Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2020-07-06 — TX
Operator
Enterprise Products Operating Llc
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$0
Incident datetime
2020-07-06 05:15
Report number
Location
TX
Narrative
At approximately 0515 cdt on 07/06/2020 during rounds, an enterprise technician discovered a 1/2" drain on a 10" valve on an incoming gasoline header leaking. Approximately 5 bbls of gasoline was released. Spill was contained and site was remediated. Investigation determined that block and bleed assembly was most likely under torqued during original installation and had loosened during operation. To prevent recurrence all similar bleed assemblies within the facility have been replaced with properly torqued, solid, threaded plugs.
Detailed record list
Report Received Date
2020-08-05 00:00:00
Iyear
2020
Report Number
20200221
Supplemental Number
34608
Report Type
Supplemental Final
Operator Id
31618
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2020-07-06 05:15:00
Location Latitude
30.01081
Location Longitude
-94.05688
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
5
Recovered Bbls
5
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Ground Patrol By Operator Or Its Contractor
Operator Type
Operator Employee
Incident Identified Datetime
2020-07-06 05:15:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Valve Was Shut In And Product Was Rerouted Via Terminal Piping.
On Site Datetime
2020-07-06 05:15:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Beaumont Terminal
Segment Name
Header Valve
Onshore State Abbreviation
Tx
Onshore Postal Code
77705
Onshore City Name
Beaumont
Onshore County Name
Jefferson
Designated Location
Milepost/valve Station
Designated Name
Facility
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
2018
Material Involved
Material Other Than Carbon Steel
Material Details
Stainless Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
475
Est Cost Prop Damage
0
Est Cost Emergency
0
Est Cost Environmental
15000
Est Cost Other
0
Prpty
15475
Accident Psig
40
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Control room personnel did not contribute to accident cause.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Threaded Connection/coupling Failure
Eq Failure Type
Threaded Connection/coupling Failure
Other Stripped Ind
Threaded Fitting
Additional Installation Ind
Yes
Preparer Name
D**** B*****
Preparer Title
Pipeline Compliance Engineer
Preparer Email
D*******@e****.com
Preparer Telephone
7133815647
Prepared Date
2020-12-10 00:00:00
Authorizer Name
D**** B*****
Authorizer Telephone
7133815647
Authorizer Title
Pipeline Compliance Engineer
Authorizer Email
D*******@e****.com
Narrative
At approximately 0515 cdt on 07/06/2020 during rounds, an enterprise technician discovered a 1/2" drain on a 10" valve on an incoming gasoline header leaking. Approximately 5 bbls of gasoline was released. Spill was contained and site was remediated. Investigation determined that block and bleed assembly was most likely under torqued during original installation and had loosened during operation. To prevent recurrence all similar bleed assemblies within the facility have been replaced with properly torqued, solid, threaded plugs.
| Report Received Date | 2020-08-05 00:00:00 |
|---|---|
| Iyear | 2020 |
| Report Number | 20200221 |
| Supplemental Number | 34608 |
| Report Type | Supplemental Final |
| Operator Id | 31618 PHMSA Enforcement |
| Name | Enterprise Products Operating Llc |
| Operator Street Address | 1100 Louisiana Street |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77002 |
| Local Datetime | 2020-07-06 05:15:00 |
| Location Latitude | 30.01081 Google Maps OpenStreetMap |
| Location Longitude | -94.05688 Google Maps OpenStreetMap |
| Commodity Released Type | Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions |
| Commodity Subtype | Gasoline (Non-Ethanol) |
| Unintentional Release Bbls | 5 |
| Recovered Bbls | 5 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Ground Patrol By Operator Or Its Contractor |
| Operator Type | Operator Employee |
| Incident Identified Datetime | 2020-07-06 05:15:00 |
| System Part Involved | Onshore Terminal/tank Farm Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | No |
| Shutdown Explain | Valve Was Shut In And Product Was Rerouted Via Terminal Piping. |
| On Site Datetime | 2020-07-06 05:15:00 |
| Nrc Rpt Num | Nrc Notification Not Required NRC Report How to search |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Beaumont Terminal |
| Segment Name | Header Valve |
| Onshore State Abbreviation | Tx |
| Onshore Postal Code | 77705 |
| Onshore City Name | Beaumont |
| Onshore County Name | Jefferson |
| Designated Location | Milepost/valve Station |
| Designated Name | Facility |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Incident Area Subtype | Typical Aboveground Facility Piping Or Appurtenance |
| Crossing | No |
| Pipe Facility Type | Interstate |
| Item Involved | Valve |
| Valve Type | Auxiliary Or Other Valve |
| Installation Year | 2018 |
| Material Involved | Material Other Than Carbon Steel |
| Material Details | Stainless Steel |
| Release Type | Leak |
| Leak Type | Connection Failure |
| Wildlife Impact Ind | No |
| Soil Contamination | Yes |
| Long Term Assessment | Yes |
| Remediation Ind | No |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | Yes |
| High Pop Ind | Yes |
| High Pop Yes No | Yes |
| Usa Drinking Ind | Yes |
| Usa Drinking Yes No | Yes |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 475 |
| Est Cost Prop Damage | 0 |
| Est Cost Emergency | 0 |
| Est Cost Environmental | 15000 |
| Est Cost Other | 0 |
| Prpty | 15475 |
| Accident Psig | 40 |
| Mop Psig | 285 |
| Accident Pressure | Pressure Did Not Exceed Mop |
| Pressure Restriction Ind | No |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Scada In Place Ind | Yes |
| Scada Operating Ind | Yes |
| Scada Functional Ind | Yes |
| Scada Detection Ind | No |
| Scada Conf Ind | No |
| Cpm In Place Ind | No |
| Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
| Investigation Status Details | Control room personnel did not contribute to accident cause. |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Threaded Connection/coupling Failure |
| Eq Failure Type | Threaded Connection/coupling Failure |
| Other Stripped Ind | Threaded Fitting |
| Additional Installation Ind | Yes |
| Preparer Name | D**** B***** |
| Preparer Title | Pipeline Compliance Engineer |
| Preparer Email | D*******@e****.com |
| Preparer Telephone | 7133815647 |
| Prepared Date | 2020-12-10 00:00:00 |
| Authorizer Name | D**** B***** |
| Authorizer Telephone | 7133815647 |
| Authorizer Title | Pipeline Compliance Engineer |
| Authorizer Email | D*******@e****.com |
| Narrative | At approximately 0515 cdt on 07/06/2020 during rounds, an enterprise technician discovered a 1/2" drain on a 10" valve on an incoming gasoline header leaking. Approximately 5 bbls of gasoline was released. Spill was contained and site was remediated. Investigation determined that block and bleed assembly was most likely under torqued during original installation and had loosened during operation. To prevent recurrence all similar bleed assemblies within the facility have been replaced with properly torqued, solid, threaded plugs. |
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