HL incident on 2020-07-18 — TX

Operator
Dcp Midstream
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$15,000
Incident datetime
2020-07-18 05:18
Report number
Location
TX
Narrative
Ngl tech was called out for a station shut-in at approximately 0518 hours. Tech arrived to location at 0623 hours and discovered the filter case door closure leaking. Tech began to isolate the filter at 0627 hours and isolation was complete at 0650 hours. Engineering total loss calculation at (7:33) determined the amount to be 22.35 gallons making the leak reportable. 11/3/20 note: dcp engineering confirmation that the leak was reportable was at 7:33 to dcp pipeline compliance. Dcp pipeline compliance called and reported it to the texas railroad commission at 8:30. Dcp has changed the time in part a, # 4.( earliest local time (24-hr clock) and date an accident reporting criteria was met: from 8:30 to 5:18 although the amount of the leak was not actually determined to be reportable until 7:33 and reported at 8:30. Changed by dwayne hillman @ request of PHMSA inspector alvaro rodriguez. Corrective action: on 8/10 - champion process came on site to install a ratchet add on in order to open the door to check for ovality. Once on site, the tech discovered that the door was very far out of alignment and adjusted the door to be in alignment. Once the door was aligned, the ratchet add on was installed and the door is able to be opened and closed easily utilizing the add on. Mitigation: addition comments added 9/29/2020. Dcp operations made assessments on the sand hills ngl system in september and identified two additional gallop corporation closures like the one located at ramsey meter station. Dcp compliance verified with operations that no issues with those closures existed. The two identified closures were already equipped with the door ratchet assembly like the one installed by gallop corporation at ramsey after the accident. Dcp will also verify the ratchet assembly be included on any future purchases of alike gallop corporation closures from champion in the future.
Detailed record list
Report Received Date
2020-08-18 00:00:00
Iyear
2020
Report Number
20200231
Supplemental Number
34470
Report Type
Supplemental Final
Operator Id
Name
Dcp Midstream
Operator Street Address
2331 Citywest Blvd. Hq-08-S812-02
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77042
Local Datetime
2020-07-18 05:18:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
0.53
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Controller
Operator Type
Operator Employee
Incident Identified Datetime
2020-07-18 05:18:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2020-07-18 05:18:00
Restart Datetime
2020-07-18 06:50:00
On Site Datetime
2020-07-18 06:23:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Ramsey Meter Station
Segment Name
Mg-1-2
Onshore State Abbreviation
Tx
Onshore Postal Code
79770
Onshore City Name
Not Within A Municipality
Onshore County Name
Reeves
Designated Location
Milepost/valve Station
Designated Name
Meter Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Other
Incident Area Details
Filter Door
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Other
Item Involved Details
Inlet Filter
Installation Year
2018
Material Involved
Material Other Than Carbon Steel
Material Details
O-Ring
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
10
Est Cost Prop Damage
15000
Est Cost Emergency
500
Est Cost Environmental
0
Est Cost Other
0
Prpty
15510
Accident Psig
1096
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
Yes
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controller notified dcp weekend on call tech as soon as the controller received alarm indicating the station shut down due to gas detection alarm. Field employee responded to the meter station to identify and confirm.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Failure Details
The 30" Door On The Filter Casing Was Misaligned Causing The Door To Pinch The O-Ring When Closed. Investigation Determined The Hinges On The Door Were Out Of Alignment Causing The Door To Pinch The O-Ring When Closed After Filter Change In May 2020. The Door Did Not Leak When Placed Back In Service At The Time The Filter Change. The Failure Occurred 7 Weeks Later On July 17, 2020.
