HL incident on 2020-06-30 — TX

Operator
Nustar Permian Transportation And Storage, Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,500
Incident datetime
2020-06-30 13:15
Report number
Location
TX
Narrative
While conducting an avo at glasscock truck station, an operator on site discovered that the seal on booster pump 401 had failed. The operator isolated the pump and made all proper notifications. The release was contained within the tank dike. The pump was locked out and repaired. The pump was filled, tested, inspected, and put back in service. The cause of the mechanical seal failure is under investigation. Update: 8/26/20-the plastic retainer in the thrust bearing failed causing seal to fail.
Detailed record list
Report Received Date
2020-07-29 00:00:00
Iyear
2020
Report Number
20200216
Supplemental Number
34362
Report Type
Supplemental Final
Operator Id
Name
Nustar Permian Transportation And Storage, Llc
Operator Street Address
8111 Westchester Drive
Operator City Name
Dallas
Operator State Abbreviation
TX
Operator Postal Code
75225
Local Datetime
2020-06-30 13:15:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
60.5
Recovered Bbls
2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2020-06-30 13:15:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
The Line Was Already Shutdown When Discovered.
On Site Datetime
2020-06-30 13:15:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
104p South Mainline Pipeline System
Segment Name
Glasscock Terminal
Onshore State Abbreviation
Tx
Onshore Postal Code
79739
Onshore City Name
Not Within A Municipality
Onshore County Name
Glasscock
Designated Location
Survey Station No.
Designated Name
0+00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pump
Installation Year
2016
Material Involved
Material Other Than Carbon Steel
Material Details
Pump Seal
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
2277
Est Cost Prop Damage
1500
Est Cost Emergency
0
Est Cost Environmental
44907
Est Cost Other
0
Prpty
48684
Accident Psig
6
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Neither control room nor controller activities contributed to the accident. Please see part g and h of this report.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Other Pump Ind
Seal/packing Failure
Eq Additional Other Ind
Yes
Eq Additional Other Details
Thrust Bearing Failure
Preparer Name
A***** R********
Preparer Title
Manager Pipeline Safety
Preparer Email
A***************@n***********.com
Preparer Telephone
806-336-0712
Prepared Date
2020-10-12 00:00:00
Authorizer Name
J**** R********
Authorizer Telephone
8063711304
Authorizer Title
General Manager Pipeline And Terminal Operations
Authorizer Email
J**************@n***********.com
Narrative
While conducting an avo at glasscock truck station, an operator on site discovered that the seal on booster pump 401 had failed. The operator isolated the pump and made all proper notifications. The release was contained within the tank dike. The pump was locked out and repaired. The pump was filled, tested, inspected, and put back in service. The cause of the mechanical seal failure is under investigation. Update: 8/26/20-the plastic retainer in the thrust bearing failed causing seal to fail.
Report Received Date 2020-07-29 00:00:00
Iyear 2020
Report Number 20200216
Supplemental Number 34362
Report Type Supplemental Final
Operator Id 39348 PHMSA Enforcement
Name Nustar Permian Transportation And Storage, Llc
Operator Street Address 8111 Westchester Drive
Operator City Name Dallas
Operator State Abbreviation TX
Operator Postal Code 75225
Local Datetime 2020-06-30 13:15:00
Location Latitude 31.86421 Google Maps OpenStreetMap
Location Longitude -101.5544 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 60.5
Recovered Bbls 2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2020-06-30 13:15:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain The Line Was Already Shutdown When Discovered.
On Site Datetime 2020-06-30 13:15:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name 104p South Mainline Pipeline System
Segment Name Glasscock Terminal
Onshore State Abbreviation Tx
Onshore Postal Code 79739
Onshore City Name Not Within A Municipality
Onshore County Name Glasscock
Designated Location Survey Station No.
Designated Name 0+00
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Pump
Installation Year 2016
Material Involved Material Other Than Carbon Steel
Material Details Pump Seal
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 2277
Est Cost Prop Damage 1500
Est Cost Emergency 0
Est Cost Environmental 44907
Est Cost Other 0
Prpty 48684
Accident Psig 6
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Neither control room nor controller activities contributed to the accident. Please see part g and h of this report.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Pump Or Pump-Related Equipment
Eq Failure Type Pump Or Pump-Related Equipment
Other Pump Ind Seal/packing Failure
Eq Additional Other Ind Yes
Eq Additional Other Details Thrust Bearing Failure
Preparer Name A***** R********
Preparer Title Manager Pipeline Safety
Preparer Email A***************@n***********.com
Preparer Telephone 806-336-0712
Prepared Date 2020-10-12 00:00:00
Authorizer Name J**** R********
Authorizer Telephone 8063711304
Authorizer Title General Manager Pipeline And Terminal Operations
Authorizer Email J**************@n***********.com
Narrative While conducting an avo at glasscock truck station, an operator on site discovered that the seal on booster pump 401 had failed. The operator isolated the pump and made all proper notifications. The release was contained within the tank dike. The pump was locked out and repaired. The pump was filled, tested, inspected, and put back in service. The cause of the mechanical seal failure is under investigation. Update: 8/26/20-the plastic retainer in the thrust bearing failed causing seal to fail.

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