HL incident on 2020-08-07 — TX

Operator
Enterprise Products Operating Llc
Cause
Corrosion Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$175,000
Incident datetime
2020-08-07 14:56
Report number
Location
TX
Narrative
On 8/6/2020 at 15:00 aerial patrol reported dead vegetation on pipeline right of way; there are several pipelines in the same right of way. On 8/7/2020, enterprise began to expose the pipeline but stopped due to hydrocarbons in the soil. At 14:56, enterprise discovered that the leak was on c53 pipeline and notified pipeline control to isolate the pipeline. At 15:40 it was determined that this would be reportable event to the nrc due to expected cost of repair. The pipeline was purged and the failed segment was cut out and replaced. Visual examination of the cut-out section indicates external corrosion. Trrc notified on 8/7/2020 at 16:21; incident # 2244 nrc 48 hr. Update 8/9/2020 at 12:24 - 1284120 updated cost 12/12/2020 updated cost 1/29/2021
Detailed record list
Report Received Date
2020-09-04 00:00:00
Iyear
2020
Report Number
20200244
Supplemental Number
34852
Report Type
Supplemental Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2020-08-06 15:00:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Y-Grade
Unintentional Release Bbls
10
Intentional Release Bbls
900
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Air Patrol
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2020-08-07 14:56:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2020-08-07 15:07:00
Restart Datetime
2020-08-13 21:07:00
On Site Datetime
2020-08-07 14:27:00
Nrc Rpt Datetime
2020-08-07 16:15:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
0
Pipe Fac Name
Saac Expanion-Dean
Segment Name
Cr 77 To S23 Tie-In
Onshore State Abbreviation
Tx
Onshore Postal Code
78387
Onshore City Name
Not Within A Municipality
Onshore County Name
San Patricio
Designated Location
Survey Station No.
Designated Name
22+15
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
50
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
6
Pipe Wall Thickness
0.25
Pipe Smys
46000
Pipe Specification
Api-5l
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Republic Steel
Pipe Coating Type
Coal Tar
Installation Year
1956
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Vegetation Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
50000
Est Cost Gas Released
19000
Est Cost Prop Damage
175000
Est Cost Emergency
0
Est Cost Environmental
1235000
Est Cost Other
0
Prpty
1479000
Accident Psig
873
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
26400
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
Localized Pitting
Galvanic Corrosion Ind
Yes
Field Exam Basis Ind
Yes
Underground Location
Yes
Under Cathodic Protection Ind
Yes
Cathodic Pro Start Year
Unknown
Shielding Evident
Yes
Cathodic Survey Type
Yes
Close Interval Survey Ind
Yes
Close Interval Survey Year
2014
Prior Damage
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Other Tool Tech Ind
Yes
Axial Recent Year
2013
Other Tool
Def
Other Recent Year
2013
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2019
Hydrtst Most Rcnt Pressure
1861
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
N*** B******
Preparer Title
Sr. Pipeline Compliance Specialist
Preparer Email
W********@e****.com
Preparer Telephone
713-381-3536
Prepared Date
2021-02-12 00:00:00
Authorizer Name
N*** T*****
Authorizer Telephone
713-381-2493
Authorizer Title
Compliance Manager
Authorizer Email
N*******@e****.com
Narrative
On 8/6/2020 at 15:00 aerial patrol reported dead vegetation on pipeline right of way; there are several pipelines in the same right of way. On 8/7/2020, enterprise began to expose the pipeline but stopped due to hydrocarbons in the soil. At 14:56, enterprise discovered that the leak was on c53 pipeline and notified pipeline control to isolate the pipeline. At 15:40 it was determined that this would be reportable event to the nrc due to expected cost of repair. The pipeline was purged and the failed segment was cut out and replaced. Visual examination of the cut-out section indicates external corrosion. Trrc notified on 8/7/2020 at 16:21; incident # 2244 nrc 48 hr. Update 8/9/2020 at 12:24 - 1284120 updated cost 12/12/2020 updated cost 1/29/2021
Report Received Date 2020-09-04 00:00:00
Iyear 2020
Report Number 20200244
Supplemental Number 34852
Report Type Supplemental Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2020-08-06 15:00:00
Location Latitude 28.005351 Google Maps OpenStreetMap
Location Longitude -97.465178 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Y-Grade
Unintentional Release Bbls 10
Intentional Release Bbls 900
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Air Patrol
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2020-08-07 14:56:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2020-08-07 15:07:00
Restart Datetime 2020-08-13 21:07:00
On Site Datetime 2020-08-07 14:27:00
Nrc Rpt Datetime 2020-08-07 16:15:00
Nrc Rpt Num 1284018 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 0
Pipe Fac Name Saac Expanion-Dean
Segment Name Cr 77 To S23 Tie-In
Onshore State Abbreviation Tx
Onshore Postal Code 78387
Onshore City Name Not Within A Municipality
Onshore County Name San Patricio
Designated Location Survey Station No.
Designated Name 22+15
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 50
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 6
Pipe Wall Thickness 0.25
Pipe Smys 46000
Pipe Specification Api-5l
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer Republic Steel
Pipe Coating Type Coal Tar
Installation Year 1956
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Vegetation Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 50000
Est Cost Gas Released 19000
Est Cost Prop Damage 175000
Est Cost Emergency 0
Est Cost Environmental 1235000
Est Cost Other 0
Prpty 1479000
Accident Psig 873
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 26400
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results Localized Pitting
Galvanic Corrosion Ind Yes
Field Exam Basis Ind Yes
Underground Location Yes
Under Cathodic Protection Ind Yes
Cathodic Pro Start Year Unknown
Shielding Evident Yes
Cathodic Survey Type Yes
Close Interval Survey Ind Yes
Close Interval Survey Year 2014
Prior Damage Yes
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Other Tool Tech Ind Yes
Axial Recent Year 2013
Other Tool Def
Other Recent Year 2013
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 2019
Hydrtst Most Rcnt Pressure 1861
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name N*** B******
Preparer Title Sr. Pipeline Compliance Specialist
Preparer Email W********@e****.com
Preparer Telephone 713-381-3536
Prepared Date 2021-02-12 00:00:00
Authorizer Name N*** T*****
Authorizer Telephone 713-381-2493
Authorizer Title Compliance Manager
Authorizer Email N*******@e****.com
Narrative On 8/6/2020 at 15:00 aerial patrol reported dead vegetation on pipeline right of way; there are several pipelines in the same right of way. On 8/7/2020, enterprise began to expose the pipeline but stopped due to hydrocarbons in the soil. At 14:56, enterprise discovered that the leak was on c53 pipeline and notified pipeline control to isolate the pipeline. At 15:40 it was determined that this would be reportable event to the nrc due to expected cost of repair. The pipeline was purged and the failed segment was cut out and replaced. Visual examination of the cut-out section indicates external corrosion. Trrc notified on 8/7/2020 at 16:21; incident # 2244 nrc 48 hr. Update 8/9/2020 at 12:24 - 1284120 updated cost 12/12/2020 updated cost 1/29/2021

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