HL incident on 2020-06-10 — TX

Operator
Enterprise Products Operating Llc
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$300,000
Incident datetime
2020-06-10 11:28
Report number
Location
TX
Narrative
On 06/09/20 at 20:49 ct, houston control center received a call from a third party near our downing block valve site indicating an odor with a possible leak. Once on site the enterprise technician discovered a small amount of product, ethane/propane, leaking from the valve stem. The technician performed maintenance on the valve and found the stem's o-ring was still leaking a deminimis amount of product. On 06/10/20 at 11:28 ct the decision was made to replace this valve to eliminate the leak. Repairs were completed 06/18/20. Initial call to nrc was made on 06/10/2020 at 12:16 cst (nrc#1279280). The call was made based on repair cost estimates exceeding $50,000. 48hr update call to nrc was made on 06/12/2020 at 10:51 cst (nrc#1279423). The update indicated that a valve replacement was underway.
Detailed record list
Report Received Date
2020-07-07 00:00:00
Iyear
2020
Report Number
20200197
Supplemental Number
34003
Report Type
Original Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2020-06-10 11:28:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
0.1
Intentional Release Bbls
4.1
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2020-06-10 11:28:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2020-06-18 06:00:00
Restart Datetime
2020-06-18 23:00:00
On Site Datetime
2020-06-10 11:28:00
Nrc Rpt Datetime
2020-06-10 12:16:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Mapl East Red Line
Segment Name
Lid 603
Onshore State Abbreviation
Mo
Onshore Postal Code
63536
Onshore City Name
Not Within A Municipality
Onshore County Name
Schuyler
Designated Location
Milepost/valve Station
Designated Name
Mp 133.9
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Mainline
Valve Mainline Type
Gate
Valve Manufacturer
Grove
Installation Year
1970
Manufactured Year
Unknown
Material Involved
Material Other Than Carbon Steel
Material Details
Buna-N
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
3000
Est Cost Gas Released
50
Est Cost Prop Damage
300000
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
303050
Accident Psig
900
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
99264
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The controllers did not contribute to causing the leak.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Block Valve Ind
Yes
Eq Additional Other Ind
Yes
Eq Additional Other Details
Material Deterioration
Preparer Name
H*** D***
Preparer Title
Sr. Pipeline Compliance Engineer
Preparer Email
H****@e****.com
Preparer Telephone
713-381-4277
Prepared Date
2020-07-07 00:00:00
Authorizer Name
H*** D***
Authorizer Telephone
713-381-4277
Authorizer Title
Sr. Pipeline Compliance Engineer
Authorizer Email
H****@e****.com
Narrative
On 06/09/20 at 20:49 ct, houston control center received a call from a third party near our downing block valve site indicating an odor with a possible leak. Once on site the enterprise technician discovered a small amount of product, ethane/propane, leaking from the valve stem. The technician performed maintenance on the valve and found the stem's o-ring was still leaking a deminimis amount of product. On 06/10/20 at 11:28 ct the decision was made to replace this valve to eliminate the leak. Repairs were completed 06/18/20. Initial call to nrc was made on 06/10/2020 at 12:16 cst (nrc#1279280). The call was made based on repair cost estimates exceeding $50,000. 48hr update call to nrc was made on 06/12/2020 at 10:51 cst (nrc#1279423). The update indicated that a valve replacement was underway.
Report Received Date 2020-07-07 00:00:00
Iyear 2020
Report Number 20200197
Supplemental Number 34003
Report Type Original Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2020-06-10 11:28:00
Location Latitude 40.45438 Google Maps OpenStreetMap
Location Longitude -92.36819 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 0.1
Intentional Release Bbls 4.1
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
Incident Identified Datetime 2020-06-10 11:28:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2020-06-18 06:00:00
Restart Datetime 2020-06-18 23:00:00
On Site Datetime 2020-06-10 11:28:00
Nrc Rpt Datetime 2020-06-10 12:16:00
Nrc Rpt Num 1279280 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Mapl East Red Line
Segment Name Lid 603
Onshore State Abbreviation Mo
Onshore Postal Code 63536
Onshore City Name Not Within A Municipality
Onshore County Name Schuyler
Designated Location Milepost/valve Station
Designated Name Mp 133.9
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Mainline
Valve Mainline Type Gate
Valve Manufacturer Grove
Installation Year 1970
Manufactured Year Unknown
Material Involved Material Other Than Carbon Steel
Material Details Buna-N
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 3000
Est Cost Gas Released 50
Est Cost Prop Damage 300000
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 303050
Accident Psig 900
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 99264
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The controllers did not contribute to causing the leak.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Block Valve Ind Yes
Eq Additional Other Ind Yes
Eq Additional Other Details Material Deterioration
Preparer Name H*** D***
Preparer Title Sr. Pipeline Compliance Engineer
Preparer Email H****@e****.com
Preparer Telephone 713-381-4277
Prepared Date 2020-07-07 00:00:00
Authorizer Name H*** D***
Authorizer Telephone 713-381-4277
Authorizer Title Sr. Pipeline Compliance Engineer
Authorizer Email H****@e****.com
Narrative On 06/09/20 at 20:49 ct, houston control center received a call from a third party near our downing block valve site indicating an odor with a possible leak. Once on site the enterprise technician discovered a small amount of product, ethane/propane, leaking from the valve stem. The technician performed maintenance on the valve and found the stem's o-ring was still leaking a deminimis amount of product. On 06/10/20 at 11:28 ct the decision was made to replace this valve to eliminate the leak. Repairs were completed 06/18/20. Initial call to nrc was made on 06/10/2020 at 12:16 cst (nrc#1279280). The call was made based on repair cost estimates exceeding $50,000. 48hr update call to nrc was made on 06/12/2020 at 10:51 cst (nrc#1279423). The update indicated that a valve replacement was underway.

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