HL incident on 2020-06-08 — KS

Operator
Nustar Pipeline Operating Partnership L.p.
Cause
Material Failure Of Pipe Or Weld
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$130,822
Incident datetime
2020-06-08 16:30
Report number
Location
KS
Narrative
Nustar confirmed the release at 16:30 on june 8, 2020. The pipeline was shut down at 17:15 on june 8, 2020. The repairs included putting a clamp around the pinhole at 20:18 on june 13, 2020. The pipeline was restarted at 20:18 on june 13, 2020. 48-hour nrc update #1279309 supplemental: the leak/release occurred at a location on the pipe that had a lack of fusion area at the erw seam bond line. During operation, outer surface pitting had occurred in the same general area. The leak occurred at the lack of fusion line where there were also several corrosion pits on the external surface of the pipe. This irregularly shaped pit was coincident with the bond line and the lack of fusion area, which acted as a crevice. Crevices are known to accelerate corrosion and the pitting widened the lack of fusion, eventually resulting in a connection between the od and id. The pitting corrosion is typical of what would occur in submerged service where the coating was either not perfect when manufactured or was damaged in usage. There were two strap marks straddling the pitted area that may have disturbed the coating locally. The external surface pitting area was generally in line with the erw weld seam at the 6:30 o'clock location (near the bottom). The coincidence of the lack of fusion (lof) and the corrosion at that location created a through hole 0.070-inch long and 0.040-inch wide on that section of pipe.
Detailed record list
Report Received Date
2020-07-06 00:00:00
Iyear
2020
Report Number
20200195
Supplemental Number
34652
Report Type
Supplemental Final
Operator Id
Name
Nustar Pipeline Operating Partnership L.p.
Operator Street Address
7340 W. 21st Street N., Suite 200
Operator City Name
Wichita
Operator State Abbreviation
KS
Operator Postal Code
67205
Local Datetime
2020-06-08 16:30:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Anhydrous Ammonia
Unintentional Release Bbls
0.5
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2020-06-08 16:30:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2020-06-08 17:15:00
Restart Datetime
2020-06-13 20:18:00
On Site Datetime
2020-06-08 16:30:00
Nrc Rpt Datetime
2020-06-08 17:37:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Ammonia Mainline
Segment Name
Chatam To Hampton 10-Inch
Onshore State Abbreviation
La
Onshore Postal Code
71222
Onshore City Name
Not Within A Municipality
Onshore County Name
Union
Designated Location
Survey Station No.
Designated Name
35.39 Mile
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
36
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
10
Pipe Wall Thickness
0.25
Pipe Smys
42000
Pipe Specification
Api 5lx-X42
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Hoesch-Thyssen
Pipe Coating Type
Other
Pipe Coating Details
Poly Tape
Installation Year
1970
Manufactured Year
1970
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
Yes
Fish Aquatic Impact Ind
Yes
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
Yes
Surface Contam Ind
Yes
Amount Released
0.5
Rel Water Name
Corney Bayou
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
130822
Est Cost Emergency
124000
Est Cost Environmental
0
Est Cost Other
0
Prpty
254822
Accident Psig
210
Mop Psig
1340
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
92241
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Metallurgical Ind
Yes
Failure Type
Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Other Factor
Yes
Other Factor Details
Occurred At Lack Of Fusion Line-Several Corrosion Pits On External Of Pipe
Additional Lack Fusion Ind
Yes
Collected Data Ind
Yes
Other Recent Year
2020
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
Yes, But The Point Of The Accident Was Not Identified As A Dig Site
Direct Asmnt Pnt Not Idntf Yr
2020
Non Destructive Exam Ind
No
Preparer Name
D***** J T******
Preparer Title
Director-Hse
Preparer Email
D**********@n***********.com
Preparer Telephone
316-721-7056
Prepared Date
2020-12-23 00:00:00
Authorizer Name
B*** F******
Authorizer Telephone
316-721-7066
Authorizer Title
General Manager
Authorizer Email
B***********@n***********.com
Narrative
Nustar confirmed the release at 16:30 on june 8, 2020. The pipeline was shut down at 17:15 on june 8, 2020. The repairs included putting a clamp around the pinhole at 20:18 on june 13, 2020. The pipeline was restarted at 20:18 on june 13, 2020. 48-hour nrc update #1279309 supplemental: the leak/release occurred at a location on the pipe that had a lack of fusion area at the erw seam bond line. During operation, outer surface pitting had occurred in the same general area. The leak occurred at the lack of fusion line where there were also several corrosion pits on the external surface of the pipe. This irregularly shaped pit was coincident with the bond line and the lack of fusion area, which acted as a crevice. Crevices are known to accelerate corrosion and the pitting widened the lack of fusion, eventually resulting in a connection between the od and id. The pitting corrosion is typical of what would occur in submerged service where the coating was either not perfect when manufactured or was damaged in usage. There were two strap marks straddling the pitted area that may have disturbed the coating locally. The external surface pitting area was generally in line with the erw weld seam at the 6:30 o'clock location (near the bottom). The coincidence of the lack of fusion (lof) and the corrosion at that location created a through hole 0.070-inch long and 0.040-inch wide on that section of pipe.
