HL incident on 2020-08-14 — GA

Operator
Colonial Pipeline Co
Cause
Material Failure Of Pipe Or Weld
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$248,290
Incident datetime
2020-08-14 18:20
Report number
Location
GA
Narrative
On 8/14/2020 at 18:20, a colonial employee was notified by a local resident about a possible product release in colonial's right-of-way (row) approximately 100 feet north (I.E., downstream) of huntersville-concord road in huntersville, nc. The possible product release location was discovered by utility vehicle riders that were on a trail that crosses the pipeline row. The colonial employee lives in the area and went to inspect the location. Upon inspection, the colonial employee confirmed a product release visible at the ground surface at 18:42 near mile marker 980 that was believed to be gasoline. The colonial employee contacted the colonial control center in alpharetta, ga to provide notification of the visible release and the control center initiated shutdown of lines 1 and 2 at 18:43. The lines were blocked by closing valves upstream of the release location at colonial's charlotte delivery facility (df) and downstream of the release location at the kannapolis station. The colonial operations manager (om) was notified at 18:44, and the director of operations (do) was notified at 19:00, followed by an internal tier 2 response notification at 19:32 to mobilize internal and contractor resources to the site, and established an incident command post to support the response. At 19:43, a nrc notification was made by the control center (report number 1284598). The initial volume was reported at 75 barrels (bbls.) based on the limited information colonial had at the time. Notifications were also made to mecklenburg county, US epa, ncdeq, and PHMSA. The nrc notification was updated on 8/16/2020 at 17:40, with an estimated release volume of 1500 bbls. Based on additional information available to colonial as a result of the initial response efforts. Following confirmation of the product release source being on line 1 (product released was confirmed to be gasoline vs. Line 2 distillate products), line 2 was authorized to restart on 8/15/2020 at 0:05. The product release source was identified on 8/15/2020 at approximately 12:00. The product release source was originating from beneath a prior repair (type a sleeve) made in 2004 to address a pipeline anomaly identified through a previous integrity assessment. The product release was repaired by installing a type b pressure containing sleeve over the prior type a sleeve repair on 8/19/2020. Line 1 was restarted on 8/19/2020 at approximately 21:00 after the repair work was completed. Due to character limitations, details provided in the narrative relating to earlier supplements have been deleted, but are incorporated herein as if restated in full. Supplemented on 9/14/2020. Supplemented on 2/01/2021. Supplemented on 4/17/2021. Supplemented on 7/22/2022 to include updated: date an accident reporting criteria was met, estimated volumes of commodity released and recovered, survey station number, amount reaching groundwater and estimated property damage. The estimate of amount reaching groundwater does not include lnapl entrained below the water table as this data is not available at this time. Relating to the date an accident reporting criteria was met (I.E., part a.4.), the report requires a specific time, we have included that time as 12:00 pm. We are confident, with a reasonable degree of scientific certainty (as verified by a third-party expert), that the accident occurred july 27,2020. However, because this report requires a specific time to be reported, we are using 12:00 pm for purposes of this report only.
Detailed record list
Report Received Date
2020-09-13 00:00:00
Iyear
2020
Report Number
20200253
Supplemental Number
36889
Report Type
Supplemental Final
Operator Id
Name
Colonial Pipeline Co
Operator Street Address
1000 Lake St.
Operator City Name
Alpharetta
Operator State Abbreviation
GA
Operator Postal Code
30009
Local Datetime
2020-07-27 12:00:00
Time Zone
Eastern
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
47619
Recovered Bbls
35566
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2020-08-14 18:20:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
On Site Datetime
2020-08-14 18:42:00
Nrc Rpt Datetime
2020-08-14 19:43:00
Nrc Rpt Num
Ignite Ind
No
Num Pub Evacuated
0
Pipe Fac Name
L01
Segment Name
Charlotte To Kannapolis
Onshore State Abbreviation
Nc
Onshore Postal Code
28078
Onshore City Name
Huntersville
Onshore County Name
Mecklenburg
Designated Location
Survey Station No.
Designated Name
2067+55
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
36
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
40
Pipe Wall Thickness
0.312
Pipe Smys
60000
Pipe Specification
Api 5l
Pipe Seam Type
Dsaw
Pipe Manufacturer
Bethlehem Steel
Pipe Coating Type
Coal Tar
Installation Year
1978
Manufactured Year
1978
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
Yes
Terrestrial Impact Ind
Yes
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
Yes
Groundwater Remed Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
Yes
Groundwater Contam Ind
Yes
Amount Released
892
Could Be Hca
Yes
Commodity Reached Hca
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
14613275
Est Cost Gas Released
2570476
Est Cost Prop Damage
248290
Est Cost Emergency
2930000
Est Cost Environmental
80553266
Est Cost Other
7648918
Est Cost Other Details
Miscellaneous Costs To Support The Response.
Prpty
108564225
Accident Psig
183
Mop Psig
673
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Not contributing factors.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Environmental Cracking-Related
Field Exam Ind
Yes
Metallurgical Ind
Yes
Failure Type
Environmental Cracking-Related
Stress Subtype
Other
Stress Details
Corrosion Fatigue.
