Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2020-06-24 — TX
Operator
Phillips 66 Pipeline Llc
Cause
Other Accident Cause
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$15,000
Incident datetime
2020-06-24 14:30
Report number
Location
TX
Narrative
On 6-24-2020, a third party line flyer identified and notified p66 of dead vegetation over the bl-01 pipeline near madison, ks. P66 responded, hand excavated and confirmed lel readings indicating a release at app. 14:30 and the line was shutdown. Pipeline was further excavated and clamp installed over a failed puddle weld repair on 6-25-2020. Line was restarted without incident at app. 16:57. 2020-8-19 - corrected part b, item #5 from coffey co. To greenwood co.
Detailed record list
Report Received Date
2020-07-22 00:00:00
Iyear
2020
Report Number
20200211
Supplemental Number
34163
Report Type
Supplemental Final
Operator Id
31684
Name
Phillips 66 Pipeline Llc
Operator Street Address
2331 Citywest Blvd
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77042
Local Datetime
2020-06-24 14:30:00
Location Latitude
38.134175
Location Longitude
-96.171873
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Butane
Unintentional Release Bbls
0.25
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Air Patrol
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2020-06-24 14:30:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2020-06-24 14:33:00
Restart Datetime
2020-06-25 16:57:00
On Site Datetime
2020-06-24 14:30:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Automatic
Downstream Valve Type Ind
Automatic
Num Pub Evacuated
0
Pipe Fac Name
Bl-01
Segment Name
Cassoday To Sharpe
Onshore State Abbreviation
Ks
Onshore Postal Code
66860
Onshore City Name
Not Within A Municipality
Onshore County Name
Greenwood
Designated Location
Milepost/valve Station
Designated Name
Mp 340.5
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
42
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Other
Item Involved Details
Puddle Weld
Installation Year
1952
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
750
Est Cost Gas Released
6
Est Cost Prop Damage
15000
Est Cost Emergency
2500
Est Cost Environmental
0
Est Cost Other
0
Prpty
18256
Accident Psig
508
Mop Psig
1087
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
246197
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Leak cause was not associated with any operational issues or concerns
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Accident Cause
Cause Details
Miscellaneous
Other Type
Miscellaneous
Misc Details
Puddle Weld Crack.
Preparer Name
J*** B*********
Preparer Title
Dot Coordinator
Preparer Email
J****************@p**.com
Preparer Telephone
580-767-4206
Prepared Date
2020-08-19 00:00:00
Authorizer Name
T*** F****
Authorizer Telephone
832-765-1632
Authorizer Title
Dot Director
Authorizer Email
T***********@p**.com
Narrative
On 6-24-2020, a third party line flyer identified and notified p66 of dead vegetation over the bl-01 pipeline near madison, ks. P66 responded, hand excavated and confirmed lel readings indicating a release at app. 14:30 and the line was shutdown. Pipeline was further excavated and clamp installed over a failed puddle weld repair on 6-25-2020. Line was restarted without incident at app. 16:57. 2020-8-19 - corrected part b, item #5 from coffey co. To greenwood co.
