Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2020-06-08 — OK
Operator
Magellan Pipeline Company, Lp
Cause
Miscellaneous Root Causes
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$2,333,500
Incident datetime
2020-06-08 14:51
Report number
Location
OK
Narrative
At 14:28 on june 8, 2020, magellan's tulsa - barnsdall #4-12" pipeline was impacted by a second party line strike during horizontal directional drilling operation. At the time of the incident, magellan's contractor was performing the pilot hole operation for the #3-12" pipeline replacement across the arkansas river and struck the #4-12" pipeline north of the arkansas river between the north levee and charles page blvd. Code red response was initiated and field personnel were dispatched to further isolate the blocked in section with manual valves and begin cleanup activities. At the time of the incident, the pipeline was shut down and isolated with remote isolation valves. The #4-12" pipeline was returned to service by commissioning a newly installed hdd replacement crossing for the #1-12". The impacted pipeline segment will be grout filled and abandoned in place. The puncture size is an estimate based on release volume. Nrc 48-hour update: #1279210, 06/09/14:12 supplemental/final:(09/11/2020) part a11, d8, e9, g3-17, h
Detailed record list
Report Received Date
2020-07-08 00:00:00
Iyear
2020
Report Number
20200201
Supplemental Number
34259
Report Type
Supplemental Final
Operator Id
22610
Name
Magellan Pipeline Company, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2020-06-08 14:28:00
Location Latitude
36.147988
Location Longitude
-96.032858
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
218
Recovered Bbls
214
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2020-06-08 14:51:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2020-06-08 15:01:00
Restart Datetime
2020-06-26 18:54:00
On Site Datetime
2020-06-08 15:15:00
Nrc Rpt Datetime
2020-06-08 15:20:00
Nrc Rpt Num
1279133
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
0
Pipe Fac Name
Tulsa-Barnsdall No. 4-12" Line
Segment Name
Line Id 6045
Onshore State Abbreviation
Ok
Onshore Postal Code
74127
Onshore City Name
Tulsa
Onshore County Name
Tulsa
Designated Location
Milepost/valve Station
Designated Name
1.16
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
672
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
12
Pipe Wall Thickness
0.375
Pipe Smys
52000
Pipe Specification
Api - 5l - X52
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Us Steel
Pipe Coating Type
Fusion Bonded Epoxy(Fbe)
Installation Year
2002
Manufactured Year
2000
Material Involved
Carbon Steel
Release Type
Mechanical Puncture
Puncture Axial
2
Puncture Circum
2
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
50000
Est Cost Gas Released
10800
Est Cost Prop Damage
2333500
Est Cost Emergency
585000
Est Cost Environmental
0
Est Cost Other
0
Prpty
2979300
Accident Psig
370
Mop Psig
1246
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
73920
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
Yes
Cpm Conf Ind
Yes
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind
Yes
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
Yes
Num Employees Tested
1
Num Employees Failed
0
Num Contractors Tested
3
Num Contractors Failed
0
Cause
Excavation Damage
Cause Details
Excavation Damage By Operator's Contractor (Second Party)
Ex Party Type
Excavation Damage By Operator's Contractor (Second Party)
Notify Cga Dirt
No
Pipeline Easement Row Ind
Yes
Excavator Type
Contractor
Excavator Equipment
Directional Drilling
Work Performed
Liquid Pipeline
One Call Notified Ind
Yes
One Call Ticket Num
2.00527e+13
Locator Type
Utility Owner
Visible Marks
Unknown/other
Service Interruption
Yes
Service Interruption Hours
436
Root Cause Category
Miscellaneous Root Causes
Root Cause Type
Root Cause Not Listed (Comment Required)
Root Cause Type Other
Engineering Design Firm Failed To Properly Show Existing Pipeline Location