Ief Addl Misalignment Ind
Yes
Preparer Name
D***** H******
Preparer Title
Principal Pipeline Compliance Specialist
Preparer Email
H******@d***********.com
Preparer Telephone
432-556-9473
Prepared Date
2020-11-03 00:00:00
Authorizer Name
J*** P*******
Authorizer Telephone
405-605-3859
Authorizer Title
Manager Pipeline Compliance
Authorizer Email
J*********@d***********.com
Narrative
N****************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************@ request of PHMSA inspector alvaro rodriguez. Corrective action: on 8/10 - champion process came on site to install a ratchet add on in order to open the door to check for ovality. Once on site, the tech discovered that the door was very far out of alignment and adjusted the door to be in alignment. Once the door was aligned, the ratchet add on was installed and the door is able to be opened and closed easily utilizing the add on. Mitigation: addition comments added 9/29/2020. Dcp operations made assessments on the sand hills ngl system in september and identified two additional gallop corporation closures like the one located at ramsey meter station. Dcp compliance verified with operations that no issues with those closures existed. The two identified closures were already equipped with the door ratchet assembly like the one installed by gallop corporation at ramsey after the accident. **********************************************************************************************************************************************.
Report Received Date 2020-08-18 00:00:00
Iyear 2020
Report Number 20200231
Supplemental Number 34470
Report Type Supplemental Final
Operator Id 31130 PHMSA Enforcement
Name Dcp Midstream
Operator Street Address 2331 Citywest Blvd. Hq-08-S812-02
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77042
Local Datetime 2020-07-18 05:18:00
Location Latitude 31.92409 Google Maps OpenStreetMap
Location Longitude -104.01934 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 0.53
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Controller
Operator Type Operator Employee
Incident Identified Datetime 2020-07-18 05:18:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2020-07-18 05:18:00
Restart Datetime 2020-07-18 06:50:00
On Site Datetime 2020-07-18 06:23:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Ramsey Meter Station
Segment Name Mg-1-2
Onshore State Abbreviation Tx
Onshore Postal Code 79770
Onshore City Name Not Within A Municipality
Onshore County Name Reeves
Designated Location Milepost/valve Station
Designated Name Meter Station
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Other
Incident Area Details Filter Door
Crossing No
Pipe Facility Type Intrastate
Item Involved Other
Item Involved Details Inlet Filter
Installation Year 2018
Material Involved Material Other Than Carbon Steel
Material Details O-Ring
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 10
Est Cost Prop Damage 15000
Est Cost Emergency 500
Est Cost Environmental 0
Est Cost Other 0
Prpty 15510
Accident Psig 1096
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind Yes
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Controller notified dcp weekend on call tech as soon as the controller received alarm indicating the station shut down due to gas detection alarm. Field employee responded to the meter station to identify and confirm.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Other Equipment Failure
Eq Failure Type Other Equipment Failure
Failure Details The 30" Door On The Filter Casing Was Misaligned Causing The Door To Pinch The O-Ring When Closed. Investigation Determined The Hinges On The Door Were Out Of Alignment Causing The Door To Pinch The O-Ring When Closed After Filter Change In May 2020. The Door Did Not Leak When Placed Back In Service At The Time The Filter Change. The Failure Occurred 7 Weeks Later On July 17, 2020.
Ief Addl Misalignment Ind Yes
Preparer Name D***** H******
Preparer Title Principal Pipeline Compliance Specialist
Preparer Email H******@d***********.com
Preparer Telephone 432-556-9473
Prepared Date 2020-11-03 00:00:00
Authorizer Name J*** P*******
Authorizer Telephone 405-605-3859
Authorizer Title Manager Pipeline Compliance
Authorizer Email J*********@d***********.com
Narrative N****************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************@ request of PHMSA inspector alvaro rodriguez. Corrective action: on 8/10 - champion process came on site to install a ratchet add on in order to open the door to check for ovality. Once on site, the tech discovered that the door was very far out of alignment and adjusted the door to be in alignment. Once the door was aligned, the ratchet add on was installed and the door is able to be opened and closed easily utilizing the add on. Mitigation: addition comments added 9/29/2020. Dcp operations made assessments on the sand hills ngl system in september and identified two additional gallop corporation closures like the one located at ramsey meter station. Dcp compliance verified with operations that no issues with those closures existed. The two identified closures were already equipped with the door ratchet assembly like the one installed by gallop corporation at ramsey after the accident. **********************************************************************************************************************************************.

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