HL incident on 2020-08-13 — TX

Operator
Holly Energy Partners - Operating, L.p.
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$5,000
Incident datetime
2020-08-13 14:06
Report number
Location
TX
Narrative
On august 13, 2020, holly energy partners (hep) technicians were performing work on a tank when they noticed what looked like a dark spot near the station piping at russell station. The hep personnel on-site immediately contacted the control center to shut down and block in the pipeline at 14:09 ct. After shutdown, the technicians on-site investigated the facility to determine other possible sources of the leak. Upon further investigation, it was determined there was a leak on the russell station relief line. At this point, the technicians could quantify the amount of the release and reported back to the control room at 14:30 ct that we had a reportable release per 49 cfr 195.50. Vac-trucks and additional hep personnel were dispatched to the site to assist in the cleanup of the release. The pipe from which the oil emanated from was inspected and was found to have corrosion localized pitting at the 6 o" clock position. ****update**** 1/05/2021. The results of the metallurgical analysis showed the root cause to be corrosive commodity and microbiological that caused localized pitting at the low point in the pipe.
Detailed record list
Report Received Date
2020-09-11 00:00:00
Iyear
2020
Report Number
20200251
Supplemental Number
34678
Report Type
Supplemental Final
Operator Id
Name
Holly Energy Partners - Operating, L.p.
Operator Street Address
2323 Victory Ave. Suite 1400
Operator City Name
Dallas
Operator State Abbreviation
TX
Operator Postal Code
75219
Local Datetime
2020-08-13 14:30:00
Location Latitude
Location Longitude
-102.9199632
Commodity Released Type
Crude Oil
Unintentional Release Bbls
1.5
Recovered Bbls
1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2020-08-13 14:06:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2020-08-13 14:06:00
Restart Datetime
2020-08-13 21:25:00
On Site Datetime
2020-08-13 14:06:00
Nrc Rpt Datetime
2020-08-13 15:46:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Riley To Russell
Segment Name
Russell Station
Onshore State Abbreviation
Tx
Onshore Postal Code
79323
Onshore City Name
Not Within A Municipality
Onshore County Name
Gaines
Designated Location
Milepost/valve Station
Designated Name
Pump Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
4.5
Pipe Wall Thickness
0.237
Pipe Smys
Unknown
Pipe Specification
Unknown
Pipe Seam Type
Erw � Unknown Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Other
Pipe Coating Details
Painted, Two Part Epoxy Primer With Polyurethane Top Coating
Installation Year
2000
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Corrosion
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
No
Est Cost Oper Paid
0
Est Cost Gas Released
67
Est Cost Prop Damage
5000
Est Cost Emergency
6285
Est Cost Environmental
6000
Est Cost Other
0
Prpty
17352
Accident Psig
0
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
No
Scada Functional Ind
No
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The failure was the result of corrosion on the relief line - the control room was under steady state operations - nor had they activated the relief line prior to the failure.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Corrosive Commodity Ind
Yes
Int Microbiological Ind
Yes
Int Metallurgical Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
No
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
C*** A****
Preparer Title
Lead Compliance Auditor
Preparer Email
C*********@h**********.com
Preparer Telephone
2149546717
Prepared Date
2021-01-05 00:00:00
Authorizer Name
C*** A****
Authorizer Telephone
2149546717
Authorizer Title
Lead Compliance Auditor
Authorizer Email
C*********@h**********.com
Narrative
On august 13, 2020, holly energy partners (hep) technicians were performing work on a tank when they noticed what looked like a dark spot near the station piping at russell station. The hep personnel on-site immediately contacted the control center to shut down and block in the pipeline at 14:09 ct. After shutdown, the technicians on-site investigated the facility to determine other possible sources of the leak. Upon further investigation, it was determined there was a leak on the russell station relief line. At this point, the technicians could quantify the amount of the release and reported back to the control room at 14:30 ct that we had a reportable release per 49 cfr 195.50. Vac-trucks and additional hep personnel were dispatched to the site to assist in the cleanup of the release. The pipe from which the oil emanated from was inspected and was found to have corrosion localized pitting at the 6 o" clock position. ****update**** 1/05/2021. The results of the metallurgical analysis showed the root cause to be corrosive commodity and microbiological that caused localized pitting at the low point in the pipe.
Report Received Date 2020-09-11 00:00:00
Iyear 2020
Report Number 20200251
Supplemental Number 34678
Report Type Supplemental Final
Operator Id 32011 PHMSA Enforcement
Name Holly Energy Partners - Operating, L.p.
Operator Street Address 2323 Victory Ave. Suite 1400
Operator City Name Dallas
Operator State Abbreviation TX
Operator Postal Code 75219
Local Datetime 2020-08-13 14:30:00
Location Latitude 32.86186765 Google Maps OpenStreetMap
Location Longitude -102.9199632 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 1.5
Recovered Bbls 1
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2020-08-13 14:06:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2020-08-13 14:06:00
Restart Datetime 2020-08-13 21:25:00
On Site Datetime 2020-08-13 14:06:00
Nrc Rpt Datetime 2020-08-13 15:46:00
Nrc Rpt Num 1284489 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Riley To Russell
Segment Name Russell Station
Onshore State Abbreviation Tx
Onshore Postal Code 79323
Onshore City Name Not Within A Municipality
Onshore County Name Gaines
Designated Location Milepost/valve Station
Designated Name Pump Station
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 4.5
Pipe Wall Thickness 0.237
Pipe Smys Unknown
Pipe Specification Unknown
Pipe Seam Type Erw � Unknown Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Other
Pipe Coating Details Painted, Two Part Epoxy Primer With Polyurethane Top Coating
Installation Year 2000
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Corrosion
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment Yes
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Usa Drinking Ind Yes
Usa Drinking Yes No No
Est Cost Oper Paid 0
Est Cost Gas Released 67
Est Cost Prop Damage 5000
Est Cost Emergency 6285
Est Cost Environmental 6000
Est Cost Other 0
Prpty 17352
Accident Psig 0
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind No
Scada Functional Ind No
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The failure was the result of corrosion on the relief line - the control room was under steady state operations - nor had they activated the relief line prior to the failure.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Corrosive Commodity Ind Yes
Int Microbiological Ind Yes
Int Metallurgical Basis Ind Yes
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors No
Corrosion Lining No
Cleaning Dewatering No
Corrosion Coupons Not Applicable - Not Mainline Pipe
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name C*** A****
Preparer Title Lead Compliance Auditor
Preparer Email C*********@h**********.com
Preparer Telephone 2149546717
Prepared Date 2021-01-05 00:00:00
Authorizer Name C*** A****
Authorizer Telephone 2149546717
Authorizer Title Lead Compliance Auditor
Authorizer Email C*********@h**********.com
Narrative On august 13, 2020, holly energy partners (hep) technicians were performing work on a tank when they noticed what looked like a dark spot near the station piping at russell station. The hep personnel on-site immediately contacted the control center to shut down and block in the pipeline at 14:09 ct. After shutdown, the technicians on-site investigated the facility to determine other possible sources of the leak. Upon further investigation, it was determined there was a leak on the russell station relief line. At this point, the technicians could quantify the amount of the release and reported back to the control room at 14:30 ct that we had a reportable release per 49 cfr 195.50. Vac-trucks and additional hep personnel were dispatched to the site to assist in the cleanup of the release. The pipe from which the oil emanated from was inspected and was found to have corrosion localized pitting at the 6 o" clock position. ****update**** 1/05/2021. The results of the metallurgical analysis showed the root cause to be corrosive commodity and microbiological that caused localized pitting at the low point in the pipe.

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