HL incident on 2020-06-30 — OK

Operator
Oneok Ngl Pipeline, Llc
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,500
Incident datetime
2020-06-30 21:15
Report number
Location
OK
Narrative
On june 30th, 2020 at approximately 8:28 pm, oneok pipeline control center received a gas detect alarm for the oneok sterling ii groveton pump station. The gas detect alarm activated the station shutdown and isolated the pump station. Oneok pipeline control dispatched local field operations to the location. At approximately 9:15pm, the oneok field operator arrived on site and noticed vapors in the vicinity of the number 1 pump. Field operator isolated the pump and began evacuating hydrocarbons from the pump and associated piping at 9:25pm. After evacuation of hydrocarbons, a pinhole leak in the outboard bearing cooler return tubing was discovered as the source of the release. The affected tubing was found to be in contact with the outboard oil drain piping, resulting in a pinhole developing in the tubing, because of friction. The tubing was replaced and adjusted so not to contact the oil drain piping and the pump returned to service. Investigation into the cause of the release, determined the pump oil drain piping had inadvertently been installed in contact with the cooler inlet tubing during previous maintenance activities.
Detailed record list
Report Received Date
2020-07-20 00:00:00
Iyear
2020
Report Number
20200210
Supplemental Number
34054
Report Type
Original Final
Operator Id
Name
Oneok Ngl Pipeline, Llc
Operator Street Address
100 West Fifth Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2020-06-30 21:25:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
0.14
Intentional Release Bbls
9.86
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2020-06-30 21:15:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2020-06-30 20:28:00
Restart Datetime
2020-06-30 21:30:00
On Site Datetime
2020-06-30 21:15:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Groveton Sterling Ii Pump Station
Segment Name
Sterling Ii - Medford To Ombs 12in
Onshore State Abbreviation
Tx
Onshore Postal Code
75845
Onshore City Name
Not Within A Municipality
Onshore County Name
Trinity
Designated Location
Milepost/valve Station
Designated Name
Pump Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pump
Installation Year
2007
Material Involved
Material Other Than Carbon Steel
Material Details
Stainless Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
15
Est Cost Prop Damage
1500
Est Cost Emergency
150
Est Cost Environmental
0
Est Cost Other
750
Est Cost Other Details
Release Investigation
Prpty
2415
Accident Psig
766
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
There were no controller actions or control room issues
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Other Pump Ind
Other
Other Pump Details
1/2" Outboard Bearing Cooler Inlet Tubing
Eq Additional Other Ind
Yes
Eq Additional Other Details
Metal To Metal Friction
Preparer Name
M***** C********
Preparer Title
Regulatory Compliance Specialist
Preparer Email
M***************@o****.com
Preparer Telephone
2542928911
Prepared Date
2020-07-20 00:00:00
Authorizer Name
M***** C********
Authorizer Telephone
2542928911
Authorizer Title
Regulatory Compliance Specialist
Authorizer Email
M***************@o****.com
Narrative
On june 30th, 2020 at approximately 8:28 pm, oneok pipeline control center received a gas detect alarm for the oneok sterling ii groveton pump station. The gas detect alarm activated the station shutdown and isolated the pump station. Oneok pipeline control dispatched local field operations to the location. At approximately 9:15pm, the oneok field operator arrived on site and noticed vapors in the vicinity of the number 1 pump. Field operator isolated the pump and began evacuating hydrocarbons from the pump and associated piping at 9:25pm. After evacuation of hydrocarbons, a pinhole leak in the outboard bearing cooler return tubing was discovered as the source of the release. The affected tubing was found to be in contact with the outboard oil drain piping, resulting in a pinhole developing in the tubing, because of friction. The tubing was replaced and adjusted so not to contact the oil drain piping and the pump returned to service. Investigation into the cause of the release, determined the pump oil drain piping had inadvertently been installed in contact with the cooler inlet tubing during previous maintenance activities.
Report Received Date 2020-07-20 00:00:00
Iyear 2020
Report Number 20200210
Supplemental Number 34054
Report Type Original Final
Operator Id 32109 PHMSA Enforcement
Name Oneok Ngl Pipeline, Llc
Operator Street Address 100 West Fifth Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2020-06-30 21:25:00
Location Latitude 31.05151 Google Maps OpenStreetMap
Location Longitude -95.24527 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 0.14
Intentional Release Bbls 9.86
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime 2020-06-30 21:15:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2020-06-30 20:28:00
Restart Datetime 2020-06-30 21:30:00
On Site Datetime 2020-06-30 21:15:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Groveton Sterling Ii Pump Station
Segment Name Sterling Ii - Medford To Ombs 12in
Onshore State Abbreviation Tx
Onshore Postal Code 75845
Onshore City Name Not Within A Municipality
Onshore County Name Trinity
Designated Location Milepost/valve Station
Designated Name Pump Station
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Pump
Installation Year 2007
Material Involved Material Other Than Carbon Steel
Material Details Stainless Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 15
Est Cost Prop Damage 1500
Est Cost Emergency 150
Est Cost Environmental 0
Est Cost Other 750
Est Cost Other Details Release Investigation
Prpty 2415
Accident Psig 766
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details There were no controller actions or control room issues
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Pump Or Pump-Related Equipment
Eq Failure Type Pump Or Pump-Related Equipment
Other Pump Ind Other
Other Pump Details 1/2" Outboard Bearing Cooler Inlet Tubing
Eq Additional Other Ind Yes
Eq Additional Other Details Metal To Metal Friction
Preparer Name M***** C********
Preparer Title Regulatory Compliance Specialist
Preparer Email M***************@o****.com
Preparer Telephone 2542928911
Prepared Date 2020-07-20 00:00:00
Authorizer Name M***** C********
Authorizer Telephone 2542928911
Authorizer Title Regulatory Compliance Specialist
Authorizer Email M***************@o****.com
Narrative On june 30th, 2020 at approximately 8:28 pm, oneok pipeline control center received a gas detect alarm for the oneok sterling ii groveton pump station. The gas detect alarm activated the station shutdown and isolated the pump station. Oneok pipeline control dispatched local field operations to the location. At approximately 9:15pm, the oneok field operator arrived on site and noticed vapors in the vicinity of the number 1 pump. Field operator isolated the pump and began evacuating hydrocarbons from the pump and associated piping at 9:25pm. After evacuation of hydrocarbons, a pinhole leak in the outboard bearing cooler return tubing was discovered as the source of the release. The affected tubing was found to be in contact with the outboard oil drain piping, resulting in a pinhole developing in the tubing, because of friction. The tubing was replaced and adjusted so not to contact the oil drain piping and the pump returned to service. Investigation into the cause of the release, determined the pump oil drain piping had inadvertently been installed in contact with the cooler inlet tubing during previous maintenance activities.

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