HL incident on 2020-08-25 — TX

Operator
Permian Express Partners Llc
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$21,200
Incident datetime
2020-08-25 09:00
Report number
Location
TX
Narrative
On 8-25-20 at approximately 9:00am, the hebert operations supervisor received notification from exxon mobile that oil was leaking at beaumont station. The oil migrated off our property onto the adjoining exxon facility. No public land was affected. The control center was notified to shut down the pipeline. The pipeline segment and trap were isolated. After excavating it was determined that the 8 inch kicker line on 16 inch pig trap had a hole at the 6 oclock position releasing approximately 23 barrels of crude oil onto the soil. The repair and start-up was prolonged due to hurricane laura and the complexity of the excavation. Initial estimates were below the immediate reporting criteria. But due to the complexity of the excavation and repair, a notification was placed to the nrc on 9/28/2020 at 2:51pm, nrc # 1288501, due to invoices coming in and meeting the 50k threshold. All soil and rock was remediated off site.
Detailed record list
Report Received Date
2020-09-23 00:00:00
Iyear
2020
Report Number
20200259
Supplemental Number
34346
Report Type
Supplemental Final
Operator Id
Name
Permian Express Partners Llc
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2020-08-25 09:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
23
Recovered Bbls
23
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Other
Accident Details
Operator From Other Company
Incident Identified Datetime
2020-08-25 09:00:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2020-08-25 09:16:00
Restart Datetime
2020-08-28 15:08:00
On Site Datetime
2020-08-25 09:30:00
Nrc Rpt Datetime
2020-09-28 14:51:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Beaumont Station
Segment Name
Nederland Access
Onshore State Abbreviation
Tx
Onshore Postal Code
77705
Onshore City Name
Beaumont
Onshore County Name
Jefferson
Designated Location
Milepost/valve Station
Designated Name
204.83
Federal
No
Location Type
Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
48
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Auxiliary Piping (E.g. Drain Lines)
Installation Year
1956
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
5000
Est Cost Gas Released
900
Est Cost Prop Damage
21200
Est Cost Emergency
8500
Est Cost Environmental
24529
Est Cost Other
0
Prpty
60129
Accident Psig
180
Mop Psig
750
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
General Corrosion
Int Microbiological Ind
Yes
Int Field Exam Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Preparer Name
N****** P********
Preparer Title
Dot Compliance Specialist
Preparer Email
N****************@e*************.com
Preparer Telephone
713-989-4527
Prepared Date
2020-10-07 00:00:00
Authorizer Name
C********** K*****
Authorizer Telephone
9795319036
Authorizer Title
Manager - Regulatory Compliance
Authorizer Email
C***********@e*************.com
Narrative
On 8-25-20 at approximately 9:00am, the hebert operations supervisor received notification from exxon mobile that oil was leaking at beaumont station. The oil migrated off our property onto the adjoining exxon facility. No public land was affected. The control center was notified to shut down the pipeline. The pipeline segment and trap were isolated. After excavating it was determined that the 8 inch kicker line on 16 inch pig trap had a hole at the 6 oclock position releasing approximately 23 barrels of crude oil onto the soil. The repair and start-up was prolonged due to hurricane laura and the complexity of the excavation. Initial estimates were below the immediate reporting criteria. But due to the complexity of the excavation and repair, a notification was placed to the nrc on 9/28/2020 at 2:51pm, nrc # 1288501, due to invoices coming in and meeting the 50k threshold. All soil and rock was remediated off site.
Report Received Date 2020-09-23 00:00:00
Iyear 2020
Report Number 20200259
Supplemental Number 34346
Report Type Supplemental Final
Operator Id 39596 PHMSA Enforcement
Name Permian Express Partners Llc
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2020-08-25 09:00:00
Location Latitude 30.049424 Google Maps OpenStreetMap
Location Longitude -94.069842 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 23
Recovered Bbls 23
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Other
Accident Details Operator From Other Company
Incident Identified Datetime 2020-08-25 09:00:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2020-08-25 09:16:00
Restart Datetime 2020-08-28 15:08:00
On Site Datetime 2020-08-25 09:30:00
Nrc Rpt Datetime 2020-09-28 14:51:00
Nrc Rpt Num 1288501 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Beaumont Station
Segment Name Nederland Access
Onshore State Abbreviation Tx
Onshore Postal Code 77705
Onshore City Name Beaumont
Onshore County Name Jefferson
Designated Location Milepost/valve Station
Designated Name 204.83
Federal No
Location Type Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 48
Crossing No
Pipe Facility Type Interstate
Item Involved Auxiliary Piping (E.g. Drain Lines)
Installation Year 1956
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Est Cost Oper Paid 5000
Est Cost Gas Released 900
Est Cost Prop Damage 21200
Est Cost Emergency 8500
Est Cost Environmental 24529
Est Cost Other 0
Prpty 60129
Accident Psig 180
Mop Psig 750
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results General Corrosion
Int Microbiological Ind Yes
Int Field Exam Basis Ind Yes
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors No
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Not Applicable - Not Mainline Pipe
Preparer Name N****** P********
Preparer Title Dot Compliance Specialist
Preparer Email N****************@e*************.com
Preparer Telephone 713-989-4527
Prepared Date 2020-10-07 00:00:00
Authorizer Name C********** K*****
Authorizer Telephone 9795319036
Authorizer Title Manager - Regulatory Compliance
Authorizer Email C***********@e*************.com
Narrative On 8-25-20 at approximately 9:00am, the hebert operations supervisor received notification from exxon mobile that oil was leaking at beaumont station. The oil migrated off our property onto the adjoining exxon facility. No public land was affected. The control center was notified to shut down the pipeline. The pipeline segment and trap were isolated. After excavating it was determined that the 8 inch kicker line on 16 inch pig trap had a hole at the 6 oclock position releasing approximately 23 barrels of crude oil onto the soil. The repair and start-up was prolonged due to hurricane laura and the complexity of the excavation. Initial estimates were below the immediate reporting criteria. But due to the complexity of the excavation and repair, a notification was placed to the nrc on 9/28/2020 at 2:51pm, nrc # 1288501, due to invoices coming in and meeting the 50k threshold. All soil and rock was remediated off site.

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