Report Received Date 2020-07-06 00:00:00
Iyear 2020
Report Number 20200195
Supplemental Number 34652
Report Type Supplemental Final
Operator Id 10012 PHMSA Enforcement
Name Nustar Pipeline Operating Partnership L.p.
Operator Street Address 7340 W. 21st Street N., Suite 200
Operator City Name Wichita
Operator State Abbreviation KS
Operator Postal Code 67205
Local Datetime 2020-06-08 16:30:00
Location Latitude 32.846528 Google Maps OpenStreetMap
Location Longitude -92.557658 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Anhydrous Ammonia
Unintentional Release Bbls 0.5
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
Incident Identified Datetime 2020-06-08 16:30:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2020-06-08 17:15:00
Restart Datetime 2020-06-13 20:18:00
On Site Datetime 2020-06-08 16:30:00
Nrc Rpt Datetime 2020-06-08 17:37:00
Nrc Rpt Num 1279145 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Ammonia Mainline
Segment Name Chatam To Hampton 10-Inch
Onshore State Abbreviation La
Onshore Postal Code 71222
Onshore City Name Not Within A Municipality
Onshore County Name Union
Designated Location Survey Station No.
Designated Name 35.39 Mile
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 36
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 10
Pipe Wall Thickness 0.25
Pipe Smys 42000
Pipe Specification Api 5lx-X42
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer Hoesch-Thyssen
Pipe Coating Type Other
Pipe Coating Details Poly Tape
Installation Year 1970
Manufactured Year 1970
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind Yes
Fish Aquatic Impact Ind Yes
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind Yes
Surface Contam Ind Yes
Amount Released 0.5
Rel Water Name Corney Bayou
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 130822
Est Cost Emergency 124000
Est Cost Environmental 0
Est Cost Other 0
Prpty 254822
Accident Psig 210
Mop Psig 1340
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 92241
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Metallurgical Ind Yes
Failure Type Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Other Factor Yes
Other Factor Details Occurred At Lack Of Fusion Line-Several Corrosion Pits On External Of Pipe
Additional Lack Fusion Ind Yes
Collected Data Ind Yes
Other Recent Year 2020
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted Yes, But The Point Of The Accident Was Not Identified As A Dig Site
Direct Asmnt Pnt Not Idntf Yr 2020
Non Destructive Exam Ind No
Preparer Name D***** J T******
Preparer Title Director-Hse
Preparer Email D**********@n***********.com
Preparer Telephone 316-721-7056
Prepared Date 2020-12-23 00:00:00
Authorizer Name B*** F******
Authorizer Telephone 316-721-7066
Authorizer Title General Manager
Authorizer Email B***********@n***********.com
Narrative Nustar confirmed the release at 16:30 on june 8, 2020. The pipeline was shut down at 17:15 on june 8, 2020. The repairs included putting a clamp around the pinhole at 20:18 on june 13, 2020. The pipeline was restarted at 20:18 on june 13, 2020. 48-hour nrc update #1279309 supplemental: the leak/release occurred at a location on the pipe that had a lack of fusion area at the erw seam bond line. During operation, outer surface pitting had occurred in the same general area. The leak occurred at the lack of fusion line where there were also several corrosion pits on the external surface of the pipe. This irregularly shaped pit was coincident with the bond line and the lack of fusion area, which acted as a crevice. Crevices are known to accelerate corrosion and the pitting widened the lack of fusion, eventually resulting in a connection between the od and id. The pitting corrosion is typical of what would occur in submerged service where the coating was either not perfect when manufactured or was damaged in usage. There were two strap marks straddling the pitted area that may have disturbed the coating locally. The external surface pitting area was generally in line with the erw weld seam at the 6:30 o'clock location (near the bottom). The coincidence of the lack of fusion (lof) and the corrosion at that location created a through hole 0.070-inch long and 0.040-inch wide on that section of pipe.

All rights reserved. Copyright © by ClearPHMSA