Additional Dent Ind
Yes
Additional Crack Ind
Yes
Collected Data Ind
Yes
Emat Ind
Yes
Emat Recent Year
2017
Other Recent Year
2017
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
Yes
Exm Wet Mgnt Partcl Rcnt Year
2004
Exm Other Type
Manual Measurement Of Deformation
Exm Other Rcnt Year
2004
Exm Wet Mgnt Partcl Rcnt Ind
Yes
Exm Other Rcnt Ind
Yes
Preparer Name
Q****** F******
Preparer Title
Director-Pipeline Compliance
Preparer Email
Q*******@c******.com
Preparer Telephone
6787622270
Prepared Date
2022-07-22 00:00:00
Local Contact Name
D***** L******
Local Contact Email
D*******@c******.com
Local Contact Telephone
7708193574
Authorizer Name
Q****** F******
Authorizer Telephone
6787622270
Authorizer Title
Director-Pipeline Compliance
Authorizer Email
Q*******@c******.com
Narrative
On 8/14/2020 at 18:20, a colonial employee was notified by a local resident about a possible product release in colonial's right-of-way (row) approximately 100 feet north (I.E., downstream) of huntersville-concord road in huntersville, nc. The possible product release location was discovered by utility vehicle riders that were on a trail that crosses the pipeline row. The colonial employee lives in the area and went to inspect the location. Upon inspection, the colonial employee confirmed a product release visible at the ground surface at 18:42 near mile marker 980 that was believed to be gasoline. The colonial employee contacted the colonial control center in alpharetta, ga to provide notification of the visible release and the control center initiated shutdown of lines 1 and 2 at 18:43. The lines were blocked by closing valves upstream of the release location at colonial's charlotte delivery facility (df) and downstream of the release location at the kannapolis station. The colonial operations manager (om) was notified at 18:44, and the director of operations (do) was notified at 19:00, followed by an internal tier 2 response notification at 19:32 to mobilize internal and contractor resources to the site, and established an incident command post to support the response. At 19:43, a nrc notification was made by the control center (report number 1284598). The initial volume was reported at 75 barrels (bbls.) based on the limited information colonial had at the time. Notifications were also made to mecklenburg county, US epa, ncdeq, and PHMSA. The nrc notification was updated on 8/16/2020 at 17:40, with an estimated release volume of 1500 bbls. Based on additional information available to colonial as a result of the initial response efforts. Following confirmation of the product release source being on line 1 (product released was confirmed to be gasoline vs. Line 2 distillate products), line 2 was authorized to restart on 8/15/2020 at 0:05. The product release source was identified on 8/15/2020 at approximately 12:00. The product release source was originating from beneath a prior repair (type a sleeve) made in 2004 to address a pipeline anomaly identified through a previous integrity assessment. The product release was repaired by installing a type b pressure containing sleeve over the prior type a sleeve repair on 8/19/2020. Line 1 was restarted on 8/19/2020 at approximately 21:00 after the repair work was completed. Due to character limitations, details provided in the narrative relating to earlier supplements have been deleted, but are incorporated herein as if restated in full. Supplemented on 9/14/2020. Supplemented on 2/01/2021. Supplemented on 4/17/2021. Supplemented on 7/22/2022 to include updated: date an accident reporting criteria was met, estimated volumes of commodity released and recovered, survey station number, amount reaching groundwater and estimated property damage. The estimate of amount reaching groundwater does not include lnapl entrained below the water table as this data is not available at this time. Relating to the date an accident reporting criteria was met (I.E., part a.4.), the report requires a specific time, we have included that time as 12:00 pm. We are confident, with a reasonable degree of scientific certainty (as verified by a third-party expert), that the accident occurred july 27,2020. However, because this report requires a specific time to be reported, we are using 12:00 pm for purposes of this report only.
Report Received Date 2020-09-13 00:00:00
Iyear 2020
Report Number 20200253
Supplemental Number 36889
Report Type Supplemental Final
Operator Id 2552 PHMSA Enforcement
Name Colonial Pipeline Co
Operator Street Address 1000 Lake St.
Operator City Name Alpharetta
Operator State Abbreviation GA
Operator Postal Code 30009
Local Datetime 2020-07-27 12:00:00
Time Zone Eastern
Daylight Savings Ind Yes
Location Latitude 35.414106 Google Maps OpenStreetMap
Location Longitude -80.806185 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 47619
Recovered Bbls 35566
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
Incident Identified Datetime 2020-08-14 18:20:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
On Site Datetime 2020-08-14 18:42:00
Nrc Rpt Datetime 2020-08-14 19:43:00
Nrc Rpt Num 1284598 NRC Report How to search
Ignite Ind No
Num Pub Evacuated 0
Pipe Fac Name L01
Segment Name Charlotte To Kannapolis
Onshore State Abbreviation Nc
Onshore Postal Code 28078
Onshore City Name Huntersville
Onshore County Name Mecklenburg
Designated Location Survey Station No.
