadequate
Related Inadequate Proc Ind
Yes
Category Type
Other Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
J*** J****
Preparer Title
Supervisor - Regulatory
Preparer Email
J*********@k***********.com
Preparer Telephone
713-369-8078
Prepared Date
2020-10-30 00:00:00
Authorizer Name
M***** L*******
Authorizer Telephone
713-420-4649
Authorizer Title
Director-Operations And Engineering
Authorizer Email
M**************@k***********.com
Narrative
On 8/31/2020, a kinder morgan operator discovered a leak on a stopple fitting flange at the poquita station. The operator notified the km manager who then notified the control room. Km operations team blew down the space between the completion plug and blind flange using a 1/4" valve. The blind flange was then re-torqued to a higher torque value to stop the leak. As a result of our root cause analysis, two new procedures are being developed to be included as CO2 construction standards. In addition to the new procedures, a listing will be created that will include location and maintenance requirements for identified flanges and will be maintained as a site specific procedure.
Report Received Date 2020-09-29 00:00:00
Iyear 2020
Report Number 20200264
Supplemental Number 34456
Report Type Supplemental Final
Operator Id 31555 PHMSA Enforcement
Name Kinder Morgan Co2 Co. Lp
Operator Street Address 1001 Louisiana St, Suite 1000
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2020-08-31 11:45:00
Location Latitude 33.96455 Google Maps OpenStreetMap
Location Longitude -104.58069 Google Maps OpenStreetMap
Commodity Released Type Co2 (Carbon Dioxide)
Unintentional Release Bbls 0.47
Intentional Release Bbls 4.38
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2020-08-31 11:45:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Due To The Nature Of The Release, Shutting Down Would Not Have Been Effective
On Site Datetime 2020-08-31 11:45:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 0
Pipe Fac Name Poquita Station
Segment Name Placitas To Poquita
Onshore State Abbreviation Nm
Onshore Postal Code 88201
Onshore City Name Roswell
Onshore County Name Chaves
Designated Location Milepost/valve Station
Designated Name Mp378
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Tap Fitting(Stopple, Thread-O-Ring, Weld-O-Let, Etc.)
Installation Year 2016
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Stopple Fitting Flange Gasket
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 17
Est Cost Prop Damage 510
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 527
Accident Psig 1973
Mop Psig 2000
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated Unknown
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The control center operations were normal at the time of the incident. There were no scada indications of a release.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Other Incorrect Operation
Operation Type Other Incorrect Operation
Operation Details Bolt Load Used On Blind Flange Was Inadequate
Related Inadequate Proc Ind Yes
Category Type Other Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name J*** J****
Preparer Title Supervisor - Regulatory
Preparer Email J*********@k***********.com
Preparer Telephone 713-369-8078
Prepared Date 2020-10-30 00:00:00
Authorizer Name M***** L*******
Authorizer Telephone 713-420-4649
Authorizer Title Director-Operations And Engineering
Authorizer Email M**************@k***********.com
Narrative On 8/31/2020, a kinder morgan operator discovered a leak on a stopple fitting flange at the poquita station. The operator notified the km manager who then notified the control room. Km operations team blew down the space between the completion plug and blind flange using a 1/4" valve. The blind flange was then re-torqued to a higher torque value to stop the leak. As a result of our root cause analysis, two new procedures are being developed to be included as CO2 construction standards. In addition to the new procedures, a listing will be created that will include location and maintenance requirements for identified flanges and will be maintained as a site specific procedure.

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