HL incident on 2020-08-10 — TX

Operator
Enbridge Storage (Cushing) L.l.c.
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$160,000
Incident datetime
2020-08-10 13:30
Report number
Location
TX
Narrative
On august 10, 2020 at approximately 11:30 am cdt crude oil was discovered in the tank berm of tank 3013 by field personnel performing routine rounds at the cushing terminal. The cushing control center was contacted and the area of concern was isolated and pipeline maintenance personnel began excavating to investigate the source of the release. Due to strong winds and lightening, the excavation and cleanup work was delayed. A call to the nrc was made on august 11, 2020 at 11:46 am cdt (report #1284289) once the source of the release was identified as a pinhole in the relief line to tank 3013 and it was determined that the costs would exceed the nrc reporting threshold. The 48-hour nrc notification was made on august 13, 2020 at 10:46 am cdt (report #1284450). After further investigation it was determined that internal corrosion caused the pinhole which led to the release of two barrels of crude oil. Additional integrity issues have been identified with the tank line and it is currently isolated from all sources of product until final repair determination is made. Contaminated soil has been cleaned up and disposed of at an approved site. Additional soil remediation is expected to be ongoing.
Detailed record list
Report Received Date
2020-09-09 00:00:00
Iyear
2020
Report Number
20200247
Supplemental Number
34626
Report Type
Supplemental Final
Operator Id
Name
Enbridge Storage (Cushing) L.l.c.
Operator Street Address
915 N Eldridge Parkway, Suite 1100
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2020-08-10 13:30:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
2
Recovered Bbls
2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2020-08-10 13:30:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Tank Lines Were Isolated
On Site Datetime
2020-08-10 13:30:00
Nrc Rpt Datetime
2020-08-11 11:46:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Cushing South Terminal
Segment Name
Tank 3013 To M223
Onshore State Abbreviation
Ok
Onshore Postal Code
74023
Onshore City Name
Cushing
Onshore County Name
Lincoln
Designated Location
Milepost/valve Station
Designated Name
Cushing
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
12
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
24
Pipe Wall Thickness
0.375
Pipe Smys
30000
Pipe Specification
Api 5l
Pipe Seam Type
Erw � Unknown Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Coal Tar
Installation Year
Unknown
Manufactured Year
1978
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
80
Est Cost Prop Damage
160000
Est Cost Emergency
5000
Est Cost Environmental
15000
Est Cost Other
0
Prpty
180080
Accident Psig
26
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Release was identified by field personnel and not a result of control center actions.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Microbiological Ind
Yes
Int Field Exam Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
S**** S****
Preparer Title
Sr Compliance Analyst
Preparer Email
S**********@e*******.com
Preparer Telephone
218-206-5872
Prepared Date
2020-12-16 00:00:00
Authorizer Name
S**** D*****
Authorizer Telephone
715-718-1236
Authorizer Title
Supervisor Us Pipeline Compliance
Authorizer Email
S************@e*******.com
Narrative
On august 10, 2020 at approximately 11:30 am cdt crude oil was discovered in the tank berm of tank 3013 by field personnel performing routine rounds at the cushing terminal. The cushing control center was contacted and the area of concern was isolated and pipeline maintenance personnel began excavating to investigate the source of the release. Due to strong winds and lightening, the excavation and cleanup work was delayed. A call to the nrc was made on august 11, 2020 at 11:46 am cdt (report #1284289) once the source of the release was identified as a pinhole in the relief line to tank 3013 and it was determined that the costs would exceed the nrc reporting threshold. The 48-hour nrc notification was made on august 13, 2020 at 10:46 am cdt (report #1284450). After further investigation it was determined that internal corrosion caused the pinhole which led to the release of two barrels of crude oil. Additional integrity issues have been identified with the tank line and it is currently isolated from all sources of product until final repair determination is made. Contaminated soil has been cleaned up and disposed of at an approved site. Additional soil remediation is expected to be ongoing.
Report Received Date 2020-09-09 00:00:00
Iyear 2020
Report Number 20200247
Supplemental Number 34626
Report Type Supplemental Final
Operator Id 39145 PHMSA Enforcement
Name Enbridge Storage (Cushing) L.l.c.
Operator Street Address 915 N Eldridge Parkway, Suite 1100
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2020-08-10 13:30:00
Location Latitude 35.934323 Google Maps OpenStreetMap
Location Longitude -96.750957 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 2
Recovered Bbls 2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2020-08-10 13:30:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Tank Lines Were Isolated
On Site Datetime 2020-08-10 13:30:00
Nrc Rpt Datetime 2020-08-11 11:46:00
Nrc Rpt Num 1284289 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Cushing South Terminal
Segment Name Tank 3013 To M223
Onshore State Abbreviation Ok
Onshore Postal Code 74023
Onshore City Name Cushing
Onshore County Name Lincoln
Designated Location Milepost/valve Station
Designated Name Cushing
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 12
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 24
Pipe Wall Thickness 0.375
Pipe Smys 30000
Pipe Specification Api 5l
Pipe Seam Type Erw � Unknown Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Coal Tar
Installation Year Unknown
Manufactured Year 1978
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 80
Est Cost Prop Damage 160000
Est Cost Emergency 5000
Est Cost Environmental 15000
Est Cost Other 0
Prpty 180080
Accident Psig 26
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Release was identified by field personnel and not a result of control center actions.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Microbiological Ind Yes
Int Field Exam Basis Ind Yes
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors No
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Not Applicable - Not Mainline Pipe
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name S**** S****
Preparer Title Sr Compliance Analyst
Preparer Email S**********@e*******.com
Preparer Telephone 218-206-5872
Prepared Date 2020-12-16 00:00:00
Authorizer Name S**** D*****
Authorizer Telephone 715-718-1236
Authorizer Title Supervisor Us Pipeline Compliance
Authorizer Email S************@e*******.com
Narrative On august 10, 2020 at approximately 11:30 am cdt crude oil was discovered in the tank berm of tank 3013 by field personnel performing routine rounds at the cushing terminal. The cushing control center was contacted and the area of concern was isolated and pipeline maintenance personnel began excavating to investigate the source of the release. Due to strong winds and lightening, the excavation and cleanup work was delayed. A call to the nrc was made on august 11, 2020 at 11:46 am cdt (report #1284289) once the source of the release was identified as a pinhole in the relief line to tank 3013 and it was determined that the costs would exceed the nrc reporting threshold. The 48-hour nrc notification was made on august 13, 2020 at 10:46 am cdt (report #1284450). After further investigation it was determined that internal corrosion caused the pinhole which led to the release of two barrels of crude oil. Additional integrity issues have been identified with the tank line and it is currently isolated from all sources of product until final repair determination is made. Contaminated soil has been cleaned up and disposed of at an approved site. Additional soil remediation is expected to be ongoing.

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