HL incident on 2020-06-17 — TX

Operator
Harvest Midstream Company
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$2,500
Incident datetime
2020-06-17 06:41
Report number
Location
TX
Narrative
On june 17, 2020 approximately 06:23 a hmc operator discovered oil on the ground inside secondary containment. The harvest operator contacted the control room to shut down the station, isolated the source of the leak, and began make the proper internal notifications. At approximately 07:15, it was determined that the estimated spill amount met the reporting criteria and the proper agency notifications were made. The leak was from a small section of above ground drain piping that originated form a strainer. An estimated total of 32 bbls of oil was released inside containment of which 10 bbls were recovered and the remainder was disposed of. Preventative measures to keep from reoccurring internally this leak has been classified as an operational dead leg. A review of all the stations is currently underway to identify if any other operational dead legs exist and each one will be address on a case by case basis to help mitigate reoccurrence.
Detailed record list
Report Received Date
2020-07-02 00:00:00
Iyear
2020
Report Number
20200192
Supplemental Number
34774
Report Type
Supplemental Final
Operator Id
Name
Harvest Midstream Company
Operator Street Address
1111 Travis
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2020-06-17 06:23:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
32
Recovered Bbls
32
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2020-06-17 06:41:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2020-06-17 06:31:00
Restart Datetime
2020-06-18 15:27:00
On Site Datetime
2020-06-17 06:23:00
Nrc Rpt Datetime
2020-06-17 07:52:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Three Rivers-Karnes Station
Segment Name
Three Rivers-Karnes Station
Onshore State Abbreviation
Tx
Onshore Postal Code
78118
Onshore City Name
Not Within A Municipality
Onshore County Name
Karnes
Designated Location
Milepost/valve Station
Designated Name
Karnes Statio
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Other
Incident Area Details
Strainer 2" Drain Piping
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Auxiliary Piping (E.g. Drain Lines)
Installation Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
1150
Est Cost Prop Damage
2500
Est Cost Emergency
240
Est Cost Environmental
9500
Est Cost Other
0
Prpty
13390
Accident Psig
10
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
80
Internal Inspection Ind
No
Diameter Change Ind
Yes
Other Restrictions Ind
Yes
Other Inspection Ind
Yes
Internal Inspection Details
Drain Piping
Operation Complications Ind
Yes
Other Complications Ind
Yes
Inspect Comp Details
Drain Pipeline
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The leak was to small to be detected by the control room.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Other Corrosion Ind
Yes
Int Corrosion Type Details
The Presence Of Elemental Sulfur As Indicated In The Metallurgical Analysis Is Believed To Have Influenced The Localized Pitting.
Int Metallurgical Basis Ind
Yes
Int Other Loc Ind
Yes
Corrosion Location Details
Low Point Drain
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Preparer Name
T*** S* B****
Preparer Title
Sr. Regulatory Compliance Specialist
Preparer Email
T******@h***************.com
Preparer Telephone
7132892688
Prepared Date
2021-01-27 00:00:00
Authorizer Name
T*** S* B****
Authorizer Telephone
7132892688
Authorizer Title
Sr. Regulatory Compliance Specialist
Authorizer Email
T******@h***************.com
Narrative
On june 17, 2020 approximately 06:23 a hmc operator discovered oil on the ground inside secondary containment. The harvest operator contacted the control room to shut down the station, isolated the source of the leak, and began make the proper internal notifications. At approximately 07:15, it was determined that the estimated spill amount met the reporting criteria and the proper agency notifications were made. The leak was from a small section of above ground drain piping that originated form a strainer. An estimated total of 32 bbls of oil was released inside containment of which 10 bbls were recovered and the remainder was disposed of. Preventative measures to keep from reoccurring internally this leak has been classified as an operational dead leg. A review of all the stations is currently underway to identify if any other operational dead legs exist and each one will be address on a case by case basis to help mitigate reoccurrence.
Report Received Date 2020-07-02 00:00:00
Iyear 2020
Report Number 20200192
Supplemental Number 34774
Report Type Supplemental Final
Operator Id 30782 PHMSA Enforcement
Name Harvest Midstream Company
Operator Street Address 1111 Travis
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2020-06-17 06:23:00
Location Latitude 28.84673 Google Maps OpenStreetMap
Location Longitude -98.08649 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 32
Recovered Bbls 32
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2020-06-17 06:41:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2020-06-17 06:31:00
Restart Datetime 2020-06-18 15:27:00
On Site Datetime 2020-06-17 06:23:00
Nrc Rpt Datetime 2020-06-17 07:52:00
Nrc Rpt Num 1279754 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Three Rivers-Karnes Station
Segment Name Three Rivers-Karnes Station
Onshore State Abbreviation Tx
Onshore Postal Code 78118
Onshore City Name Not Within A Municipality
Onshore County Name Karnes
Designated Location Milepost/valve Station
Designated Name Karnes Statio
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Other
Incident Area Details Strainer 2" Drain Piping
Crossing No
Pipe Facility Type Intrastate
Item Involved Auxiliary Piping (E.g. Drain Lines)
Installation Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 1150
Est Cost Prop Damage 2500
Est Cost Emergency 240
Est Cost Environmental 9500
Est Cost Other 0
Prpty 13390
Accident Psig 10
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 80
Internal Inspection Ind No
Diameter Change Ind Yes
Other Restrictions Ind Yes
Other Inspection Ind Yes
Internal Inspection Details Drain Piping
Operation Complications Ind Yes
Other Complications Ind Yes
Inspect Comp Details Drain Pipeline
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The leak was to small to be detected by the control room.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Other Corrosion Ind Yes
Int Corrosion Type Details The Presence Of Elemental Sulfur As Indicated In The Metallurgical Analysis Is Believed To Have Influenced The Localized Pitting.
Int Metallurgical Basis Ind Yes
Int Other Loc Ind Yes
Corrosion Location Details Low Point Drain
Corrosion Inhibitors No
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Not Applicable - Not Mainline Pipe
Preparer Name T*** S* B****
Preparer Title Sr. Regulatory Compliance Specialist
Preparer Email T******@h***************.com
Preparer Telephone 7132892688
Prepared Date 2021-01-27 00:00:00
Authorizer Name T*** S* B****
Authorizer Telephone 7132892688
Authorizer Title Sr. Regulatory Compliance Specialist
Authorizer Email T******@h***************.com
Narrative On june 17, 2020 approximately 06:23 a hmc operator discovered oil on the ground inside secondary containment. The harvest operator contacted the control room to shut down the station, isolated the source of the leak, and began make the proper internal notifications. At approximately 07:15, it was determined that the estimated spill amount met the reporting criteria and the proper agency notifications were made. The leak was from a small section of above ground drain piping that originated form a strainer. An estimated total of 32 bbls of oil was released inside containment of which 10 bbls were recovered and the remainder was disposed of. Preventative measures to keep from reoccurring internally this leak has been classified as an operational dead leg. A review of all the stations is currently underway to identify if any other operational dead legs exist and each one will be address on a case by case basis to help mitigate reoccurrence.

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