HL incident on 2020-05-27 — TX

Operator
Targa Downstream Llc
Cause
Corrosion Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,035,000
Incident datetime
2020-05-27 15:15
Report number
Location
TX
Narrative
A targa pipeline technician discovered vapor releasing on targa's peregrine pipeline row. The peregrine lateral transports y grade ngl. An investigation determined the release was coming from targa's pipeline and the pipeline was shut-down and de-inventoried using a pipeline pig pushed with nitrogen. The segment of pipeline that failed is a bored segment installed by directional drill. The length of the drill is 926 feet with a maximum depth below grade of 70 feet. Removing the pipeline to determine the cause of the failure has been difficult and time consuming because of the depth and length of the drilled segment. A corroded area with pitting that created a hole in the pipe wall has been found at the location where pipe was 30 feet below grade. The hole has been measured at 3/8 inch in diameter. An investigation with corrosion specialists is on-going to determine the cause of the corrosion. The failed segment will also be sent to a metallurgical lab for analysis. Targa will run an in-line inspection of the peregrine lateral to assess the integrity of the pipeline once the failed segment is replaced. Eight quail were found that were killed by the release. A texas state wildlife official was notified. The section of pipe where the leak occurred was installed by a horizontal directional drill. That section was replaced by a horizontal directional drill. The pipeline lost coating when installed by the horizontal directional drill due to rocky soil conditions. External corrosion was caused by dc stray current interference from a combined operation of cathodic protection systems for the nearby pipelines most prevalent before cathodic protection for the pipeline was activated after construction. The following measures are being adopted to a prevent a similar accident in the future. 1. Enhanced design study to include investigating r.O.W. For interference issues to include anodic/cathodic interference along with the purpose of ac/dc cathodic protection design. 2. Enhance native study to provide native reading and to investigate any possible interference issues before cp is commissioned. 3. Install interim galvanic cp systems on segments installed by horizontal directional drill for temporary protection until permanent cp system is energized. The ili run after repair did not identify any actional anomalies.
Detailed record list
Report Received Date
2020-06-26 00:00:00
Iyear
2020
Report Number
20200188
Supplemental Number
34527
Report Type
Supplemental Final
Operator Id
Name
Targa Downstream Llc
Operator Street Address
811 Louisiana St. Suite 2100
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2020-05-27 14:00:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
1800
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Ground Patrol By Operator Or Its Contractor
Operator Type
Operator Employee
Incident Identified Datetime
2020-05-27 15:15:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2020-05-27 15:15:00
Restart Datetime
2020-08-05 11:00:00
On Site Datetime
2020-05-27 15:10:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
0
Pipe Fac Name
Grand Prix
Segment Name
Peregrine Lateral
Onshore State Abbreviation
Tx
Onshore Postal Code
79855
Onshore City Name
Van Horn
Onshore County Name
Culberson
Designated Location
Survey Station No.
Designated Name
65200
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
360
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Weld, Including Heat-Affected Zone
Pipe Diameter
12.75
Pipe Wall Thickness
0.33
Pipe Smys
60000
Pipe Specification
Api 5l Hfw Psl2
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Axis Pipe And Tube
Pipe Coating Type
Field Applied Epoxy
Weld Subtype
Pipe Girth Weld
Installation Year
2019
Manufactured Year
2019
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
3/8" Diameter Hole.
Wildlife Impact Ind
Yes
Birds Impact Ind
Yes
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
30000
Est Cost Prop Damage
1035000
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
1065000
Accident Psig
764
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
89760
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
Yes
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Pipeline in steady state operation at time of discovery. No changes to operation occurring at time of discovery.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
Localized Pitting
Stray Current Corrosion Ind
Yes
Field Exam Basis Ind
Yes
Metallurgical Basis Ind
Yes
Underground Location
Yes
Under Cathodic Protection Ind
Yes
Cathodic Pro Start Year
2020
Shielding Evident
No
Cathodic Survey Type
Yes
Cp Annual Survey Ind
Yes
Cp Annual Survey Year
2020
Prior Damage
No
Collected Data Ind
Yes
Geometry Recent Year
2019
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
T** H*****
Preparer Title
Manager Operational Discipline
Preparer Email
T******@t*************.com
Preparer Telephone
3375835200
Preparer Fax
3375834630
Prepared Date
2020-11-12 00:00:00
Authorizer Name
T** H*****
Authorizer Telephone
3375835200
Authorizer Title
Manager Operational Discipline
Authorizer Email
T******@t*************.com
Narrative
A targa pipeline technician discovered vapor releasing on targa's peregrine pipeline row. The peregrine lateral transports y grade ngl. An investigation determined the release was coming from targa's pipeline and the pipeline was shut-down and de-inventoried using a pipeline pig pushed with nitrogen. The segment of pipeline that failed is a bored segment installed by directional drill. The length of the drill is 926 feet with a maximum depth below grade of 70 feet. Removing the pipeline to determine the cause of the failure has been difficult and time consuming because of the depth and length of the drilled segment. A corroded area with pitting that created a hole in the pipe wall has been found at the location where pipe was 30 feet below grade. The hole has been measured at 3/8 inch in diameter. An investigation with corrosion specialists is on-going to determine the cause of the corrosion. The failed segment will also be sent to a metallurgical lab for analysis. Targa will run an in-line inspection of the peregrine lateral to assess the integrity of the pipeline once the failed segment is replaced. Eight quail were found that were killed by the release. A texas state wildlife official was notified. The section of pipe where the leak occurred was installed by a horizontal directional drill. That section was replaced by a horizontal directional drill. The pipeline lost coating when installed by the horizontal directional drill due to rocky soil conditions. External corrosion was caused by dc stray current interference from a combined operation of cathodic protection systems for the nearby pipelines most prevalent before cathodic protection for the pipeline was activated after construction. The following measures are being adopted to a prevent a similar accident in the future. 1. Enhanced design study to include investigating r.O.W. For interference issues to include anodic/cathodic interference along with the purpose of ac/dc cathodic protection design. 2. Enhance native study to provide native reading and to investigate any possible interference issues before cp is commissioned. 3. Install interim galvanic cp systems on segments installed by horizontal directional drill for temporary protection until permanent cp system is energized. The ili run after repair did not identify any actional anomalies.
