HL incident on 2020-05-19 — TX

Operator
Phillips 66 Pipeline Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2020-05-19 07:45
Report number
Location
TX
Narrative
Pipeliner discovered oil on the piping in the receive trap area at the sweeny midpoint pump station near louise, tx. The pipeline was not running and no active leaking was observed at the time of discovery. A spray of crude oil occurred when an inadequately torqued valve body pressure release plug was exposed to normal pipeline pressures during valve travel to the fully closed position. Spill was cleaned up and contaminated gravel was properly disposed. All other valve body bleed plugs and area fittings were checked for proper torque (none found to be deficient). Pipeliner oq was revoked, and will be required to re-qualify. 7/10/20 - final report - no changes. Incorrectly submitted as supplemental - not final. 2/8/2021 - corrected c-2 for the location of the incident to mainline, not terminal for API reporting purposes. Tf
Detailed record list
Report Received Date
2020-06-17 00:00:00
Iyear
2020
Report Number
20200183
Supplemental Number
34822
Report Type
Supplemental Final
Operator Id
Name
Phillips 66 Pipeline Llc
Operator Street Address
2331 Citywest Blvd
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77042
Local Datetime
2020-05-19 07:45:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.4
Recovered Bbls
0.4
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2020-05-19 07:45:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
System Was Not Running At The Time Of Discovery
On Site Datetime
2020-05-19 07:45:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
0
Pipe Fac Name
Sweeny Midpoint Pump Station
Segment Name
G0-08 - Central Jct. To Sweeny Jct
Onshore State Abbreviation
Tx
Onshore Postal Code
77455
Onshore City Name
Louise
Onshore County Name
Wharton
Designated Location
Milepost/valve Station
Designated Name
Pump Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
2020
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
14
Est Cost Prop Damage
0
Est Cost Emergency
20000
Est Cost Environmental
0
Est Cost Other
0
Est Cost Other Details
Cost Of Cleanup And Disposal Of Contaminated Gravel.
Prpty
20014
Accident Psig
410
Mop Psig
1480
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
32051
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Fitting leak from valve due to improper torque. No operational contributing factors.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Defective Or Loose Tubing Or Fitting
Eq Failure Type
Defective Or Loose Tubing Or Fitting
Additional Installation Ind
Yes
Preparer Name
J*** S*****
Preparer Title
Dot Coordinator
Preparer Email
J************@p**.com
Preparer Telephone
832-765-1858
Prepared Date
2021-02-08 00:00:00
Authorizer Name
T*** F****
Authorizer Telephone
832-765-1632
Authorizer Title
Director Dot Compliance
Authorizer Email
T***********@p**.com
Narrative
Pipeliner discovered oil on the piping in the receive trap area at the sweeny midpoint pump station near louise, tx. The pipeline was not running and no active leaking was observed at the time of discovery. A spray of crude oil occurred when an inadequately torqued valve body pressure release plug was exposed to normal pipeline pressures during valve travel to the fully closed position. Spill was cleaned up and contaminated gravel was properly disposed. All other valve body bleed plugs and area fittings were checked for proper torque (none found to be deficient). Pipeliner oq was revoked, and will be required to re-qualify. 7/10/20 - final report - no changes. Incorrectly submitted as supplemental - not final. 2/8/2021 - corrected c-2 for the location of the incident to mainline, not terminal for API reporting purposes. Tf
Report Received Date 2020-06-17 00:00:00
Iyear 2020
Report Number 20200183
Supplemental Number 34822
Report Type Supplemental Final
Operator Id 31684 PHMSA Enforcement
Name Phillips 66 Pipeline Llc
Operator Street Address 2331 Citywest Blvd
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77042
Local Datetime 2020-05-19 07:45:00
Location Latitude 29.092756 Google Maps OpenStreetMap
Location Longitude -96.421525 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.4
Recovered Bbls 0.4
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2020-05-19 07:45:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain System Was Not Running At The Time Of Discovery
On Site Datetime 2020-05-19 07:45:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 0
Pipe Fac Name Sweeny Midpoint Pump Station
Segment Name G0-08 - Central Jct. To Sweeny Jct
Onshore State Abbreviation Tx
Onshore Postal Code 77455
Onshore City Name Louise
Onshore County Name Wharton
Designated Location Milepost/valve Station
Designated Name Pump Station
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 2020
Material Involved Carbon Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 14
Est Cost Prop Damage 0
Est Cost Emergency 20000
Est Cost Environmental 0
Est Cost Other 0
Est Cost Other Details Cost Of Cleanup And Disposal Of Contaminated Gravel.
Prpty 20014
Accident Psig 410
Mop Psig 1480
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 32051
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Fitting leak from valve due to improper torque. No operational contributing factors.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Defective Or Loose Tubing Or Fitting
Eq Failure Type Defective Or Loose Tubing Or Fitting
Additional Installation Ind Yes
Preparer Name J*** S*****
Preparer Title Dot Coordinator
Preparer Email J************@p**.com
Preparer Telephone 832-765-1858
Prepared Date 2021-02-08 00:00:00
Authorizer Name T*** F****
Authorizer Telephone 832-765-1632
Authorizer Title Director Dot Compliance
Authorizer Email T***********@p**.com
Narrative Pipeliner discovered oil on the piping in the receive trap area at the sweeny midpoint pump station near louise, tx. The pipeline was not running and no active leaking was observed at the time of discovery. A spray of crude oil occurred when an inadequately torqued valve body pressure release plug was exposed to normal pipeline pressures during valve travel to the fully closed position. Spill was cleaned up and contaminated gravel was properly disposed. All other valve body bleed plugs and area fittings were checked for proper torque (none found to be deficient). Pipeliner oq was revoked, and will be required to re-qualify. 7/10/20 - final report - no changes. Incorrectly submitted as supplemental - not final. 2/8/2021 - corrected c-2 for the location of the incident to mainline, not terminal for API reporting purposes. Tf

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