HL incident on 2020-08-21 — TX

Operator
Targa Downstream Llc
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$48,472
Incident datetime
2020-08-21 14:01
Report number
Location
TX
Narrative
While completing the 6 month valve inspections on the mlv-17 site a targa employee noticed a tiny spot of ice on the side of a 4" balon ball valve that is/can be used to blowdown the pipeline. This valve is a two piece body type that bolts together with an o-ring forming a seal where to two parts come together. It is this o-ring that was seeping. The leak was barely detectable. Targa employees monitored the condition of the leak continually while making plans to perform the repair. Product was moved downstream out of the line segment using a pig pushed by nitrogen. Once product was removed and valves were closed the nitrogen was blown out of the pipeline and the valve was replaced and pipeline was put back in service.
Detailed record list
Report Received Date
2020-09-15 00:00:00
Iyear
2020
Report Number
20200254
Supplemental Number
34292
Report Type
Supplemental Final
Operator Id
Name
Targa Downstream Llc
Operator Street Address
811 Louisiana St. Suite 2100
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2020-08-21 14:15:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
0.47
Intentional Release Bbls
0.07
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2020-08-21 14:01:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2020-08-22 06:20:00
Restart Datetime
2020-08-24 19:28:00
On Site Datetime
2020-08-21 14:01:00
Nrc Rpt Datetime
2020-08-21 16:17:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
0
Pipe Fac Name
Grand Prix North
Segment Name
Grand Prix North
Onshore State Abbreviation
Tx
Onshore Postal Code
76265
Onshore City Name
Not Within A Municipality
Onshore County Name
Montague
Designated Location
Milepost/valve Station
Designated Name
Okmlv-17 Stat
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
2018
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
15
Est Cost Prop Damage
48472
Est Cost Emergency
4000
Est Cost Environmental
0
Est Cost Other
143000
Est Cost Other Details
Cost Of Nitrogen To Push Pig And Product Down The Pipeline Away From The Valve
Prpty
195487
Accident Psig
589
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
89954
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The o-ring leak was extremely small and undetectable without an instrument.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
O-Ring
Additional Defect Ind
Yes
Preparer Name
R**** J H*******
Preparer Title
Sr Specialist Operational Discipline Group
Preparer Email
R********@t*************.com
Preparer Telephone
918-574-3834
Prepared Date
2020-09-22 00:00:00
Authorizer Name
R**** J H*******
Authorizer Telephone
918-574-3834
Authorizer Title
Sr Specialist Operational Discipline Group
Authorizer Email
R********@t*************.com
Narrative
While completing the 6 month valve inspections on the mlv-17 site a targa employee noticed a tiny spot of ice on the side of a 4" balon ball valve that is/can be used to blowdown the pipeline. This valve is a two piece body type that bolts together with an o-ring forming a seal where to two parts come together. It is this o-ring that was seeping. The leak was barely detectable. Targa employees monitored the condition of the leak continually while making plans to perform the repair. Product was moved downstream out of the line segment using a pig pushed by nitrogen. Once product was removed and valves were closed the nitrogen was blown out of the pipeline and the valve was replaced and pipeline was put back in service.
Report Received Date 2020-09-15 00:00:00
Iyear 2020
Report Number 20200254
Supplemental Number 34292
Report Type Supplemental Final
Operator Id 39823 PHMSA Enforcement
Name Targa Downstream Llc
Operator Street Address 811 Louisiana St. Suite 2100
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2020-08-21 14:15:00
Location Latitude 33.740358 Google Maps OpenStreetMap
Location Longitude -97.585948 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 0.47
Intentional Release Bbls 0.07
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2020-08-21 14:01:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2020-08-22 06:20:00
Restart Datetime 2020-08-24 19:28:00
On Site Datetime 2020-08-21 14:01:00
Nrc Rpt Datetime 2020-08-21 16:17:00
Nrc Rpt Num 1285209 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 0
Pipe Fac Name Grand Prix North
Segment Name Grand Prix North
Onshore State Abbreviation Tx
Onshore Postal Code 76265
Onshore City Name Not Within A Municipality
Onshore County Name Montague
Designated Location Milepost/valve Station
Designated Name Okmlv-17 Stat
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 2018
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 15
Est Cost Prop Damage 48472
Est Cost Emergency 4000
Est Cost Environmental 0
Est Cost Other 143000
Est Cost Other Details Cost Of Nitrogen To Push Pig And Product Down The Pipeline Away From The Valve
Prpty 195487
Accident Psig 589
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 89954
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The o-ring leak was extremely small and undetectable without an instrument.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind O-Ring
Additional Defect Ind Yes
Preparer Name R**** J H*******
Preparer Title Sr Specialist Operational Discipline Group
Preparer Email R********@t*************.com
Preparer Telephone 918-574-3834
Prepared Date 2020-09-22 00:00:00
Authorizer Name R**** J H*******
Authorizer Telephone 918-574-3834
Authorizer Title Sr Specialist Operational Discipline Group
Authorizer Email R********@t*************.com
Narrative While completing the 6 month valve inspections on the mlv-17 site a targa employee noticed a tiny spot of ice on the side of a 4" balon ball valve that is/can be used to blowdown the pipeline. This valve is a two piece body type that bolts together with an o-ring forming a seal where to two parts come together. It is this o-ring that was seeping. The leak was barely detectable. Targa employees monitored the condition of the leak continually while making plans to perform the repair. Product was moved downstream out of the line segment using a pig pushed by nitrogen. Once product was removed and valves were closed the nitrogen was blown out of the pipeline and the valve was replaced and pipeline was put back in service.

All rights reserved. Copyright © by ClearPHMSA