HL incident on 2020-07-17 — TX

Operator
Enterprise Crude Pipeline Llc
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$200,000
Incident datetime
2020-07-17 07:45
Report number
Location
TX
Narrative
On 7/17/2020 at 7:45ct, an enterprise technician discovered oil inside a valve vault at cedar pump station. The section of pipe was isolated and a vacuum truck was used to remove free standing oil from the vault. After hydroexcavation, operations determined the oil was coming from the body bleed of an underground 24" valve. At 21:12 ct on 07/18/2020, the nrc was notified due to valve repair costs exceeding $50k. The valve was replaced on 7/24/2020 and the line was returned to service on 7/25/2020. An estimated 25 barrels of crude oil leaked from the valve. Upon investigation, it was determined that the leak was caused by internal corrosion. To prevent reoccurrence, operations and corrosion groups have developed and implemented a flush plan for the facility. Nrc#:1282280 on 07/18/2020, 21:21ct nrc 48hr #:1282366 on 07/20/2020, 11:40ct
Detailed record list
Report Received Date
2020-08-12 00:00:00
Iyear
2020
Report Number
20200229
Supplemental Number
34545
Report Type
Supplemental Final
Operator Id
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2020-07-18 20:57:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
25
Recovered Bbls
25
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2020-07-17 07:45:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Line Was Down Due Maintenance Activities.
On Site Datetime
2020-07-17 07:45:00
Nrc Rpt Datetime
2020-07-18 21:12:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
S1/cedar Station
Segment Name
Txxx0161
Onshore State Abbreviation
Tx
Onshore Postal Code
75838
Onshore City Name
Teague
Onshore County Name
Freestone
Designated Location
Milepost/valve Station
Designated Name
Mp 319.792
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
61
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Mainline
Valve Mainline Type
Gate
Valve Manufacturer
Wkm
Installation Year
1996
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
1250
Est Cost Prop Damage
200000
Est Cost Emergency
150000
Est Cost Environmental
50000
Est Cost Other
0
Prpty
401250
Accident Psig
263
Mop Psig
899
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Low leak volume.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Not Cut Open
Int Water Acid Ind
Yes
Int Field Exam Basis Ind
Yes
Int Other Basis Ind
Yes
Int Corrosion Basis Details
Ut Measurements
Int Other Loc Ind
Yes
Corrosion Location Details
Bottom Of Valve Body
Corrosion Inhibitors
Yes
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Yes
Preparer Name
R*** T********
Preparer Title
Engineer Pipeline Compliance
Preparer Email
R*********@e****.com
Preparer Telephone
7133814659
Prepared Date
2020-11-18 00:00:00
Authorizer Name
S**** D****
Authorizer Telephone
7133815855
Authorizer Title
Manager Compliance
Authorizer Email
S******@e****.com
Narrative
On 7/17/2020 at 7:45ct, an enterprise technician discovered oil inside a valve vault at cedar pump station. The section of pipe was isolated and a vacuum truck was used to remove free standing oil from the vault. After hydroexcavation, operations determined the oil was coming from the body bleed of an underground 24" valve. At 21:12 ct on 07/18/2020, the nrc was notified due to valve repair costs exceeding $50k. The valve was replaced on 7/24/2020 and the line was returned to service on 7/25/2020. An estimated 25 barrels of crude oil leaked from the valve. Upon investigation, it was determined that the leak was caused by internal corrosion. To prevent reoccurrence, operations and corrosion groups have developed and implemented a flush plan for the facility. Nrc#:1282280 on 07/18/2020, 21:21ct nrc 48hr #:1282366 on 07/20/2020, 11:40ct
Report Received Date 2020-08-12 00:00:00
Iyear 2020
Report Number 20200229
Supplemental Number 34545
Report Type Supplemental Final
Operator Id 30829 PHMSA Enforcement
Name Enterprise Crude Pipeline Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2020-07-18 20:57:00
Location Latitude 31.532208 Google Maps OpenStreetMap
Location Longitude -96.185686 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 25
Recovered Bbls 25
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2020-07-17 07:45:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Line Was Down Due Maintenance Activities.
On Site Datetime 2020-07-17 07:45:00
Nrc Rpt Datetime 2020-07-18 21:12:00
Nrc Rpt Num 1282280 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name S1/cedar Station
Segment Name Txxx0161
Onshore State Abbreviation Tx
Onshore Postal Code 75838
Onshore City Name Teague
Onshore County Name Freestone
Designated Location Milepost/valve Station
Designated Name Mp 319.792
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 61
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Mainline
Valve Mainline Type Gate
Valve Manufacturer Wkm
Installation Year 1996
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 1250
Est Cost Prop Damage 200000
Est Cost Emergency 150000
Est Cost Environmental 50000
Est Cost Other 0
Prpty 401250
Accident Psig 263
Mop Psig 899
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Low leak volume.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Not Cut Open
Int Water Acid Ind Yes
Int Field Exam Basis Ind Yes
Int Other Basis Ind Yes
Int Corrosion Basis Details Ut Measurements
Int Other Loc Ind Yes
Corrosion Location Details Bottom Of Valve Body
Corrosion Inhibitors Yes
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Yes
Preparer Name R*** T********
Preparer Title Engineer Pipeline Compliance
Preparer Email R*********@e****.com
Preparer Telephone 7133814659
Prepared Date 2020-11-18 00:00:00
Authorizer Name S**** D****
Authorizer Telephone 7133815855
Authorizer Title Manager Compliance
Authorizer Email S******@e****.com
Narrative On 7/17/2020 at 7:45ct, an enterprise technician discovered oil inside a valve vault at cedar pump station. The section of pipe was isolated and a vacuum truck was used to remove free standing oil from the vault. After hydroexcavation, operations determined the oil was coming from the body bleed of an underground 24" valve. At 21:12 ct on 07/18/2020, the nrc was notified due to valve repair costs exceeding $50k. The valve was replaced on 7/24/2020 and the line was returned to service on 7/25/2020. An estimated 25 barrels of crude oil leaked from the valve. Upon investigation, it was determined that the leak was caused by internal corrosion. To prevent reoccurrence, operations and corrosion groups have developed and implemented a flush plan for the facility. Nrc#:1282280 on 07/18/2020, 21:21ct nrc 48hr #:1282366 on 07/20/2020, 11:40ct

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