Designated Name 2067+55
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 36
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 40
Pipe Wall Thickness 0.312
Pipe Smys 60000
Pipe Specification Api 5l
Pipe Seam Type Dsaw
Pipe Manufacturer Bethlehem Steel
Pipe Coating Type Coal Tar
Installation Year 1978
Manufactured Year 1978
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Wildlife Impact Ind Yes
Terrestrial Impact Ind Yes
Soil Contamination Yes
Long Term Assessment Yes
Remediation Ind Yes
Groundwater Remed Ind Yes
Soil Remed Ind Yes
Water Contam Ind Yes
Groundwater Contam Ind Yes
Amount Released 892
Could Be Hca Yes
Commodity Reached Hca Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 14613275
Est Cost Gas Released 2570476
Est Cost Prop Damage 248290
Est Cost Emergency 2930000
Est Cost Environmental 80553266
Est Cost Other 7648918
Est Cost Other Details Miscellaneous Costs To Support The Response.
Prpty 108564225
Accident Psig 183
Mop Psig 673
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Not contributing factors.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Environmental Cracking-Related
Field Exam Ind Yes
Metallurgical Ind Yes
Failure Type Environmental Cracking-Related
Stress Subtype Other
Stress Details Corrosion Fatigue.
Additional Dent Ind Yes
Additional Crack Ind Yes
Collected Data Ind Yes
Emat Ind Yes
Emat Recent Year 2017
Other Recent Year 2017
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind Yes
Exm Wet Mgnt Partcl Rcnt Year 2004
Exm Other Type Manual Measurement Of Deformation
Exm Other Rcnt Year 2004
Exm Wet Mgnt Partcl Rcnt Ind Yes
Exm Other Rcnt Ind Yes
Preparer Name Q****** F******
Preparer Title Director-Pipeline Compliance
Preparer Email Q*******@c******.com
Preparer Telephone 6787622270
Prepared Date 2022-07-22 00:00:00
Local Contact Name D***** L******
Local Contact Email D*******@c******.com
Local Contact Telephone 7708193574
Authorizer Name Q****** F******
Authorizer Telephone 6787622270
Authorizer Title Director-Pipeline Compliance
Authorizer Email Q*******@c******.com
Narrative On 8/14/2020 at 18:20, a colonial employee was notified by a local resident about a possible product release in colonial's right-of-way (row) approximately 100 feet north (I.E., downstream) of huntersville-concord road in huntersville, nc. The possible product release location was discovered by utility vehicle riders that were on a trail that crosses the pipeline row. The colonial employee lives in the area and went to inspect the location. Upon inspection, the colonial employee confirmed a product release visible at the ground surface at 18:42 near mile marker 980 that was believed to be gasoline. The colonial employee contacted the colonial control center in alpharetta, ga to provide notification of the visible release and the control center initiated shutdown of lines 1 and 2 at 18:43. The lines were blocked by closing valves upstream of the release location at colonial's charlotte delivery facility (df) and downstream of the release location at the kannapolis station. The colonial operations manager (om) was notified at 18:44, and the director of operations (do) was notified at 19:00, followed by an internal tier 2 response notification at 19:32 to mobilize internal and contractor resources to the site, and established an incident command post to support the response. At 19:43, a nrc notification was made by the control center (report number 1284598). The initial volume was reported at 75 barrels (bbls.) based on the limited information colonial had at the time. Notifications were also made to mecklenburg county, US epa, ncdeq, and PHMSA. The nrc notification was updated on 8/16/2020 at 17:40, with an estimated release volume of 1500 bbls. Based on additional information available to colonial as a result of the initial response efforts. Following confirmation of the product release source being on line 1 (product released was confirmed to be gasoline vs. Line 2 distillate products), line 2 was authorized to restart on 8/15/2020 at 0:05. The product release source was identified on 8/15/2020 at approximately 12:00. The product release source was originating from beneath a prior repair (type a sleeve) made in 2004 to address a pipeline anomaly identified through a previous integrity assessment. The product release was repaired by installing a type b pressure containing sleeve over the prior type a sleeve repair on 8/19/2020. Line 1 was restarted on 8/19/2020 at approximately 21:00 after the repair work was completed. Due to character limitations, details provided in the narrative relating to earlier supplements have been deleted, but are incorporated herein as if restated in full. Supplemented on 9/14/2020. Supplemented on 2/01/2021. Supplemented on 4/17/2021. Supplemented on 7/22/2022 to include updated: date an accident reporting criteria was met, estimated volumes of commodity released and recovered, survey station number, amount reaching groundwater and estimated property damage. The estimate of amount reaching groundwater does not include lnapl entrained below the water table as this data is not available at this time. Relating to the date an accident reporting criteria was met (I.E., part a.4.), the report requires a specific time, we have included that time as 12:00 pm. We are confident, with a reasonable degree of scientific certainty (as verified by a third-party expert), that the accident occurred july 27,2020. However, because this report requires a specific time to be reported, we are using 12:00 pm for purposes of this report only.

All rights reserved. Copyright © by ClearPHMSA