HL incident on 2020-06-19 — OK

Operator
Magellan Pipeline Company, Lp
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$50
Incident datetime
2020-06-19 19:30
Report number
Location
OK
Narrative
At 19:30 on 6/19/20, magellan operations personnel were conducting tank checks when they noticed the tank 1501 booster pump leaking product into secondary containment. The line was shut down, the segment was isolated, and cleanup activities were initiated. The nipple on the booster pump sheared off where it connects to the pipe, likely contributed to excessive vibration. Programming is being assessed which would enable the line to pack before startup, reducing the potential for vibration
Detailed record list
Report Received Date
2020-07-17 00:00:00
Iyear
2020
Report Number
20200209
Supplemental Number
34052
Report Type
Original Final
Operator Id
Name
Magellan Pipeline Company, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2020-06-19 19:30:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
221
Recovered Bbls
221
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2020-06-19 19:30:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2020-06-19 19:33:00
Restart Datetime
2020-06-20 08:00:00
On Site Datetime
2020-06-19 19:35:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
East Houston
Segment Name
Terminal No. 357
Onshore State Abbreviation
Tx
Onshore Postal Code
77029
Onshore City Name
Houston
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Other
Item Involved Details
Nipple
Installation Year
2012
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
50
Est Cost Emergency
40500
Est Cost Environmental
0
Est Cost Other
0
Prpty
40550
Accident Psig
50
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The release was inside the facility upstream of the meter. There were no flow deviations or alarms during the event due to the small volume released.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Threaded Connection/coupling Failure
Eq Failure Type
Threaded Connection/coupling Failure
Other Stripped Ind
Pipe Nipple
Additional Vibration Ind
Yes
Preparer Name
S****** L******
Preparer Title
Ai Analyst
Preparer Email
S**************@m*********.com
Preparer Telephone
918-574-7327
Preparer Fax
918-574-7376
Prepared Date
2020-07-17 00:00:00
Authorizer Name
G**** R****
Authorizer Telephone
918-574-7165
Authorizer Title
Supervisor Integrity Management
Authorizer Email
G**********@m*********.com
Narrative
At 19:30 on 6/19/20, magellan operations personnel were conducting tank checks when they noticed the tank 1501 booster pump leaking product into secondary containment. The line was shut down, the segment was isolated, and cleanup activities were initiated. The nipple on the booster pump sheared off where it connects to the pipe, likely contributed to excessive vibration. Programming is being assessed which would enable the line to pack before startup, reducing the potential for vibration
Report Received Date 2020-07-17 00:00:00
Iyear 2020
Report Number 20200209
Supplemental Number 34052
Report Type Original Final
Operator Id 22610 PHMSA Enforcement
Name Magellan Pipeline Company, Lp
Operator Street Address 100 West 5th Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2020-06-19 19:30:00
Location Latitude 29.794256 Google Maps OpenStreetMap
Location Longitude -95.285208 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 221
Recovered Bbls 221
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2020-06-19 19:30:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2020-06-19 19:33:00
Restart Datetime 2020-06-20 08:00:00
On Site Datetime 2020-06-19 19:35:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name East Houston
Segment Name Terminal No. 357
Onshore State Abbreviation Tx
Onshore Postal Code 77029
Onshore City Name Houston
Onshore County Name Harris
Designated Location Milepost/valve Station
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Other
Item Involved Details Nipple
Installation Year 2012
Material Involved Carbon Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 50
Est Cost Emergency 40500
Est Cost Environmental 0
Est Cost Other 0
Prpty 40550
Accident Psig 50
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The release was inside the facility upstream of the meter. There were no flow deviations or alarms during the event due to the small volume released.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Threaded Connection/coupling Failure
Eq Failure Type Threaded Connection/coupling Failure
Other Stripped Ind Pipe Nipple
Additional Vibration Ind Yes
Preparer Name S****** L******
Preparer Title Ai Analyst
Preparer Email S**************@m*********.com
Preparer Telephone 918-574-7327
Preparer Fax 918-574-7376
Prepared Date 2020-07-17 00:00:00
Authorizer Name G**** R****
Authorizer Telephone 918-574-7165
Authorizer Title Supervisor Integrity Management
Authorizer Email G**********@m*********.com
Narrative At 19:30 on 6/19/20, magellan operations personnel were conducting tank checks when they noticed the tank 1501 booster pump leaking product into secondary containment. The line was shut down, the segment was isolated, and cleanup activities were initiated. The nipple on the booster pump sheared off where it connects to the pipe, likely contributed to excessive vibration. Programming is being assessed which would enable the line to pack before startup, reducing the potential for vibration

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