| Report Received Date | 2020-07-22 00:00:00 |
|---|---|
| Iyear | 2020 |
| Report Number | 20200211 |
| Supplemental Number | 34163 |
| Report Type | Supplemental Final |
| Operator Id | 31684 PHMSA Enforcement |
| Name | Phillips 66 Pipeline Llc |
| Operator Street Address | 2331 Citywest Blvd |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77042 |
| Local Datetime | 2020-06-24 14:30:00 |
| Location Latitude | 38.134175 Google Maps OpenStreetMap |
| Location Longitude | -96.171873 Google Maps OpenStreetMap |
| Commodity Released Type | Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions |
| Commodity Subtype | Other Hvl |
| Commodity Details | Butane |
| Unintentional Release Bbls | 0.25 |
| Intentional Release Bbls | 0 |
| Recovered Bbls | 0 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Air Patrol |
| Operator Type | Contractor Working For The Operator |
| Incident Identified Datetime | 2020-06-24 14:30:00 |
| System Part Involved | Onshore Pipeline, Including Valve Sites |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | Yes |
| Shutdown Datetime | 2020-06-24 14:33:00 |
| Restart Datetime | 2020-06-25 16:57:00 |
| On Site Datetime | 2020-06-24 14:30:00 |
| Nrc Rpt Num | Nrc Notification Not Required NRC Report How to search |
| Ignite Ind | No |
| Explode Ind | No |
| Upstream Valve Type Ind | Automatic |
| Downstream Valve Type Ind | Automatic |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Bl-01 |
| Segment Name | Cassoday To Sharpe |
| Onshore State Abbreviation | Ks |
| Onshore Postal Code | 66860 |
| Onshore City Name | Not Within A Municipality |
| Onshore County Name | Greenwood |
| Designated Location | Milepost/valve Station |
| Designated Name | Mp 340.5 |
| Federal | No |
| Location Type | Pipeline Right-Of-Way |
| Incident Area Type | Underground |
| Incident Area Subtype | Under Soil |
| Depth Of Cover | 42 |
| Crossing | No |
| Pipe Facility Type | Interstate |
| Item Involved | Other |
| Item Involved Details | Puddle Weld |
| Installation Year | 1952 |
| Material Involved | Carbon Steel |
| Release Type | Leak |
| Leak Type | Crack |
| Wildlife Impact Ind | No |
| Soil Contamination | No |
| Long Term Assessment | No |
| Remediation Ind | No |
| Water Contam Ind | No |
| Could Be Hca | No |
| Commodity Reached Hca | Yes |
| Usa Drinking Ind | Yes |
| Usa Drinking Yes No | Yes |
| Est Cost Oper Paid | 750 |
| Est Cost Gas Released | 6 |
| Est Cost Prop Damage | 15000 |
| Est Cost Emergency | 2500 |
| Est Cost Environmental | 0 |
| Est Cost Other | 0 |
| Prpty | 18256 |
| Accident Psig | 508 |
| Mop Psig | 1087 |
| Accident Pressure | Pressure Did Not Exceed Mop |
| Pressure Restriction Ind | No |
| Length Segment Isolated | 246197 |
| Internal Inspection Ind | Yes |
| Operation Complications Ind | No |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Scada In Place Ind | Yes |
| Scada Operating Ind | Yes |
| Scada Functional Ind | Yes |
| Scada Detection Ind | No |
| Scada Conf Ind | No |
| Cpm In Place Ind | Yes |
| Cpm Operating Ind | Yes |
| Cpm Functional Ind | Yes |
| Cpm Detection Ind | No |
| Cpm Conf Ind | No |
| Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
| Investigation Status Details | Leak cause was not associated with any operational issues or concerns |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Other Accident Cause |
| Cause Details | Miscellaneous |
| Other Type | Miscellaneous |
| Misc Details | Puddle Weld Crack. |
| Preparer Name | J*** B********* |
| Preparer Title | Dot Coordinator |
| Preparer Email | J****************@p**.com |
| Preparer Telephone | 580-767-4206 |
| Prepared Date | 2020-08-19 00:00:00 |
| Authorizer Name | T*** F**** |
| Authorizer Telephone | 832-765-1632 |
| Authorizer Title | Dot Director |
| Authorizer Email | T***********@p**.com |
| Narrative | On 6-24-2020, a third party line flyer identified and notified p66 of dead vegetation over the bl-01 pipeline near madison, ks. P66 responded, hand excavated and confirmed lel readings indicating a release at app. 14:30 and the line was shutdown. Pipeline was further excavated and clamp installed over a failed puddle weld repair on 6-25-2020. Line was restarted without incident at app. 16:57. 2020-8-19 - corrected part b, item #5 from coffey co. To greenwood co. |
External Resources
PHMSA pipeline safety insights.
Product
Features
Company
All rights reserved. Copyright © by ClearPHMSA