Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2020-09-02 — TX
Operator
Phillips 66 Pipeline Llc
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$1,500
Incident datetime
2020-09-02 04:15
Report number
Location
TX
Narrative
During normal operations, a terminal operator discovered a pinhole leak in a temporary terminal pump discharge hose while performing routine operator rounds. The pump was immediately shutdown, product was cleaned up and contaminated soil was properly disposed. The temporary hose was removed from service and replaced with hard pipe to prevent further occurrences. 10/01/2020--trrc asked for report to be updated for a cause of the pinhole in the hose. Updated report to reflect hose wear due to laying on a rocky surface.
Detailed record list
Report Received Date
2020-09-22 00:00:00
Iyear
2020
Report Number
20200258
Supplemental Number
34327
Report Type
Supplemental Final
Operator Id
31684
Name
Phillips 66 Pipeline Llc
Operator Street Address
2331 Citywest Blvd
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77042
Local Datetime
2020-09-02 04:15:00
Location Latitude
30.0012
Location Longitude
-93.9775
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Other
Commodity Details
Light Cycle Oil
Unintentional Release Bbls
0.17
Recovered Bbls
0.17
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2020-09-02 04:15:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2020-09-02 04:15:00
Restart Datetime
2020-09-02 17:00:00
On Site Datetime
2020-09-02 04:15:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Phillips 66 Beaumont Terminal
Segment Name
Internal Plant Piping - Xom Lco Pipeline
Onshore State Abbreviation
Tx
Onshore Postal Code
77627
Onshore City Name
Nederland
Onshore County Name
Jefferson
Designated Location
Milepost/valve Station
Designated Name
Internal
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Other
Item Involved Details
Temporary Pump Discharge Hose
Installation Year
2020
Material Involved
Material Other Than Carbon Steel
Material Details
Composite Hose
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
16
Est Cost Prop Damage
1500
Est Cost Emergency
5000
Est Cost Environmental
4500
Est Cost Other
500
Est Cost Other Details
New Hose Rental And Rocks
Prpty
11516
Accident Psig
110
Mop Psig
200
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Material failure - pinhole leak was not due to any operator error or overpressure situation.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Failure Details
Temporary Hose
Eq Additional Other Ind
Yes
Eq Additional Other Details
Wear/friction
Preparer Name
M****** B*********
Preparer Title
Dot Coordinator
Preparer Email
M*******************@p**.com
Preparer Telephone
8327651321
Prepared Date
2020-10-01 00:00:00
Authorizer Name
T*** F****
Authorizer Telephone
8327651632
Authorizer Title
Director Dot Operations Compliance
Authorizer Email
T***********@p**.com
Narrative
During normal operations, a terminal operator discovered a pinhole leak in a temporary terminal pump discharge hose while performing routine operator rounds. The pump was immediately shutdown, product was cleaned up and contaminated soil was properly disposed. The temporary hose was removed from service and replaced with hard pipe to prevent further occurrences. 10/01/2020--trrc asked for report to be updated for a cause of the pinhole in the hose. Updated report to reflect hose wear due to laying on a rocky surface.
| Report Received Date | 2020-09-22 00:00:00 |
|---|---|
| Iyear | 2020 |
| Report Number | 20200258 |
| Supplemental Number | 34327 |
| Report Type | Supplemental Final |
| Operator Id | 31684 PHMSA Enforcement |
| Name | Phillips 66 Pipeline Llc |
| Operator Street Address | 2331 Citywest Blvd |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77042 |
| Local Datetime | 2020-09-02 04:15:00 |
| Location Latitude | 30.0012 Google Maps OpenStreetMap |
| Location Longitude | -93.9775 Google Maps OpenStreetMap |
| Commodity Released Type | Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions |
| Commodity Subtype | Other |
| Commodity Details | Light Cycle Oil |
| Unintentional Release Bbls | 0.17 |
| Recovered Bbls | 0.17 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Local Operating Personnel, Including Contractors |
| Operator Type | Operator Employee |
| Incident Identified Datetime | 2020-09-02 04:15:00 |
| System Part Involved | Onshore Terminal/tank Farm Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | Yes |
| Shutdown Datetime | 2020-09-02 04:15:00 |
| Restart Datetime | 2020-09-02 17:00:00 |
| On Site Datetime | 2020-09-02 04:15:00 |
| Nrc Rpt Num | Nrc Notification Not Required NRC Report How to search |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Phillips 66 Beaumont Terminal |
| Segment Name | Internal Plant Piping - Xom Lco Pipeline |
| Onshore State Abbreviation | Tx |
| Onshore Postal Code | 77627 |
| Onshore City Name | Nederland |
| Onshore County Name | Jefferson |
| Designated Location | Milepost/valve Station |
| Designated Name | Internal |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Incident Area Subtype | Typical Aboveground Facility Piping Or Appurtenance |
| Crossing | No |
| Pipe Facility Type | Intrastate |
| Item Involved | Other |
| Item Involved Details | Temporary Pump Discharge Hose |
| Installation Year | 2020 |
| Material Involved | Material Other Than Carbon Steel |
| Material Details | Composite Hose |
| Release Type | Leak |
| Leak Type | Pinhole |
| Wildlife Impact Ind | No |
| Soil Contamination | Yes |
| Long Term Assessment | No |
| Remediation Ind | Yes |
| Soil Remed Ind | Yes |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | Yes |
| High Pop Ind | Yes |
| High Pop Yes No | Yes |
| Usa Drinking Ind | Yes |
| Usa Drinking Yes No | Yes |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 16 |
| Est Cost Prop Damage | 1500 |
| Est Cost Emergency | 5000 |
| Est Cost Environmental | 4500 |
| Est Cost Other | 500 |
| Est Cost Other Details | New Hose Rental And Rocks |
| Prpty | 11516 |
| Accident Psig | 110 |
| Mop Psig | 200 |
| Accident Pressure | Pressure Did Not Exceed Mop |
| Pressure Restriction Ind | No |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Scada In Place Ind | No |
| Cpm In Place Ind | No |
| Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
| Investigation Status Details | Material failure - pinhole leak was not due to any operator error or overpressure situation. |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Other Equipment Failure |
| Eq Failure Type | Other Equipment Failure |
| Failure Details | Temporary Hose |
| Eq Additional Other Ind | Yes |
| Eq Additional Other Details | Wear/friction |
| Preparer Name | M****** B********* |
| Preparer Title | Dot Coordinator |
| Preparer Email | M*******************@p**.com |
| Preparer Telephone | 8327651321 |
| Prepared Date | 2020-10-01 00:00:00 |
| Authorizer Name | T*** F**** |
| Authorizer Telephone | 8327651632 |
| Authorizer Title | Director Dot Operations Compliance |
| Authorizer Email | T***********@p**.com |
| Narrative | During normal operations, a terminal operator discovered a pinhole leak in a temporary terminal pump discharge hose while performing routine operator rounds. The pump was immediately shutdown, product was cleaned up and contaminated soil was properly disposed. The temporary hose was removed from service and replaced with hard pipe to prevent further occurrences. 10/01/2020--trrc asked for report to be updated for a cause of the pinhole in the hose. Updated report to reflect hose wear due to laying on a rocky surface. |
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