HL incident on 2020-06-24 — TX

Operator
Phillips 66 Pipeline Llc
Cause
Other Accident Cause
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$15,000
Incident datetime
2020-06-24 14:30
Report number
Location
TX
Narrative
On 6-24-2020, a third party line flyer identified and notified p66 of dead vegetation over the bl-01 pipeline near madison, ks. P66 responded, hand excavated and confirmed lel readings indicating a release at app. 14:30 and the line was shutdown. Pipeline was further excavated and clamp installed over a failed puddle weld repair on 6-25-2020. Line was restarted without incident at app. 16:57. 2020-8-19 - corrected part b, item #5 from coffey co. To greenwood co.
Detailed record list
Report Received Date
2020-07-22 00:00:00
Iyear
2020
Report Number
20200211
Supplemental Number
34163
Report Type
Supplemental Final
Operator Id
Name
Phillips 66 Pipeline Llc
Operator Street Address
2331 Citywest Blvd
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77042
Local Datetime
2020-06-24 14:30:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Butane
Unintentional Release Bbls
0.25
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Air Patrol
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2020-06-24 14:30:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2020-06-24 14:33:00
Restart Datetime
2020-06-25 16:57:00
On Site Datetime
2020-06-24 14:30:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Automatic
Downstream Valve Type Ind
Automatic
Num Pub Evacuated
0
Pipe Fac Name
Bl-01
Segment Name
Cassoday To Sharpe
Onshore State Abbreviation
Ks
Onshore Postal Code
66860
Onshore City Name
Not Within A Municipality
Onshore County Name
Greenwood
Designated Location
Milepost/valve Station
Designated Name
Mp 340.5
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
42
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Other
Item Involved Details
Puddle Weld
Installation Year
1952
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
750
Est Cost Gas Released
6
Est Cost Prop Damage
15000
Est Cost Emergency
2500
Est Cost Environmental
0
Est Cost Other
0
Prpty
18256
Accident Psig
508
Mop Psig
1087
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
246197
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Leak cause was not associated with any operational issues or concerns
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Accident Cause
Cause Details
Miscellaneous
Other Type
Miscellaneous
Misc Details
Puddle Weld Crack.
Preparer Name
J*** B*********
Preparer Title
Dot Coordinator
Preparer Email
J****************@p**.com
Preparer Telephone
580-767-4206
Prepared Date
2020-08-19 00:00:00
Authorizer Name
T*** F****
Authorizer Telephone
832-765-1632
Authorizer Title
Dot Director
Authorizer Email
T***********@p**.com
Narrative
On 6-24-2020, a third party line flyer identified and notified p66 of dead vegetation over the bl-01 pipeline near madison, ks. P66 responded, hand excavated and confirmed lel readings indicating a release at app. 14:30 and the line was shutdown. Pipeline was further excavated and clamp installed over a failed puddle weld repair on 6-25-2020. Line was restarted without incident at app. 16:57. 2020-8-19 - corrected part b, item #5 from coffey co. To greenwood co.
Report Received Date 2020-07-22 00:00:00
Iyear 2020
Report Number 20200211
Supplemental Number 34163
Report Type Supplemental Final
Operator Id 31684 PHMSA Enforcement
Name Phillips 66 Pipeline Llc
Operator Street Address 2331 Citywest Blvd
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77042
Local Datetime 2020-06-24 14:30:00
Location Latitude 38.134175 Google Maps OpenStreetMap
Location Longitude -96.171873 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Butane
Unintentional Release Bbls 0.25
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Air Patrol
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2020-06-24 14:30:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2020-06-24 14:33:00
Restart Datetime 2020-06-25 16:57:00
On Site Datetime 2020-06-24 14:30:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Automatic
Downstream Valve Type Ind Automatic
Num Pub Evacuated 0
Pipe Fac Name Bl-01
Segment Name Cassoday To Sharpe
Onshore State Abbreviation Ks
Onshore Postal Code 66860
Onshore City Name Not Within A Municipality
Onshore County Name Greenwood
Designated Location Milepost/valve Station
Designated Name Mp 340.5
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 42
Crossing No
Pipe Facility Type Interstate
Item Involved Other
Item Involved Details Puddle Weld
Installation Year 1952
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Est Cost Oper Paid 750
Est Cost Gas Released 6
Est Cost Prop Damage 15000
Est Cost Emergency 2500
Est Cost Environmental 0
Est Cost Other 0
Prpty 18256
Accident Psig 508
Mop Psig 1087
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 246197
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Leak cause was not associated with any operational issues or concerns
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Accident Cause
Cause Details Miscellaneous
Other Type Miscellaneous
Misc Details Puddle Weld Crack.
Preparer Name J*** B*********
Preparer Title Dot Coordinator
Preparer Email J****************@p**.com
Preparer Telephone 580-767-4206
Prepared Date 2020-08-19 00:00:00
Authorizer Name T*** F****
Authorizer Telephone 832-765-1632
Authorizer Title Dot Director
Authorizer Email T***********@p**.com
Narrative On 6-24-2020, a third party line flyer identified and notified p66 of dead vegetation over the bl-01 pipeline near madison, ks. P66 responded, hand excavated and confirmed lel readings indicating a release at app. 14:30 and the line was shutdown. Pipeline was further excavated and clamp installed over a failed puddle weld repair on 6-25-2020. Line was restarted without incident at app. 16:57. 2020-8-19 - corrected part b, item #5 from coffey co. To greenwood co.

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