HL incident on 2020-07-13 — TX

Operator
Enterprise Crude Pipeline Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$30,000
Incident datetime
2020-07-13 10:15
Report number
Location
TX
Narrative
On 7/13/2020 at 10:15ct, an enterprise pipeline technician identified an oil sheen around mov-a005, the bypass valve for the seaway 1 scraper trap. A hydroexcavation truck was called to the site to expose the underground valve. Once the valve was exposed, it was determined that its bonnet was leaking. An estimated 1 quart of oil was released. The valve was then isolated and its bonnet wrapped in absorbent pads to prevent additional contamination. On 7/15/2020 at 08:30ct it was determined that repair and cleanup costs for the leak would exceed $50k. Upon investigation, it was determined that failure of the valve's o-ring to completely seal caused the leak. For repair, the o-ring was replaced and flange faces on the valve body and bonnet were resurfaced to ensure a seal. Cause of the o-ring failure is undeterminable. Cleanup & repairs are complete and the valve has been placed back into service. No offsite impacts. Nrc: #1281937 at 7/15/2020 08:45ct nrc 48 hour: #1282096 on 7/16/2020 14:11ct
Detailed record list
Report Received Date
2020-08-12 00:00:00
Iyear
2020
Report Number
20200228
Supplemental Number
34261
Report Type
Supplemental Final
Operator Id
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2020-07-13 10:15:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.1
Recovered Bbls
0.1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2020-07-13 10:15:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Line Was Down Due To Scheduling.
On Site Datetime
2020-07-13 10:15:00
Nrc Rpt Datetime
2020-07-15 08:45:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Cushing East
Segment Name
Okxx1056
Onshore State Abbreviation
Ok
Onshore Postal Code
74023
Onshore City Name
Cushing
Onshore County Name
Payne
Designated Location
Milepost/valve Station
Designated Name
Mp 0.0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
102
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Mainline
Valve Mainline Type
Gate
Valve Manufacturer
Wkm
Installation Year
1995
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
1
Est Cost Prop Damage
30000
Est Cost Emergency
65000
Est Cost Environmental
5000
Est Cost Other
0
Prpty
100001
Accident Psig
254
Mop Psig
701
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Leak volume not significant.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
O-Ring
Eq Additional Other Ind
Yes
Eq Additional Other Details
Unable To Determine.
Preparer Name
R*** T********
Preparer Title
Engineer Pipeline Compliance
Preparer Email
R*********@e****.com
Preparer Telephone
713-381-4659
Prepared Date
2020-09-11 00:00:00
Authorizer Name
S**** D****
Authorizer Telephone
713-381-5585
Authorizer Title
Manager Compliance
Authorizer Email
S******@e****.com
Narrative
On 7/13/2020 at 10:15ct, an enterprise pipeline technician identified an oil sheen around mov-a005, the bypass valve for the seaway 1 scraper trap. A hydroexcavation truck was called to the site to expose the underground valve. Once the valve was exposed, it was determined that its bonnet was leaking. An estimated 1 quart of oil was released. The valve was then isolated and its bonnet wrapped in absorbent pads to prevent additional contamination. On 7/15/2020 at 08:30ct it was determined that repair and cleanup costs for the leak would exceed $50k. Upon investigation, it was determined that failure of the valve's o-ring to completely seal caused the leak. For repair, the o-ring was replaced and flange faces on the valve body and bonnet were resurfaced to ensure a seal. Cause of the o-ring failure is undeterminable. Cleanup & repairs are complete and the valve has been placed back into service. No offsite impacts. Nrc: #1281937 at 7/15/2020 08:45ct nrc 48 hour: #1282096 on 7/16/2020 14:11ct
Report Received Date 2020-08-12 00:00:00
Iyear 2020
Report Number 20200228
Supplemental Number 34261
Report Type Supplemental Final
Operator Id 30829 PHMSA Enforcement
Name Enterprise Crude Pipeline Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2020-07-13 10:15:00
Location Latitude 35.94075 Google Maps OpenStreetMap
Location Longitude -96.74893 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.1
Recovered Bbls 0.1
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2020-07-13 10:15:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Line Was Down Due To Scheduling.
On Site Datetime 2020-07-13 10:15:00
Nrc Rpt Datetime 2020-07-15 08:45:00
Nrc Rpt Num 1281937 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Cushing East
Segment Name Okxx1056
Onshore State Abbreviation Ok
Onshore Postal Code 74023
Onshore City Name Cushing
Onshore County Name Payne
Designated Location Milepost/valve Station
Designated Name Mp 0.0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 102
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Mainline
Valve Mainline Type Gate
Valve Manufacturer Wkm
Installation Year 1995
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 1
Est Cost Prop Damage 30000
Est Cost Emergency 65000
Est Cost Environmental 5000
Est Cost Other 0
Prpty 100001
Accident Psig 254
Mop Psig 701
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Leak volume not significant.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind O-Ring
Eq Additional Other Ind Yes
Eq Additional Other Details Unable To Determine.
Preparer Name R*** T********
Preparer Title Engineer Pipeline Compliance
Preparer Email R*********@e****.com
Preparer Telephone 713-381-4659
Prepared Date 2020-09-11 00:00:00
Authorizer Name S**** D****
Authorizer Telephone 713-381-5585
Authorizer Title Manager Compliance
Authorizer Email S******@e****.com
Narrative On 7/13/2020 at 10:15ct, an enterprise pipeline technician identified an oil sheen around mov-a005, the bypass valve for the seaway 1 scraper trap. A hydroexcavation truck was called to the site to expose the underground valve. Once the valve was exposed, it was determined that its bonnet was leaking. An estimated 1 quart of oil was released. The valve was then isolated and its bonnet wrapped in absorbent pads to prevent additional contamination. On 7/15/2020 at 08:30ct it was determined that repair and cleanup costs for the leak would exceed $50k. Upon investigation, it was determined that failure of the valve's o-ring to completely seal caused the leak. For repair, the o-ring was replaced and flange faces on the valve body and bonnet were resurfaced to ensure a seal. Cause of the o-ring failure is undeterminable. Cleanup & repairs are complete and the valve has been placed back into service. No offsite impacts. Nrc: #1281937 at 7/15/2020 08:45ct nrc 48 hour: #1282096 on 7/16/2020 14:11ct

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