Report Received Date 2020-06-26 00:00:00
Iyear 2020
Report Number 20200188
Supplemental Number 34527
Report Type Supplemental Final
Operator Id 39823 PHMSA Enforcement
Name Targa Downstream Llc
Operator Street Address 811 Louisiana St. Suite 2100
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2020-05-27 14:00:00
Location Latitude 31.83148 Google Maps OpenStreetMap
Location Longitude -104.18947 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 1800
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Ground Patrol By Operator Or Its Contractor
Operator Type Operator Employee
Incident Identified Datetime 2020-05-27 15:15:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2020-05-27 15:15:00
Restart Datetime 2020-08-05 11:00:00
On Site Datetime 2020-05-27 15:10:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 0
Pipe Fac Name Grand Prix
Segment Name Peregrine Lateral
Onshore State Abbreviation Tx
Onshore Postal Code 79855
Onshore City Name Van Horn
Onshore County Name Culberson
Designated Location Survey Station No.
Designated Name 65200
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 360
Crossing No
Pipe Facility Type Intrastate
Item Involved Weld, Including Heat-Affected Zone
Pipe Diameter 12.75
Pipe Wall Thickness 0.33
Pipe Smys 60000
Pipe Specification Api 5l Hfw Psl2
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer Axis Pipe And Tube
Pipe Coating Type Field Applied Epoxy
Weld Subtype Pipe Girth Weld
Installation Year 2019
Manufactured Year 2019
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other 3/8" Diameter Hole.
Wildlife Impact Ind Yes
Birds Impact Ind Yes
Soil Contamination Yes
Long Term Assessment Yes
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 30000
Est Cost Prop Damage 1035000
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 1065000
Accident Psig 764
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 89760
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind Yes
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Pipeline in steady state operation at time of discovery. No changes to operation occurring at time of discovery.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results Localized Pitting
Stray Current Corrosion Ind Yes
Field Exam Basis Ind Yes
Metallurgical Basis Ind Yes
Underground Location Yes
Under Cathodic Protection Ind Yes
Cathodic Pro Start Year 2020
Shielding Evident No
Cathodic Survey Type Yes
Cp Annual Survey Ind Yes
Cp Annual Survey Year 2020
Prior Damage No
Collected Data Ind Yes
Geometry Recent Year 2019
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name T** H*****
Preparer Title Manager Operational Discipline
Preparer Email T******@t*************.com
Preparer Telephone 3375835200
Preparer Fax 3375834630
Prepared Date 2020-11-12 00:00:00
Authorizer Name T** H*****
Authorizer Telephone 3375835200
Authorizer Title Manager Operational Discipline
Authorizer Email T******@t*************.com
Narrative A targa pipeline technician discovered vapor releasing on targa's peregrine pipeline row. The peregrine lateral transports y grade ngl. An investigation determined the release was coming from targa's pipeline and the pipeline was shut-down and de-inventoried using a pipeline pig pushed with nitrogen. The segment of pipeline that failed is a bored segment installed by directional drill. The length of the drill is 926 feet with a maximum depth below grade of 70 feet. Removing the pipeline to determine the cause of the failure has been difficult and time consuming because of the depth and length of the drilled segment. A corroded area with pitting that created a hole in the pipe wall has been found at the location where pipe was 30 feet below grade. The hole has been measured at 3/8 inch in diameter. An investigation with corrosion specialists is on-going to determine the cause of the corrosion. The failed segment will also be sent to a metallurgical lab for analysis. Targa will run an in-line inspection of the peregrine lateral to assess the integrity of the pipeline once the failed segment is replaced. Eight quail were found that were killed by the release. A texas state wildlife official was notified. The section of pipe where the leak occurred was installed by a horizontal directional drill. That section was replaced by a horizontal directional drill. The pipeline lost coating when installed by the horizontal directional drill due to rocky soil conditions. External corrosion was caused by dc stray current interference from a combined operation of cathodic protection systems for the nearby pipelines most prevalent before cathodic protection for the pipeline was activated after construction. The following measures are being adopted to a prevent a similar accident in the future. 1. Enhanced design study to include investigating r.O.W. For interference issues to include anodic/cathodic interference along with the purpose of ac/dc cathodic protection design. 2. Enhance native study to provide native reading and to investigate any possible interference issues before cp is commissioned. 3. Install interim galvanic cp systems on segments installed by horizontal directional drill for temporary protection until permanent cp system is energized. The ili run after repair did not identify any actional anomalies.

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