HL incident on 2020-06-17 — OK

Operator
Magellan Pipeline Company, Lp
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$100
Incident datetime
2020-06-17 10:15
Report number
Location
OK
Narrative
At 10:15 on 6/17/2020, magellan operations personnel noticed product leaking from the strainer on a 12" line within the iowa city terminal. The line was shutdown, the strainer was isolated and cleanup activities were performed. Upon further investigation, it was determined that an o-ring on the strainer lid had failed due to normal wear and tear. The o-ring was replaced and the line was placed back into service
Detailed record list
Report Received Date
2020-07-16 00:00:00
Iyear
2020
Report Number
20200208
Supplemental Number
34046
Report Type
Original Final
Operator Id
Name
Magellan Pipeline Company, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2020-06-17 10:15:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
0.24
Recovered Bbls
0.24
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2020-06-17 10:15:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2020-06-17 10:23:00
Restart Datetime
2020-06-17 15:57:00
On Site Datetime
2020-06-17 10:20:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Iowa City Terminal
Segment Name
Term. No. 202
Onshore State Abbreviation
Ia
Onshore Postal Code
52241
Onshore City Name
Coralville
Onshore County Name
Johnson
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Other
Item Involved Details
Strainer.
Installation Year
1986
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
50
Est Cost Prop Damage
100
Est Cost Emergency
2500
Est Cost Environmental
0
Est Cost Other
0
Prpty
2650
Accident Psig
90
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Investigation determined control room personnel did not contribute to the cause of the event
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
O-Ring
Eq Additional Other Ind
Yes
Eq Additional Other Details
Normal Wear And Tear
Preparer Name
S****** L******
Preparer Title
Ai Analyst
Preparer Email
S**************@m*********.com
Preparer Telephone
918-574-7327
Preparer Fax
918-574-7376
Prepared Date
2020-07-16 00:00:00
Authorizer Name
G**** R****
Authorizer Telephone
918-574-7165
Authorizer Title
Supervisor Integrity Management
Authorizer Email
G**********@m*********.com
Narrative
At 10:15 on 6/17/2020, magellan operations personnel noticed product leaking from the strainer on a 12" line within the iowa city terminal. The line was shutdown, the strainer was isolated and cleanup activities were performed. Upon further investigation, it was determined that an o-ring on the strainer lid had failed due to normal wear and tear. The o-ring was replaced and the line was placed back into service
Report Received Date 2020-07-16 00:00:00
Iyear 2020
Report Number 20200208
Supplemental Number 34046
Report Type Original Final
Operator Id 22610 PHMSA Enforcement
Name Magellan Pipeline Company, Lp
Operator Street Address 100 West 5th Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2020-06-17 10:15:00
Location Latitude 41.682031 Google Maps OpenStreetMap
Location Longitude -91.56983 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 0.24
Recovered Bbls 0.24
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2020-06-17 10:15:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2020-06-17 10:23:00
Restart Datetime 2020-06-17 15:57:00
On Site Datetime 2020-06-17 10:20:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Iowa City Terminal
Segment Name Term. No. 202
Onshore State Abbreviation Ia
Onshore Postal Code 52241
Onshore City Name Coralville
Onshore County Name Johnson
Designated Location Milepost/valve Station
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Other
Item Involved Details Strainer.
Installation Year 1986
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 50
Est Cost Prop Damage 100
Est Cost Emergency 2500
Est Cost Environmental 0
Est Cost Other 0
Prpty 2650
Accident Psig 90
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Investigation determined control room personnel did not contribute to the cause of the event
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind O-Ring
Eq Additional Other Ind Yes
Eq Additional Other Details Normal Wear And Tear
Preparer Name S****** L******
Preparer Title Ai Analyst
Preparer Email S**************@m*********.com
Preparer Telephone 918-574-7327
Preparer Fax 918-574-7376
Prepared Date 2020-07-16 00:00:00
Authorizer Name G**** R****
Authorizer Telephone 918-574-7165
Authorizer Title Supervisor Integrity Management
Authorizer Email G**********@m*********.com
Narrative At 10:15 on 6/17/2020, magellan operations personnel noticed product leaking from the strainer on a 12" line within the iowa city terminal. The line was shutdown, the strainer was isolated and cleanup activities were performed. Upon further investigation, it was determined that an o-ring on the strainer lid had failed due to normal wear and tear. The o-ring was replaced and the line was placed back into service

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