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Cir Trn Wave Mgn Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Emat Ind
Yes
Axial Recent Year
2005
Circ Wave Recent Year
2010
Geometry Recent Year
2020
Emat Recent Year
2020
Other Recent Year
2020
Insp Compl Before Damage Ind
Yes
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
S****** L******
Preparer Title
Ai Analyst
Preparer Email
S**************@m*********.com
Preparer Telephone
918-574-7327
Preparer Fax
918-574-7376
Prepared Date
2020-09-11 00:00:00
Authorizer Name
G**** R****
Authorizer Telephone
918-574-7165
Authorizer Title
Supervisor Integrity Management
Authorizer Email
G**********@m*********.com
Narrative
At 14:28 on june 8, 2020, magellan's tulsa - barnsdall #4-12" pipeline was impacted by a second party line strike during horizontal directional drilling operation. At the time of the incident, magellan's contractor was performing the pilot hole operation for the #3-12" pipeline replacement across the arkansas river and struck the #4-12" pipeline north of the arkansas river between the north levee and charles page blvd. Code red response was initiated and field personnel were dispatched to further isolate the blocked in section with manual valves and begin cleanup activities. At the time of the incident, the pipeline was shut down and isolated with remote isolation valves. The #4-12" pipeline was returned to service by commissioning a newly installed hdd replacement crossing for the #1-12". The impacted pipeline segment will be grout filled and abandoned in place. The puncture size is an estimate based on release volume. Nrc 48-hour update: #1279210, 06/09/14:12 supplemental/final:(09/11/2020) part a11, d8, e9, g3-17, h
| Report Received Date | 2020-07-08 00:00:00 |
|---|---|
| Iyear | 2020 |
| Report Number | 20200201 |
| Supplemental Number | 34259 |
| Report Type | Supplemental Final |
| Operator Id | 22610 PHMSA Enforcement |
| Name | Magellan Pipeline Company, Lp |
| Operator Street Address | 100 West 5th Street |
| Operator City Name | Tulsa |
| Operator State Abbreviation | OK |
| Operator Postal Code | 74103 |
| Local Datetime | 2020-06-08 14:28:00 |
| Location Latitude | 36.147988 Google Maps OpenStreetMap |
| Location Longitude | -96.032858 Google Maps OpenStreetMap |
| Commodity Released Type | Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions |
| Commodity Subtype | Diesel, Fuel Oil, Kerosene, Jet Fuel |
| Unintentional Release Bbls | 218 |
| Recovered Bbls | 214 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations) |
| Incident Identified Datetime | 2020-06-08 14:51:00 |
| System Part Involved | Onshore Pipeline, Including Valve Sites |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | Yes |
| Shutdown Datetime | 2020-06-08 15:01:00 |
| Restart Datetime | 2020-06-26 18:54:00 |
| On Site Datetime | 2020-06-08 15:15:00 |
| Nrc Rpt Datetime | 2020-06-08 15:20:00 |
| Nrc Rpt Num | 1279133 NRC Report How to search |
| Ignite Ind | No |
| Explode Ind | No |
| Upstream Valve Type Ind | Remotely Controlled |
| Downstream Valve Type Ind | Remotely Controlled |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Tulsa-Barnsdall No. 4-12" Line |
| Segment Name | Line Id 6045 |
| Onshore State Abbreviation | Ok |
| Onshore Postal Code | 74127 |
| Onshore City Name | Tulsa |
| Onshore County Name | Tulsa |
| Designated Location | Milepost/valve Station |
| Designated Name | 1.16 |
| Federal | No |
| Location Type | Pipeline Right-Of-Way |
| Incident Area Type | Underground |
| Incident Area Subtype | Under Soil |
| Depth Of Cover | 672 |
| Crossing | No |
| Pipe Facility Type | Interstate |
| Item Involved | Pipe |
| Pipe Type | Pipe Body |
| Pipe Diameter | 12 |
| Pipe Wall Thickness | 0.375 |
| Pipe Smys | 52000 |
| Pipe Specification | Api - 5l - X52 |
| Pipe Seam Type | Erw - High Frequency |
| Pipe Manufacturer | Us Steel |
| Pipe Coating Type | Fusion Bonded Epoxy(Fbe) |
| Installation Year | 2002 |
| Manufactured Year | 2000 |
| Material Involved | Carbon Steel |
| Release Type | Mechanical Puncture |
| Puncture Axial | 2 |
| Puncture Circum | 2 |
