HL incident on 2020-08-12 — TX

Operator
Plantation Pipe Line Co
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2020-08-12 18:30
Report number
Location
TX
Narrative
On august 12th 2020, a km employee was onsite at center station near commerce ga to ensure valve alignment for a cng gauge plate pig passage. During the realignment of the valves after pig passage the employee noticed the stem seal was leaking from vbk valve. The employee began to inject stem packing into the injector and noticed that the old packing was not coming out of the packing pressure relief port. The employee stated that he thought that the body pressure port plug was just another stem packing pressure port and removed the plug from the valve. The removal of the body pressure port plug caused gasoline to be released onto the ground. The control center was notified and the employee began closing manual block valves on the upstream and downstream side of the facility. After the block valves were closed the release stopped and the body pressure port plug was re-installed into the valve. Total release was 19.5 gallons.
Detailed record list
Report Received Date
2020-09-10 00:00:00
Iyear
2020
Report Number
20200250
Supplemental Number
34251
Report Type
Supplemental Final
Operator Id
Name
Plantation Pipe Line Co
Operator Street Address
1001 Louisiana St Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2020-08-12 18:30:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
0.5
Recovered Bbls
0.5
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2020-08-12 18:30:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2020-08-12 18:30:00
Restart Datetime
2020-08-12 23:35:00
On Site Datetime
2020-08-12 18:30:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Center Station
Segment Name
Cng 26" Pipeline
Onshore State Abbreviation
Ga
Onshore Postal Code
30646
Onshore City Name
Hull
Onshore County Name
Madison
Designated Location
Milepost/valve Station
Designated Name
Center
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
1971
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Incorrect Operation
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
23
Est Cost Prop Damage
0
Est Cost Emergency
15419
Est Cost Environmental
0
Est Cost Other
0
Prpty
15442
Accident Psig
467
Mop Psig
720
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
Yes
Cpm In Place Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
1
Num Employees Failed
0
Cause
Incorrect Operation
Cause Details
Other Incorrect Operation
Operation Type
Other Incorrect Operation
Operation Details
Employee Opened Wrong Port On Valve Stem
Related Failure Follow Ind
Yes
Category Type
Other Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
K*** M*******
Preparer Title
Pipeline Engineer
Preparer Email
K************@k***********.com
Preparer Telephone
713-824-3833
Preparer Fax
713-495-2713
Prepared Date
2020-09-10 00:00:00
Authorizer Name
Q****** F******
Authorizer Telephone
770-751-4240
Authorizer Title
Director - Compliance-Codes-Standards
Authorizer Email
Q**************@k***********.com
Narrative
On august 12th 2020, a km employee was onsite at center station near commerce ga to ensure valve alignment for a cng gauge plate pig passage. During the realignment of the valves after pig passage the employee noticed the stem seal was leaking from vbk valve. The employee began to inject stem packing into the injector and noticed that the old packing was not coming out of the packing pressure relief port. The employee stated that he thought that the body pressure port plug was just another stem packing pressure port and removed the plug from the valve. The removal of the body pressure port plug caused gasoline to be released onto the ground. The control center was notified and the employee began closing manual block valves on the upstream and downstream side of the facility. After the block valves were closed the release stopped and the body pressure port plug was re-installed into the valve. Total release was 19.5 gallons.
Report Received Date 2020-09-10 00:00:00
Iyear 2020
Report Number 20200250
Supplemental Number 34251
Report Type Supplemental Final
Operator Id 15674 PHMSA Enforcement
Name Plantation Pipe Line Co
Operator Street Address 1001 Louisiana St Suite 1000
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2020-08-12 18:30:00
Location Latitude 34.06577 Google Maps OpenStreetMap
Location Longitude -83.3171 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 0.5
Recovered Bbls 0.5
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2020-08-12 18:30:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2020-08-12 18:30:00
Restart Datetime 2020-08-12 23:35:00
On Site Datetime 2020-08-12 18:30:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Center Station
Segment Name Cng 26" Pipeline
Onshore State Abbreviation Ga
Onshore Postal Code 30646
Onshore City Name Hull
Onshore County Name Madison
Designated Location Milepost/valve Station
Designated Name Center
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 1971
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Incorrect Operation
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 23
Est Cost Prop Damage 0
Est Cost Emergency 15419
Est Cost Environmental 0
Est Cost Other 0
Prpty 15442
Accident Psig 467
Mop Psig 720
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind Yes
Cpm In Place Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 1
Num Employees Failed 0
Cause Incorrect Operation
Cause Details Other Incorrect Operation
Operation Type Other Incorrect Operation
Operation Details Employee Opened Wrong Port On Valve Stem
Related Failure Follow Ind Yes
Category Type Other Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name K*** M*******
Preparer Title Pipeline Engineer
Preparer Email K************@k***********.com
Preparer Telephone 713-824-3833
Preparer Fax 713-495-2713
Prepared Date 2020-09-10 00:00:00
Authorizer Name Q****** F******
Authorizer Telephone 770-751-4240
Authorizer Title Director - Compliance-Codes-Standards
Authorizer Email Q**************@k***********.com
Narrative On august 12th 2020, a km employee was onsite at center station near commerce ga to ensure valve alignment for a cng gauge plate pig passage. During the realignment of the valves after pig passage the employee noticed the stem seal was leaking from vbk valve. The employee began to inject stem packing into the injector and noticed that the old packing was not coming out of the packing pressure relief port. The employee stated that he thought that the body pressure port plug was just another stem packing pressure port and removed the plug from the valve. The removal of the body pressure port plug caused gasoline to be released onto the ground. The control center was notified and the employee began closing manual block valves on the upstream and downstream side of the facility. After the block valves were closed the release stopped and the body pressure port plug was re-installed into the valve. Total release was 19.5 gallons.

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