HL incident on 2020-08-07 — TX

Operator
Enbridge Storage (Cushing) L.l.c.
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$6,000
Incident datetime
2020-08-07 06:44
Report number
Location
TX
Narrative
On august 7, 2020 at approximately 6:44 am cdt operations technicians discovered crude oil seeping up near valves 206-b-301 and 206-b-302 in manifold 206 within the cushing north terminal. After hydro excavation the source was determined to be a pinhole in the heat affected zone on the flange side of the weld between the tee fitting and flange connected to valve 206-b-301. The affected tee fitting was removed and blinds were installed. This section of pipe has been idle since it was replaced with a new manifold. Approximately 1 barrel of oil was released. All free oil was recovered and contaminated soils removed. A metallurgical analysis was completed and identified internal corrosion on the tee as the cause of the pinhole release.
Detailed record list
Report Received Date
2020-09-03 00:00:00
Iyear
2020
Report Number
20200243
Supplemental Number
34633
Report Type
Supplemental Final
Operator Id
Name
Enbridge Storage (Cushing) L.l.c.
Operator Street Address
915 N Eldridge Parkway, Suite 1100
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2020-08-07 06:44:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
1
Recovered Bbls
1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2020-08-07 06:44:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Line Was Isolated
On Site Datetime
2020-08-07 06:44:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Cushing North Terminal
Segment Name
Manifold 206
Onshore State Abbreviation
Ok
Onshore Postal Code
74023
Onshore City Name
Cushing
Onshore County Name
Payne
Designated Location
Milepost/valve Station
Designated Name
Cushing
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
18
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Weld, Including Heat-Affected Zone
Weld Subtype
Other Butt Weld
Installation Year
2015
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
40
Est Cost Prop Damage
6000
Est Cost Emergency
22000
Est Cost Environmental
11000
Est Cost Other
0
Prpty
39040
Accident Psig
9
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Lack of control center involvement. Release was identified by field personnel.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Other Corrosion Ind
Yes
Int Corrosion Type Details
Corrosion Product Build Up
Int Metallurgical Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
S**** S****
Preparer Title
Sr Compliance Analyst
Preparer Email
S**********@e*******.com
Preparer Telephone
218-206-5872
Prepared Date
2020-12-17 00:00:00
Authorizer Name
S**** D*****
Authorizer Telephone
715-718-1236
Authorizer Title
Supervisor Us Pipeline Compliance
Authorizer Email
S************@e*******.com
Narrative
On august 7, 2020 at approximately 6:44 am cdt operations technicians discovered crude oil seeping up near valves 206-b-301 and 206-b-302 in manifold 206 within the cushing north terminal. After hydro excavation the source was determined to be a pinhole in the heat affected zone on the flange side of the weld between the tee fitting and flange connected to valve 206-b-301. The affected tee fitting was removed and blinds were installed. This section of pipe has been idle since it was replaced with a new manifold. Approximately 1 barrel of oil was released. All free oil was recovered and contaminated soils removed. A metallurgical analysis was completed and identified internal corrosion on the tee as the cause of the pinhole release.
Report Received Date 2020-09-03 00:00:00
Iyear 2020
Report Number 20200243
Supplemental Number 34633
Report Type Supplemental Final
Operator Id 39145 PHMSA Enforcement
Name Enbridge Storage (Cushing) L.l.c.
Operator Street Address 915 N Eldridge Parkway, Suite 1100
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2020-08-07 06:44:00
Location Latitude 35.95886 Google Maps OpenStreetMap
Location Longitude -96.75335 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 1
Recovered Bbls 1
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2020-08-07 06:44:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Line Was Isolated
On Site Datetime 2020-08-07 06:44:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Cushing North Terminal
Segment Name Manifold 206
Onshore State Abbreviation Ok
Onshore Postal Code 74023
Onshore City Name Cushing
Onshore County Name Payne
Designated Location Milepost/valve Station
Designated Name Cushing
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 18
Crossing No
Pipe Facility Type Interstate
Item Involved Weld, Including Heat-Affected Zone
Weld Subtype Other Butt Weld
Installation Year 2015
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 40
Est Cost Prop Damage 6000
Est Cost Emergency 22000
Est Cost Environmental 11000
Est Cost Other 0
Prpty 39040
Accident Psig 9
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Lack of control center involvement. Release was identified by field personnel.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Other Corrosion Ind Yes
Int Corrosion Type Details Corrosion Product Build Up
Int Metallurgical Basis Ind Yes
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors No
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Not Applicable - Not Mainline Pipe
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name S**** S****
Preparer Title Sr Compliance Analyst
Preparer Email S**********@e*******.com
Preparer Telephone 218-206-5872
Prepared Date 2020-12-17 00:00:00
Authorizer Name S**** D*****
Authorizer Telephone 715-718-1236
Authorizer Title Supervisor Us Pipeline Compliance
Authorizer Email S************@e*******.com
Narrative On august 7, 2020 at approximately 6:44 am cdt operations technicians discovered crude oil seeping up near valves 206-b-301 and 206-b-302 in manifold 206 within the cushing north terminal. After hydro excavation the source was determined to be a pinhole in the heat affected zone on the flange side of the weld between the tee fitting and flange connected to valve 206-b-301. The affected tee fitting was removed and blinds were installed. This section of pipe has been idle since it was replaced with a new manifold. Approximately 1 barrel of oil was released. All free oil was recovered and contaminated soils removed. A metallurgical analysis was completed and identified internal corrosion on the tee as the cause of the pinhole release.

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