| Wildlife Impact Ind | No |
| Soil Contamination | Yes |
| Long Term Assessment | No |
| Remediation Ind | No |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | Yes |
| High Pop Ind | Yes |
| High Pop Yes No | Yes |
| Est Cost Oper Paid | 50000 |
| Est Cost Gas Released | 10800 |
| Est Cost Prop Damage | 2333500 |
| Est Cost Emergency | 585000 |
| Est Cost Environmental | 0 |
| Est Cost Other | 0 |
| Prpty | 2979300 |
| Accident Psig | 370 |
| Mop Psig | 1246 |
| Accident Pressure | Pressure Did Not Exceed Mop |
| Pressure Restriction Ind | No |
| Length Segment Isolated | 73920 |
| Internal Inspection Ind | Yes |
| Operation Complications Ind | No |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Scada In Place Ind | Yes |
| Scada Operating Ind | Yes |
| Scada Functional Ind | Yes |
| Scada Detection Ind | Yes |
| Scada Conf Ind | Yes |
| Cpm In Place Ind | Yes |
| Cpm Operating Ind | Yes |
| Cpm Functional Ind | Yes |
| Cpm Detection Ind | Yes |
| Cpm Conf Ind | Yes |
| Investigation Status | Yes, specify investigation result(s): (select all that apply) |
| Invest No Control Room Ind | Yes |
| Employee Drug Test Ind | Yes |
| Contractor Drug Test Ind | Yes |
| Num Employees Tested | 1 |
| Num Employees Failed | 0 |
| Num Contractors Tested | 3 |
| Num Contractors Failed | 0 |
| Cause | Excavation Damage |
| Cause Details | Excavation Damage By Operator's Contractor (Second Party) |
| Ex Party Type | Excavation Damage By Operator's Contractor (Second Party) |
| Notify Cga Dirt | No |
| Pipeline Easement Row Ind | Yes |
| Excavator Type | Contractor |
| Excavator Equipment | Directional Drilling |
| Work Performed | Liquid Pipeline |
| One Call Notified Ind | Yes |
| One Call Ticket Num | 2.00527e+13 |
| Locator Type | Utility Owner |
| Visible Marks | Unknown/other |
| Service Interruption | Yes |
| Service Interruption Hours | 436 |
| Root Cause Category | Miscellaneous Root Causes |
| Root Cause Type | Root Cause Not Listed (Comment Required) |
| Root Cause Type Other | Engineering Design Firm Failed To Properly Show Existing Pipeline Location |
| Collected Data Ind | Yes |
| Axial Magnetic Flx Lkg Ind | Yes |
| Cir Trn Wave Mgn Flx Lkg Ind | Yes |
| Geometry Deformation Ind | Yes |
| Emat Ind | Yes |
| Axial Recent Year | 2005 |
| Circ Wave Recent Year | 2010 |
| Geometry Recent Year | 2020 |
| Emat Recent Year | 2020 |
| Other Recent Year | 2020 |
| Insp Compl Before Damage Ind | Yes |
| Has Hydrtst Conduc Before Ind | No |
| Direct Asmnt Conducted | No |
| Non Destructive Exam Ind | No |
| Preparer Name | S****** L****** |
| Preparer Title | Ai Analyst |
| Preparer Email | S**************@m*********.com |
| Preparer Telephone | 918-574-7327 |
| Preparer Fax | 918-574-7376 |
| Prepared Date | 2020-09-11 00:00:00 |
| Authorizer Name | G**** R**** |
| Authorizer Telephone | 918-574-7165 |
| Authorizer Title | Supervisor Integrity Management |
| Authorizer Email | G**********@m*********.com |
| Narrative | At 14:28 on june 8, 2020, magellan's tulsa - barnsdall #4-12" pipeline was impacted by a second party line strike during horizontal directional drilling operation. At the time of the incident, magellan's contractor was performing the pilot hole operation for the #3-12" pipeline replacement across the arkansas river and struck the #4-12" pipeline north of the arkansas river between the north levee and charles page blvd. Code red response was initiated and field personnel were dispatched to further isolate the blocked in section with manual valves and begin cleanup activities. At the time of the incident, the pipeline was shut down and isolated with remote isolation valves. The #4-12" pipeline was returned to service by commissioning a newly installed hdd replacement crossing for the #1-12". The impacted pipeline segment will be grout filled and abandoned in place. The puncture size is an estimate based on release volume. Nrc 48-hour update: #1279210, 06/09/14:12 supplemental/final:(09/11/2020) part a11, d8, e9, g3-17, h |
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